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Difference between revisions of "37-063-35592"

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== Well Details ==
 
== Well Details ==
{| class="wikitable" width="95%"
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{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-063-35592
 
| Well ID: 37-063-35592
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 40.480573, -79.206236 | width=100% | height=100% }}  
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| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.480573, -79.206236 | width=100% | height=100% }}  
 
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| Operator Name: [[DL RESOURCES INC]]
 
| Operator Name: [[DL RESOURCES INC]]

Revision as of 20:09, 28 June 2014

Well Details

Well ID: 37-063-35592
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Operator Name: DL RESOURCES INC
First Permit Date: 2007-08-20
Last Permit Date: 2007-08-20
Spud Date: 2007-09-20
Unconventional: No
Horizontal: No
Violations: None
Latitude: 40.480573
Longitude: -79.206236

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 6016.0 358.0 0.0 0.0 0.0 0.0
2012-0 4608.0 353.0 0.0 0.0 0.0 0.0
2011-0 4085.0 212.0 0.0 0.0 0.0 0.0
2010-0 542.0 51.0 0.0 0.0 0.0 0.0
2009-0 4967.0 327.0 0.0 0.0 0.0 0.0
2008-0 5703.0 212.0 0.0 0.0 0.0 0.0
2007-0 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2013-0 PRODUCED FLUID 85.0 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273 FLUID RECOVERY SERVICE JOSEPHINE FACILITY JOSEPHINE PA

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1858268 2010-01-21 No Violations Noted Well drilled on 9/27/07 to depth of 3940 ft. Well head consisted of 8¿ pipe reduced to 4 ¿pipe reduced to 2¿ production. Total flow showed 11,190 cubic feet. Production equipment consisted of separator (200 psi), 100 bbl brine tank. Brine tank contained about <10 bbl of brine. At the time of inspection, no E&S and IW or gas leakage around well head issues at the site.

References