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Difference between revisions of "37-015-21976"

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Revision as of 17:23, 10 May 2014

Well Details

Well ID: 015-21976
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County: Bradford
Municipality: Wilmot Township
Operator Name: CHESAPEAKE APPALACHIA LLC
Farm/Lease Name: JOE BRA 3H
First Permit Date: 2011-10-12
Last Permit Date: 2011-10-12
Spud Date: 2011-11-08
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: None
Latitude: 41.600725
Longitude: -76.230738

Well Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
2019372 2011-11-15 No Violations Noted Conductor set. 2 other cellars. No one on site.
2023814 2011-12-01 No Violations Noted NOMAC 34, Comp. Man - Brandon Started drilling on 11/26/2011.

Have permit. Checked drillers log, @1359' BOP test - 11/29/2011 0 - 30' red clay, rocks 30 -36' red shale 36 - 80' gray shale (bedrock) no water 20" @ 92' (82' GL) w/ 190 sx, 15.6 ppg 13 3/8" @ 682' w/ 600 sx Cl H, 15.6 ppg, 26 bbls to surf. (11/28/2011)

2025041 2011-12-08 No Violations Noted NOMAC 34, Comp. Man - Larry Hart, checked drillers log, @ 4332'

1483' - gas show, 22 - 233 units 9 5/8" @ 2022' w/ 860 sx Cl H, 15.6 ppg, 40 bbls back to surf. of 15.6 ppg, O-TEX 12/3/2011

   They had a small gas show so they ran an inflatable packer.

BOP test 12/4/2011 - good Checked cellar, no bubbles Drilling on air. Shut down now, Had a hole in shale seperator pipe & cuttings leaked on containment. Welder is working on it now. Will clean up. Need to vac up water in all containments.

2030175 2011-12-28 No Violations Noted NOMAC 34, Comp. Man Michael Gwin(Brandon)

Stuck pipe for about 12 days Checked drillers log, @ 7509' 1483' gas show 22 - 233 u 5592'MD 6889u flare burned 2 -3 hrs 5350' Genesee Top 5530' Tully 5630' Hamilton 7400' Up. Marcellus Checked cellar, no bubbles discussed need to clean up diesel and fix any leak - all on containment- small area 1 sq ft

2036679 2012-01-20 No Violations Noted Drilling complete. Site looks good. Need to fill in around rathole, will be done.

Vent on 13 3/8" X 9 5/8" annulus. I don't have my gas meter, it's being calabrated.

2082927 2012-07-11 No Violations Noted Cellar is full of water - no bubbles.

Checked 13 3/8" x 9 5/8" annulus - no gas or comb. Crews on site working on erosion control. 2 empty cellars on site.

2086716 2012-07-27 No Violations Noted On site w/ Eric Rooney to collect gas samples. Also, Shawna, SAIC and Chris, Rods Prod Serv. Annuliu were shut in Monday, 7/23/12 @ 1130AM.

0 pressure and 0 gas on all annuli. No samples collected.

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2011-2 DRILLING FLUID WASTE 560.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE OF BRINE TO FRAC A WELL
2012-1 PRODUCED FLUID 110.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING

References