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Difference between revisions of "37-115-20676"

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m (Maintenance script moved page 42-115-20676 to 37-115-20676: -i0)
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Revision as of 19:30, 4 June 2014

Well Details

Well ID: 42-115-20676
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County: Susquehanna
Municipality: New Milford Township
Operator Name: SOUTHWESTERN ENERGY PROD CO
Farm/Lease Name: ZEFFER 3H
First Permit Date: 2011-10-04
Last Permit Date: 2011-10-04
Spud Date: 2011-10-25
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: None
Latitude: 41.814722
Longitude: -75.766052

Well Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
2031176 2012-01-03 No Violations Noted DDI-10...Co. man - Joe Davis. Circulating at time of inspection. Depth of drilling = 7665'. Walked site with Co. Man. Secondary containment in place. Drillers log on site and up to date. Cement reports show adequate cement quantities.
2074435 2012-05-31 No Violations Noted Well drilled. operator reported bubbling outside of casing. At time of inspection I observed minor bubbling between 9 5/8" and 13 3/8" casings. No other bubbling observed. No activity on site. Secondary containment still down around well. Will Follow up with Operator on condition of well. No violations observed at this time. Well tag and site i.d. sign in place.
2110216 2012-10-15 Pending DDI-10 on site drilling Zeffer 2H. During inspection checked cellar - observed bubbling in cellar of 3H. Consistent bubbling outside 9 5/8" approximately 1/4" in size. Cellar half full of water so could not see source of bubbling. Requested Operator to pump down cellar and identify source and report to DEP. Copy of detailed Summary Sheet provided for this well by Co. Man. at time of inspection. Violation is Pending.

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 148948.0 34.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-2 FLOWBACK FRACTURING SAND 466.36 Tons LANDFILL 101247 KEYSTONE SANITARY LANDFILL DUNMORE PA
2012-1 DRILL CUTTINGS 360.03 Tons LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH

References