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Difference between revisions of "34-011-20103"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-011-20103
 
| Well ID: 34-011-20103
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.5431010263, -84.3609145226 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.54198233, -84.36091864 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Auglaize County, Ohio|Auglaize]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[INNEX OIL AND GAS INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2010-02-23
 
| Spud Date: 2010-02-23
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 40.5431010263
+
| Latitude: 40.54198233
 
|-
 
|-
| Longitude: -84.3609145226
+
| Longitude: -84.36091864
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -1738332536
 
| 2013-01-30
 
|
 
| At the time of my inspection the well was being used to inject fluids collected during the release associated with Complaint #4186. Mark Amell of Amell Inc. was hired to oversee the plugging of the well for Innex Oil and Gas Inc. as soon as the remaining fluids have been injected.
 
|
 
|
 
|
 
|-
 
|-
 
| -1808706409
 
| 2012-04-30
 
|
 
| Inspect Well.
 
|
 
|
 
|
 
|-
 
|-
 
| -1825346400
 
| 2012-09-11
 
|
 
| At the time of my inspection, Preliminary Restoration was passed.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1269056497
 
| 1269056497
 
| 2012-03-08
 
| 2012-03-08
|
+
|  
 
| Inspect Well. Injector rate of 60 bbl/day.
 
| Inspect Well. Injector rate of 60 bbl/day.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1273849339
 
| 1273849339
 
| 2010-05-14
 
| 2010-05-14
|
+
|  
 
| On site to witness Mechanical Integrity Test.
 
| On site to witness Mechanical Integrity Test.
 
Pulled the tubing and packer. Cleaned the drill mud from the well. Put a 40,000lb shear ring on the packer and ran it back into the hole. Put in 500gal of acid. Unseat the packer and put in 1000gal of fresh water and inhibitor, reset the packer at the same depth and pressure up on the annulus to 1000psi and held for 15 min. test. Lost 10 psi for a final pressure of 990 psi. Past test.
 
Pulled the tubing and packer. Cleaned the drill mud from the well. Put a 40,000lb shear ring on the packer and ran it back into the hole. Put in 500gal of acid. Unseat the packer and put in 1000gal of fresh water and inhibitor, reset the packer at the same depth and pressure up on the annulus to 1000psi and held for 15 min. test. Lost 10 psi for a final pressure of 990 psi. Past test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1311187720
 
| 1311187720
 
| 2011-06-16
 
| 2011-06-16
|
+
|  
 
| An inspection conducted with Will Ziegler revealed that the Pre-liminary Restoration meets ORC 1509.072.  No violations were noted.
 
| An inspection conducted with Will Ziegler revealed that the Pre-liminary Restoration meets ORC 1509.072.  No violations were noted.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1351777087
 
| 1351777087
 
| 2012-10-29
 
| 2012-10-29
|
+
|  
| At the time of my inspection the pressure on the annular space between the 5.5" casing and the 2 3/8" tubing was pressured up to 140 psi. In five minutes the pressure was at 138 and at 15 minutes it was at 136 psi. This represents a 2.8% loss over 15 minutes. The annulus was pressured to 250 psi at 8 am and my test was done at noon on the same day. The drop from 250 psi to 140 psi over a four hour period represents a 3% loss. The operator of the well believes that the 5.5" longstring casing was not connected tightly and the annulus is losing pressure to formations behind the casing that are not cemented. At the time of my inspection the well was shut in due to a leak in the flow line from the pump to the well but during normal operation pressures in the tubing exceed 800 psi with no sign of lost pressure into the annulus.
+
| At the time of my inspection the pressure on the annular space between the 5.5 casing and the 2 3/8 tubing was pressured up to 140 psi. In five minutes the pressure was at 138 and at 15 minutes it was at 136 psi. This represents a 2.8% loss over 15 minutes. The annulus was pressured to 250 psi at 8 am and my test was done at noon on the same day. The drop from 250 psi to 140 psi over a four hour period represents a 3% loss. The operator of the well believes that the 5.5 longstring casing was not connected tightly and the annulus is losing pressure to formations behind the casing that are not cemented. At the time of my inspection the well was shut in due to a leak in the flow line from the pump to the well but during normal operation pressures in the tubing exceed 800 psi with no sign of lost pressure into the annulus.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1366893871
 
| 1366893871
 
| 2013-04-04
 
| 2013-04-04
|
+
|  
 
| At the time of the inspection the well had been bailed down to 575', 125' below the surface casing, and filled from the surface with approximately 5 yards of 9 sack grout from St. Henry Tile Co.
 
| At the time of the inspection the well had been bailed down to 575', 125' below the surface casing, and filled from the surface with approximately 5 yards of 9 sack grout from St. Henry Tile Co.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1424138826
 
| 1424138826
 
| 2013-03-22
 
| 2013-03-22
|
+
|  
 
| At the time of the inspection a bottom plug was set in the well from 2900' to 2515' with 45 sacks of 50/50 pozmix from PetroSet Cementing Services.
 
| At the time of the inspection a bottom plug was set in the well from 2900' to 2515' with 45 sacks of 50/50 pozmix from PetroSet Cementing Services.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1504942545
 
| 1504942545
 
| 2011-06-16
 
| 2011-06-16
|
+
|  
 
| I inspected the well location with Brent Bear.  See Bear's report for details.
 
| I inspected the well location with Brent Bear.  See Bear's report for details.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 164653730
 
| 164653730
 
| 2010-09-30
 
| 2010-09-30
|
+
|  
 
| Check well and storage.
 
| Check well and storage.
 
Id posted by the well head.
 
Id posted by the well head.
 
Preliminary restoration not done, top soil still stock piled around the site.
 
Preliminary restoration not done, top soil still stock piled around the site.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1738332536
 +
| 2013-01-30
 +
|
 +
| At the time of my inspection the well was being used to inject fluids collected during the release associated with Complaint #4186. Mark Amell of Amell Inc. was hired to oversee the plugging of the well for Innex Oil and Gas Inc. as soon as the remaining fluids have been injected.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1808706409
 +
| 2012-04-30
 +
|
 +
| Inspect Well.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1825346400
 +
| 2012-09-11
 +
|
 +
| At the time of my inspection, Preliminary Restoration was passed.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1848265083
 
| 1848265083
 
| 2012-09-11
 
| 2012-09-11
|
+
|  
 
| At the time of my inspection both the annular space and the tubing were on a vacuum. I contacted the operator who indicated the well is shut in due to a leak in the line from the pump to the well. The operator will set up a time to test and service the well and will contact the necessary inspectors prior to doing so.
 
| At the time of my inspection both the annular space and the tubing were on a vacuum. I contacted the operator who indicated the well is shut in due to a leak in the line from the pump to the well. The operator will set up a time to test and service the well and will contact the necessary inspectors prior to doing so.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2037892039
 
| 2037892039
 
| 2013-04-03
 
| 2013-04-03
|
+
|  
| At the time of the inspection a  plug was set across the Trenton from 1300' to 900' with 80 sacks of 50/50 pozmix from PetroSet Cementing Services. The cement was pumped through 1.5" tubing and no circulation was observed. The cement will be tagged with the bailer after 24 hours to determine the top of the plug.
+
| At the time of the inspection a  plug was set across the Trenton from 1300' to 900' with 80 sacks of 50/50 pozmix from PetroSet Cementing Services. The cement was pumped through 1.5 tubing and no circulation was observed. The cement will be tagged with the bailer after 24 hours to determine the top of the plug.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 293824688
 
| 293824688
 
| 2011-11-21
 
| 2011-11-21
|
+
|  
 
| Inspect well. Well shut in. Tanks have rust holes. Replacement fiberglass tanks on order. No ID at Tanks. Advised operator that well will need to be tested once a month and data recorded, because pressure leaks off within several days.
 
| Inspect well. Well shut in. Tanks have rust holes. Replacement fiberglass tanks on order. No ID at Tanks. Advised operator that well will need to be tested once a month and data recorded, because pressure leaks off within several days.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 312890608
 
| 312890608
 
| 2013-04-01
 
| 2013-04-01
|
+
|  
| At the time of the inspection Jet Wire Line Services were on site for a cement bond log on the 5.5" casing. The top of the cement from the bottom plug set on 3-22-13 was tagged at 2513'. The bond log showed good cement behind the casing at 2290' and some partial cement up to 2200'. The casing was then shot by Jet Wire Line at 2127' and removed from the well.
+
| At the time of the inspection Jet Wire Line Services were on site for a cement bond log on the 5.5 casing. The top of the cement from the bottom plug set on 3-22-13 was tagged at 2513'. The bond log showed good cement behind the casing at 2290' and some partial cement up to 2200'. The casing was then shot by Jet Wire Line at 2127' and removed from the well.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 395588498
 
| 395588498
 
| 2013-05-21
 
| 2013-05-21
|
+
|  
 
| At the time of the inspection all plugging operation were completed and all equipment had been removed from the location. The location is in a farm field and was graded by the plugging contractor. The location was tilled and planted by the landowner. Final Restoration Passed.
 
| At the time of the inspection all plugging operation were completed and all equipment had been removed from the location. The location is in a farm field and was graded by the plugging contractor. The location was tilled and planted by the landowner. Final Restoration Passed.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 477928497
 
| 477928497
 
| 2013-01-17
 
| 2013-01-17
|
+
|  
 
| At the time of my inspection the well was being used to inject the water recovered from the release on 1-12-2013. Detailed records of all fluids injected are to be kept by Allied Environmental and Innex Oil and Gas Inc.
 
| At the time of my inspection the well was being used to inject the water recovered from the release on 1-12-2013. Detailed records of all fluids injected are to be kept by Allied Environmental and Innex Oil and Gas Inc.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 13:52, 15 July 2015

Well Details

Well ID: 34-011-20103
Loading map...
County: Auglaize
Municipality:
Operator Name: INNEX OIL AND GAS INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2010-02-23
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.54198233
Longitude: -84.36091864

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1269056497 2012-03-08 Inspect Well. Injector rate of 60 bbl/day.
1273849339 2010-05-14 On site to witness Mechanical Integrity Test.

Pulled the tubing and packer. Cleaned the drill mud from the well. Put a 40,000lb shear ring on the packer and ran it back into the hole. Put in 500gal of acid. Unseat the packer and put in 1000gal of fresh water and inhibitor, reset the packer at the same depth and pressure up on the annulus to 1000psi and held for 15 min. test. Lost 10 psi for a final pressure of 990 psi. Past test.

1311187720 2011-06-16 An inspection conducted with Will Ziegler revealed that the Pre-liminary Restoration meets ORC 1509.072. No violations were noted.
1351777087 2012-10-29 At the time of my inspection the pressure on the annular space between the 5.5 casing and the 2 3/8 tubing was pressured up to 140 psi. In five minutes the pressure was at 138 and at 15 minutes it was at 136 psi. This represents a 2.8% loss over 15 minutes. The annulus was pressured to 250 psi at 8 am and my test was done at noon on the same day. The drop from 250 psi to 140 psi over a four hour period represents a 3% loss. The operator of the well believes that the 5.5 longstring casing was not connected tightly and the annulus is losing pressure to formations behind the casing that are not cemented. At the time of my inspection the well was shut in due to a leak in the flow line from the pump to the well but during normal operation pressures in the tubing exceed 800 psi with no sign of lost pressure into the annulus.
1366893871 2013-04-04 At the time of the inspection the well had been bailed down to 575', 125' below the surface casing, and filled from the surface with approximately 5 yards of 9 sack grout from St. Henry Tile Co.
1424138826 2013-03-22 At the time of the inspection a bottom plug was set in the well from 2900' to 2515' with 45 sacks of 50/50 pozmix from PetroSet Cementing Services.
1504942545 2011-06-16 I inspected the well location with Brent Bear. See Bear's report for details.
164653730 2010-09-30 Check well and storage.

Id posted by the well head. Preliminary restoration not done, top soil still stock piled around the site.

-1738332536 2013-01-30 At the time of my inspection the well was being used to inject fluids collected during the release associated with Complaint #4186. Mark Amell of Amell Inc. was hired to oversee the plugging of the well for Innex Oil and Gas Inc. as soon as the remaining fluids have been injected.
-1808706409 2012-04-30 Inspect Well.
-1825346400 2012-09-11 At the time of my inspection, Preliminary Restoration was passed.
1848265083 2012-09-11 At the time of my inspection both the annular space and the tubing were on a vacuum. I contacted the operator who indicated the well is shut in due to a leak in the line from the pump to the well. The operator will set up a time to test and service the well and will contact the necessary inspectors prior to doing so.
2037892039 2013-04-03 At the time of the inspection a plug was set across the Trenton from 1300' to 900' with 80 sacks of 50/50 pozmix from PetroSet Cementing Services. The cement was pumped through 1.5 tubing and no circulation was observed. The cement will be tagged with the bailer after 24 hours to determine the top of the plug.
293824688 2011-11-21 Inspect well. Well shut in. Tanks have rust holes. Replacement fiberglass tanks on order. No ID at Tanks. Advised operator that well will need to be tested once a month and data recorded, because pressure leaks off within several days.
312890608 2013-04-01 At the time of the inspection Jet Wire Line Services were on site for a cement bond log on the 5.5 casing. The top of the cement from the bottom plug set on 3-22-13 was tagged at 2513'. The bond log showed good cement behind the casing at 2290' and some partial cement up to 2200'. The casing was then shot by Jet Wire Line at 2127' and removed from the well.
395588498 2013-05-21 At the time of the inspection all plugging operation were completed and all equipment had been removed from the location. The location is in a farm field and was graded by the plugging contractor. The location was tilled and planted by the landowner. Final Restoration Passed.
477928497 2013-01-17 At the time of my inspection the well was being used to inject the water recovered from the release on 1-12-2013. Detailed records of all fluids injected are to be kept by Allied Environmental and Innex Oil and Gas Inc.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.