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Difference between revisions of "37-033-26872"

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| INJECTION DISPOSAL WELL
 
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| PANDER #1 (SWIW #15)
 
| PANDER #1 (SWIW #15)
 
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| PAROBEK #2 (SWIW #12)
 
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| SALTY'S DISPOSAL - MEYERS #2 (SWIW #33)
 
| SALTY'S DISPOSAL - MEYERS #2 (SWIW #33)
 
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| SALTYS DISPOSAL - GROSELLE INECTION WELL # 2
 
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| WOLF #1 DISP WELL (PANDER RAY TRUCKING INC)
 
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| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
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| WARREN DRILLING CO #1 (SWIW #6) HUNTER DISPOSAL
 
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| PANDER #1 (SWIW #15)
 
| PANDER #1 (SWIW #15)
 
| NEWTON FALLS
 
| NEWTON FALLS

Revision as of 15:09, 23 June 2014

Well Details

Well ID: 37-033-26872
Loading map...
County: Clearfield
Municipality: Lawrence Township
Operator Name: EOG RESOURCES INC
Well Pad ID: 149105
Farm/Lease Name: PUNXSUTAWNEY HUNTING CLUB 36H
First Permit Date: 2009-10-14
Last Permit Date: 2009-10-14
Spud Date: 2010-01-06
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: 7
Latitude: 41.16264
Longitude: -78.453222

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1858089 2010-01-22 No Violations Noted Conductor is set and is covered with a steel plate covering the cellar.

Met with Chuck Peterman on site. A Dallas Morris rig will be brought in on Monday to start the top hole drilling. Site ID Sign and E/S Plan are on location.

1863772 2010-02-18 No Violations Noted Precision Drilling Rig #823 is currently tripping out and will be drilling a 7 7/8" hole through the curve and lateral.

Well pad is in good condition with no visable spills

1867626 2010-03-03 No Violations Noted Met On site with Company Representative Duane Winkler.

Precision Drilling Rig #823 has reached TD at 12,660' and is currently circulating

1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589126
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589126
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589126
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589127
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589127
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589127
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589129
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589129
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589129
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589130
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589130
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589130
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589131
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589131
1890291 2010-06-04 Violation(s) Noted PHC 36H 37-033-26872 - Failure of blow out prevention equipment, uncontrolled discharge of natural gas and flowback fluids, well vented for approx 18 hours before it was shut in. 589131
1892770 2010-06-04 Violation(s) Noted Operator had a blowout and lost control of the well at approx 10:00pm on June 3, 2010. Well control was regained at 12:13pm on June 4, 2010. 589901
1892770 2010-06-04 Violation(s) Noted Operator had a blowout and lost control of the well at approx 10:00pm on June 3, 2010. Well control was regained at 12:13pm on June 4, 2010. 589901
1892770 2010-06-04 Violation(s) Noted Operator had a blowout and lost control of the well at approx 10:00pm on June 3, 2010. Well control was regained at 12:13pm on June 4, 2010. 589901
1892770 2010-06-04 Violation(s) Noted Operator had a blowout and lost control of the well at approx 10:00pm on June 3, 2010. Well control was regained at 12:13pm on June 4, 2010. 589902
1892770 2010-06-04 Violation(s) Noted Operator had a blowout and lost control of the well at approx 10:00pm on June 3, 2010. Well control was regained at 12:13pm on June 4, 2010. 589902
1892770 2010-06-04 Violation(s) Noted Operator had a blowout and lost control of the well at approx 10:00pm on June 3, 2010. Well control was regained at 12:13pm on June 4, 2010. 589902
1892792 2010-06-06 No Violations Noted EOG is conducting clean up operations.
1892795 2010-06-07 No Violations Noted EOG still conducting clean up. Wet with OGI Supervisors Bruce Jankura and Doug Welsh, and BOGM Director Scott Perry
1921832 2010-10-21 No Violations Noted
1954471 2011-03-02 No Violations Noted

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 151947.0 184.0 0.0 0.0 0.0 0.0
2012-1 241357.0 182.0 0.0 0.0 0.0 0.0
2011-2 260814.0 184.0 0.0 0.0 0.0 0.0
2011-1 316552.0 181.0 0.0 0.0 0.0 0.0
2010-2 69177.0 33.0 0.0 0.0 0.0 0.0
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2009-0 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-2 PRODUCED FLUID 59.0 Bbl INJECTION DISPOSAL WELL 34-151-23420 B & B WELL # 2 (BELDEN & BLAKE) HARTVILLE OH
2012-2 PRODUCED FLUID 93.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 525-1 BLAZEK PUMP AND WELL HIRAM OH
2012-2 PRODUCED FLUID 385.0 Bbl INJECTION DISPOSAL WELL 34-155-21438 KLEESE #1 (SWIW #18) - KLEESE DEVELOPMENT ASSOCS VIENNA OH
2012-2 PRODUCED FLUID 191.0 Bbl INJECTION DISPOSAL WELL 34-155-21447 KLEESE #2 (SWIW #19) - KLEESE DEVELOPMENT ASSOCS VIENNA OH
2012-2 PRODUCED FLUID 534.0 Bbl INJECTION DISPOSAL WELL 34-155-23584 KOONTZ #1 DISPOSAL WELL WARREN OH
2012-2 PRODUCED FLUID 415.0 Bbl INJECTION DISPOSAL WELL 34-155-23795 PANDER #1 (SWIW #15) NEWTON FALLS OH
2012-2 PRODUCED FLUID 315.0 Bbl INJECTION DISPOSAL WELL 34-007-22038 PAROBEK #2 (SWIW #12) OH
2012-2 PRODUCED FLUID 321.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-2 PRODUCED FLUID 105.0 Bbl INJECTION DISPOSAL WELL 34-133-24189 SALTY'S DISPOSAL - MEYERS #2 (SWIW #33) ATWATER OH
2012-2 PRODUCED FLUID 182.26 Bbl INJECTION DISPOSAL WELL 34-133-20114 SALTY'S DISPOSAL - WILCOX #1 ROOTSTOWN OH
2012-2 PRODUCED FLUID 205.0 Bbl INJECTION DISPOSAL WELL 34-133-24096 SALTYS DISPOSAL - GROSELLE INECTION WELL # 2 GARRETTSVILLE OH
2012-2 PRODUCED FLUID 1441.0 Bbl STORAGE PENDING DISPOSAL OR REUSE STORAGE PENDING DISPOSAL OR REUSE PA
2012-2 PRODUCED FLUID 211.0 Bbl INJECTION DISPOSAL WELL 34-155-21893 WOLF #1 DISP WELL (PANDER RAY TRUCKING INC) NEWTON FALLS OH
2010-2 PRODUCED FLUID 654.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508 PA BRINE TRT INC - FRANKLIN PLT - VENANGO CO FRANKLIN PA
2010-2 PRODUCED FLUID 2798.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR DRILLING OR PLUGGING PA
2010-2 PRODUCED FLUID 502.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0023213 RIDGWAY BOROUGH SEWAGE TREATMENT PLANT RIDGWAY PA
2011-1 PRODUCED FLUID 992.0 Bbl INJECTION DISPOSAL WELL 34-133-24096 GROSELLE #2 - SALTYS DISPOSAL WELLS LP GARRETTSVILLE OH
2011-1 PRODUCED FLUID 1564.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 34-099-23127 NORTH STAR BRINE DISPOSAL YOUNGSTOWN OH
2011-1 PRODUCED FLUID 5811.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508 PA BRINE TRT INC - FRANKLIN PLT - VENANGO CO FRANKLIN PA
2011-1 PRODUCED FLUID 1025.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY JOSEPHINE PA
2011-1 PRODUCED FLUID 7705.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE OF BRINE TO FRAC A WELL
2011-1 PRODUCED FLUID 135.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0023213 RIDGWAY BOROUGH SEWAGE TREATMENT PLANT RIDGWAY PA
2011-1 DRILL CUTTINGS 65.35 Tons LANDFILL 101397 VIOLIA ES GREENTREE LANDFILL PA
2011-1 PRODUCED FLUID 195.0 Bbl INJECTION DISPOSAL WELL 34-121-23995 WARREN DRILLING CO #1 (SWIW #6) HUNTER DISPOSAL DEXTER CITY OH
2011-1 PRODUCED FLUID 190.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0027057 WILLIAMSPORT SAN AUTH - CENTRAL STP WILLIAMSPORT PA
2011-2 PRODUCED FLUID 2543.0 Bbl INJECTION DISPOSAL WELL 34-133-24096 GROSELLE #2 - SALTYS DISPOSAL WELLS LP GARRETTSVILLE OH
2011-2 PRODUCED FLUID 4707.0 Bbl INJECTION DISPOSAL WELL 34-049-23127 NORTH STAR YOUNGSTOWN OH
2011-2 PRODUCED FLUID 2250.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE OF BRINE TO FRAC A WELL
2012-1 PRODUCED FLUID 126.0 Bbl INJECTION DISPOSAL WELL 34-099-23127 NORTH STAR BRINE DISPOSAL YOUNGSTOWN OH
2012-1 PRODUCED FLUID 780.0 Bbl INJECTION DISPOSAL WELL 34-155-23795 PANDER #1 (SWIW #15) NEWTON FALLS OH
2012-1 PRODUCED FLUID 6267.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING

References