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== Well Details == | == Well Details == | ||
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== Inspection Data == | == Inspection Data == | ||
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Well ID: 37-117-21556 | Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. To navigate, press the arrow keys. |
County: Tioga | |
Municipality: Liberty Township | |
Operator Name: SWEPI LP | |
Well Pad ID: 148866 | |
Farm/Lease Name: MCNETT F 708 6H | |
First Permit Date: 2012-07-02 | |
Last Permit Date: 2012-07-02 | |
Spud Date: 2012-07-07 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: 2 | |
Latitude: 41.57633 | |
Longitude: -77.031022 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2113414 | 2012-10-24 | Viol(s) Noted & Immediately Corrected | washing on liner with holes VIOIC | 653072 |
2113414 | 2012-10-24 | Viol(s) Noted & Immediately Corrected | washing on liner with holes VIOIC | 653073 |
2119323 | 2012-11-29 | No Violations Noted | fracking 2H, 4H, 6H | |
2123739 | 2012-12-13 | No Violations Noted | ||
2134438 | 2013-01-24 | Violation(s) Noted | Violations cited to the 6H well for a brine/flowback spill to the rock-lined ditch on the site. | 659311 |
2134438 | 2013-01-24 | Violation(s) Noted | Violations cited to the 6H well for a brine/flowback spill to the rock-lined ditch on the site. | 659312 |
2134438 | 2013-01-24 | Violation(s) Noted | Violations cited to the 6H well for a brine/flowback spill to the rock-lined ditch on the site. | 659313 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | SPENT LUBRICANT | 1.5 | Bbl | CENTRALIZD TREATMENT/DISCHARGE(>500MG/L) | PAD987266749 | ENVIRONMENTAL RECOVERY CORPORATION OF PA (ERC) | LANCASTER | PA |
2012-2 | DRILLING FLUID WASTE | 72.49 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR0123 | HYDRO RECOVERY - BLOSSBURG | BLOSSBURG | PA |
2012-2 | FRACING FLUID WASTE | 487.2 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR0123 | HYDRO RECOVERY - BLOSSBURG | BLOSSBURG | PA |
2012-2 | DRILL CUTTINGS | 2929.19 | Tons | LANDFILL | 743884 | PHOENIX RESOURCES LANDFILL | WELLSBORO | PA |
2012-2 | FRACING FLUID WASTE | 311.31 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING |