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Difference between revisions of "34-175-20344"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-175-20344
 
| Well ID: 34-175-20344
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.9731798636, -83.1841155717 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.97303403, -83.18435178 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Wyandot County, Ohio|Wyandot]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[NORSTAR OPERATING LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2005-04-01
 
| Spud Date: 2005-04-01
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 40.9731798636
+
| Latitude: 40.97303403
 
|-
 
|-
| Longitude: -83.1841155717
+
| Longitude: -83.18435178
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -692258637
 
| 2005-04-07
 
|
 
| Attempt to set bottom plug.  A 330 foot plug was attempted to be set from 2358 to 2028  with 88 sacks cement in a 7 inch hole using 2 inch upset tubing. During the cementing process the cement setup and locked tubing in place Free point was calculated by stretch of 40K lb with 25" of stretch at 2027 feet. Upon determination of cemented in pipe circulation of upwards of 145 bbl water to wash out cement plug. Circulation of water was maintained throughout.  Suspect channeling occurred. Reverse circulation was attempted to free pipe. Pipe would need to be shot.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1543376881
 
| 1543376881
 
| 2005-04-18
 
| 2005-04-18
|
+
|  
 
| Inspect location. Pits filled site graded. Crop field.
 
| Inspect location. Pits filled site graded. Crop field.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1587742088
 
| 1587742088
 
| 2005-03-31
 
| 2005-03-31
|
+
|  
 
| Inspect Site. Drilling, conductor set at 174 feet.
 
| Inspect Site. Drilling, conductor set at 174 feet.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1953007992
 
| 1953007992
 
| 2005-04-08
 
| 2005-04-08
|
+
|  
 
| Plug well. Shoot pipe at second collar above calculated free point of 2037. First collar at 2037, second collar shot off at 1994. Pull up 2 to 3 feet and set 100foot plug, and subsequent plugs for closing well.
 
| Plug well. Shoot pipe at second collar above calculated free point of 2037. First collar at 2037, second collar shot off at 1994. Pull up 2 to 3 feet and set 100foot plug, and subsequent plugs for closing well.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 422939706
 
| 422939706
 
| 2005-04-01
 
| 2005-04-01
|
+
|  
 
| Set surface casing at 706 foot.
 
| Set surface casing at 706 foot.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -692258637
 +
| 2005-04-07
 +
|
 +
| Attempt to set bottom plug.  A 330 foot plug was attempted to be set from 2358 to 2028  with 88 sacks cement in a 7 inch hole using 2 inch upset tubing. During the cementing process the cement setup and locked tubing in place Free point was calculated by stretch of 40K lb with 25 of stretch at 2027 feet. Upon determination of cemented in pipe circulation of upwards of 145 bbl water to wash out cement plug. Circulation of water was maintained throughout.  Suspect channeling occurred. Reverse circulation was attempted to free pipe. Pipe would need to be shot.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 05:14, 16 July 2015

Well Details

Well ID: 34-175-20344
Loading map...
County: Wyandot
Municipality:
Operator Name: NORSTAR OPERATING LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2005-04-01
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.97303403
Longitude: -83.18435178

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1543376881 2005-04-18 Inspect location. Pits filled site graded. Crop field.
1587742088 2005-03-31 Inspect Site. Drilling, conductor set at 174 feet.
1953007992 2005-04-08 Plug well. Shoot pipe at second collar above calculated free point of 2037. First collar at 2037, second collar shot off at 1994. Pull up 2 to 3 feet and set 100foot plug, and subsequent plugs for closing well.
422939706 2005-04-01 Set surface casing at 706 foot.
-692258637 2005-04-07 Attempt to set bottom plug. A 330 foot plug was attempted to be set from 2358 to 2028 with 88 sacks cement in a 7 inch hole using 2 inch upset tubing. During the cementing process the cement setup and locked tubing in place Free point was calculated by stretch of 40K lb with 25 of stretch at 2027 feet. Upon determination of cemented in pipe circulation of upwards of 145 bbl water to wash out cement plug. Circulation of water was maintained throughout. Suspect channeling occurred. Reverse circulation was attempted to free pipe. Pipe would need to be shot.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.