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− | == | + | == Inspection Data == |
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | INSPECTION ID | !scope="col" | INSPECTION ID |
Well ID: 42-051-24505 | Loading map...
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County: Fayette | |
Municipality: Jefferson Township | |
Operator Name: CHEVRON APPALACHIA LLC | |
Farm/Lease Name: LESTER UNIT 5H | |
First Permit Date: 2012-04-11 | |
Last Permit Date: 2012-04-11 | |
Spud Date: 2012-04-28 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: None | |
Latitude: 40.065563 | |
Longitude: -79.824775 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2079807 | 2012-06-19 | No Violations Noted | HORIZONTAL MARCELLUS, KEANE # 2144 DRILLING ON AIR @ 670' (TD). RUNNING WATER PROTECTION CASING AND CEMENTING TONIGHT. | |
2079808 | 2012-06-18 | No Violations Noted | HORIZONTAL MARCELLUS, KEANE # 2144 DRILLING ON AIR @ 253' (TD). RUNNING COAL PROTECTION CASING AND CEMENTING TONIGHT. SET BASKET @ 164'. | |
2090006 | 2012-06-21 | No Violations Noted | HORIZONTAL MARCELLUS, KEANE # 2144 DRILLING ON AIR @ 2380' (TD). RUNNING INTERMEDIATE CASING AND CEMENTING TONIGHT. | |
2090007 | 2012-07-02 | No Violations Noted | HORIZONTAL MARCELLUS, KEANE # 2144 DRILLING ON AIR @ 6800' (TD). RUNNING BRIDGE PLUG AND LOADING HOLE WITH OIL BASE MUD.CAPPING AND MOVING TO NEXT WELL. | |
2092030 | 2012-08-15 | No Violations Noted | 5 verticals and no horizontals drilled. Crew cleaning frac tank. | |
2113721 | 2012-09-28 | No Violations Noted | HORIZONTAL MARCELLUS, PATTERSON # 339 MOVING ON TO LESTER 5 - H (9/26/2012). DRILLING ON FLUID @ 8589'. | |
2113724 | 2012-10-04 | No Violations Noted | HORIZONTAL MARCELLUS, PATTERSON # 339 DRILLING ON FLUID @ 9087' TODAY. | |
2113742 | 2012-10-10 | No Violations Noted | HORIZONTAL MARCELLUS, PATTERSON # 339 DRILLING ON FLUID @ 13,431' (TD). RUNNIG 51/2" CASING AND CEMENTING TONIGHT.DURING CEMENTING PROCEDURES OF PROD. CASING (I/R OF CEMENT TO SURFASE TO SOON).THEY FLUSH CEMENT OUT OF HOLE WITH WATER THAN OIL BASE MUD AT THIS TIME.CHEVRON EXSPECTED PROD. CASING HAS SEPERATED .STARTED PULLING PROD. CASING AND FINDING OUT PROD. CASING SEPERATED @ 5051' DOWN HOLE. LEAVING 8000' OF 51/2"CASING IN WELL BORE. CHEVRON GOING TO RETRIEVE PIPE WITH A SPEAR. | |
2113746 | 2012-10-17 | No Violations Noted | HORIZONTAL MARCELLUS, PATTERSON # 339 FISHING OUT LAST 20 - JOINTS OF PROD. CASING TODAY. GOING IN TO MAKE SURE NO CENTRALIZERS LEFT IN WELL BORE. RUNNING NEW PROD. CASING AS SOON AS WELL BORE IS CLEAN. | |
2113749 | 2012-10-22 | No Violations Noted | HORIZONTAL MARCELLUS, PATTERSON # 339 DRILLING ON FLUID @ 13,341' (TD). RUNNING 51/2" PROD. CASING AND CEMENTING TONIGHT (10/20/2012). | |
2121521 | 2012-12-06 | No Violations Noted | E&S, PPC, Permits in box, site ID sign up. Some erosion issues at back of water impoundment being addressed by operator. Will monitor further. | |
2137229 | 2013-02-06 | No Violations Noted | Site ID sign up, Plans and permits in box, Site stable. Impoundment reaching 2 foot freeboard, operator told and will pump level down. |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | DRILLING FLUID WASTE | 645.4 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0253723 | APPALACHIAN WATER SERVICES LLC (RONCO WTP) | MASONTOWN | PA |
2012-2 | DRILLING FLUID WASTE | 100.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR DRILLING OR PLUGGING | PA | ||
2012-2 | FRACING FLUID WASTE | 1418.2 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR DRILLING OR PLUGGING | PA | ||
2012-1 | DRILLING FLUID WASTE | 350.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0253723 | APPALACHIAN WATER SERVICES LLC (RONCO WTP) | MASONTOWN | PA |