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− | == | + | == Inspection Data == |
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | INSPECTION ID | !scope="col" | INSPECTION ID |
Well ID: 42-015-21980 | Loading map...
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County: Bradford | |
Municipality: Albany Township | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Farm/Lease Name: FITZSIMMONS BRA 3H | |
First Permit Date: 2011-10-13 | |
Last Permit Date: 2011-10-13 | |
Spud Date: 2011-10-20 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: None | |
Latitude: 41.639552 | |
Longitude: -76.3952 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2017331 | 2011-11-07 | No Violations Noted | NOMAC 31, Comp. Man - Gene Belsom , Drilling @ 1149'
Wet hole , had to set 28" to seal off water, no water after 40', drilled to 85' and set 20" cond. Pulled 28" pipe then cemented. 0 - 20' clay, water 20 - 50' boulders, clay 50 - 85' clay, dry 20" @ 85' on 10/22/11 w/ 44.13 bbls of 15.6 cement 13 3/8" @ 511' w/ 500 sx Cl A, 15.6 ppg, 30 bbls back to surf of 15.5 ppg cement BOP test - 11/6/11 good |
|
2021540 | 2011-11-22 | No Violations Noted | NOMAC 31, Comp Man - Dean Cook
checked drillers log - good, @10,330', need to put BOP fcn tests in back. 1600-1750' 150 units gas 1750-1996' 130 u 3310' 667 u 5550-6240' 280 u 9 5/8" @ 1996' w/ 850 sx prem. cement, 15.6 ppg, 40 bbls back to surf, 15.5 ppg Discussed need to clean up spilled chemicals ( on containment) |
|
2064912 | 2012-04-25 | No Violations Noted | 4 wells on site. All are producing. On the 3H, one valve is leaking, dripping, accumulation of white substance ( salt?) in area. Small silver tubing(methanol inj line) , bubbling where it comes out of the ground. photo
2771.4 o n prod, 1.75 and 58.266 psi on other guages. Talked to Jake Swanson ( Ches. rep.) - someone was sent out to look at the well. |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 1083175.0 | 183.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 529852.0 | 90.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | PRODUCED FLUID | 1243.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2011-2 | DRILLING FLUID WASTE | 6129.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE OF BRINE TO FRAC A WELL | |||
2012-1 | PRODUCED FLUID | 2254.64 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING |