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Difference between revisions of "34-147-20392"

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__TOC__
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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-147-20392
 
| Well ID: 34-147-20392
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.22443295, -83.42014672 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.224379890, -83.42022042 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Seneca County, Ohio|Seneca]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Seneca_County,_Ohio|Seneca]]
 +
|-
 +
| Municipality: [[Jackson_Township,_Seneca_County,_Ohio|Jackson Township]]
 
|-
 
|-
 
| Operator Name: [[BOCKBRADER LEROY]]
 
| Operator Name: [[BOCKBRADER LEROY]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: BROCKBRADER
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2003-07-24
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.224379890
 +
|-
 +
| Longitude: -83.42022042
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| APP
 +
| 2001-12-04
 +
| Proposed Formations:TRENTON, Issued Date:12/4/2001, Expired Date:12/4/2002 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Latitude: 41.22443295
+
| Construction Permit Expires
 +
| 2002-12-04
 +
| RBDMS Rec
 
|-
 
|-
| Longitude: -83.42014672
+
| Plugged by Orphan Well Program
 +
| 2003-02-24
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2003-02-24
 +
| RBDMS Rec
 +
|-
 +
| Record Last Modified
 +
| 2013-03-14
 +
| RBDMS Rec
 
|-
 
|-
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Job Number
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Job Start Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Job End Date
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| True Vertical Depth (ft)
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Total Water Volume (gal)
!scope="col" | VIOLATION CODE
+
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
!scope="col" | VIOLATION COMMENT
+
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
| 1046115991
+
|}-->
| 2003-02-24
+
<!--== Stimulations Data ==
|  
+
{| class="wikitable sortable" width="95%"
| Frantz drilling plug well with cement. Six inch casing previously pulled. Ream out eight inch casing to total depth of 1250.  Steel plug previously set at 300 feet was reamed out.
+
!scope="col" style="text-align: center"| Stimulation Date
|  
+
!scope="col" style="text-align: center"| Chemical Agent
|  
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
|  
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1265420181
+
|}-->
| 2003-02-24
+
<!--== Waste Data ==
|  
+
{| class="wikitable sortable"
| Plug well. See plug report.
+
!scope="col" style="text-align: center"| Period
|  
+
!scope="col" style="text-align: center"| Operator Name
|  
+
!scope="col" style="text-align: center"| Waste Type
|  
+
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
|}-->
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| 262396111
+
| 0262396111
 
| 2003-02-20
 
| 2003-02-20
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Inspect Idle & orphan drilling project. Drilled to total depth of 1250 feet. Six inch casing had previously been pulled.
 
| Inspect Idle & orphan drilling project. Drilled to total depth of 1250 feet. Six inch casing had previously been pulled.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0622415253
| -622415253
 
 
| 2003-07-24
 
| 2003-07-24
|  
+
| Final Restoration
 +
| No Violations
 
| inspect site. Final restoration. Crop field.
 
| inspect site. Final restoration. Crop field.
|  
+
|-
|  
+
| 1046115991
|  
+
| 2003-02-24
 +
| Plug / Plug Back
 +
| No Violations
 +
| Frantz drilling plug well with cement. Six inch casing previously pulled. Ream out eight inch casing to total depth of 1250.  Steel plug previously set at 300 feet was reamed out.
 +
|-
 +
| 1265420181
 +
| 2003-02-24
 +
| Plug / Plug Back
 +
| No Violations
 +
| Plug well. See plug report.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 14:09, 23 July 2019

Well Details

Well ID: 34-147-20392
Loading map...
Country: United States
State: Ohio
County: Seneca
Municipality: Jackson Township
Operator Name: BOCKBRADER LEROY
Well Pad ID:
Farm/Lease Name: BROCKBRADER
License Status: Final Restoration
License Date: 2003-07-24
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.224379890
Longitude: -83.42022042

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2001-12-04 Proposed Formations:TRENTON, Issued Date:12/4/2001, Expired Date:12/4/2002 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2002-12-04 RBDMS Rec
Plugged by Orphan Well Program 2003-02-24 Plugged by Orphan Well Program
Plugged/Abandoned 2003-02-24 RBDMS Rec
Record Last Modified 2013-03-14 RBDMS Rec

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0262396111 2003-02-20 Plug / Plug Back No Violations Inspect Idle & orphan drilling project. Drilled to total depth of 1250 feet. Six inch casing had previously been pulled.
0622415253 2003-07-24 Final Restoration No Violations inspect site. Final restoration. Crop field.
1046115991 2003-02-24 Plug / Plug Back No Violations Frantz drilling plug well with cement. Six inch casing previously pulled. Ream out eight inch casing to total depth of 1250. Steel plug previously set at 300 feet was reamed out.
1265420181 2003-02-24 Plug / Plug Back No Violations Plug well. See plug report.

For data sources see[3]

References