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Difference between revisions of "34-171-20065"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-171-20065
 
| Well ID: 34-171-20065
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.44256912, -84.5666088 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.442312186, -84.56670826 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Williams County, Ohio|Williams]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[HILL DAVID R INC]]
+
| County: [[Williams_County,_Ohio|Williams]]
 +
|-
 +
| Municipality: [[Pulaski_Township,_Williams_County,_Ohio|Pulaski Township]]
 +
|-
 +
| Operator Name: [[DAVID R HILL INC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: W MUSSER
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2018-07-24
 
|-
 
|-
 
| Spud Date: 2009-04-23
 
| Spud Date: 2009-04-23
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[KILBARGER DRLG]]
 +
|-
 +
| Final Drill Date: 2009-05-03
 +
|-
 +
| Well Total Depth: 2739 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Plugged and Abandoned
+
| Latitude: 41.442312186
 +
|-
 +
| Longitude: -84.56670826
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| APP
 +
| 2009-02-23
 +
| Proposed Formations:TRENTON THRU PRAIRIE DU CHIEN, Issued Date:2/23/2009, Expired Date:2/23/2010 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:EDPW
 +
|-
 +
| Reached Total Depth
 +
| 2009-05-03
 +
| WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED.  PLUGGING AFFIDAVIT REC'D 11/20/2014.  RECORD UPDATED PER SO.
 +
|-
 +
| Completion Report Received
 +
| 2010-03-16
 +
| WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED.  PLUGGING AFFIDAVIT REC'D 11/20/2014.  RECORD UPDATED PER SO.
 +
|-
 +
| APP
 +
| 2010-04-29
 +
| Proposed Formations:PRAIRIE DU CHIEN, Issued Date:4/29/2010, Expired Date:4/29/2011 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| APP
 +
| 2012-09-04
 +
| Proposed Formations:TRENTON THRU PRAIRIE DE CHIEN, Issued Date:9/4/2012, Expired Date:9/4/2014 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Plugged/Abandoned
 +
| 2014-07-23
 +
| WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED.  PLUGGING AFFIDAVIT REC'D 11/20/2014.  RECORD UPDATED PER SO.
 +
|-
 +
| Construction Permit Expires
 +
| 2014-09-04
 +
| WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED.  PLUGGING AFFIDAVIT REC'D 11/20/2014.  RECORD UPDATED PER SO.
 +
|-
 +
| Record Last Modified
 +
| 2018-08-08
 +
| WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED.  PLUGGING AFFIDAVIT REC'D 11/20/2014.  RECORD UPDATED PER SO.
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 2010-07-08
 +
| style="text-align: right;" | 1956
 +
| style="text-align: right;" | 1975
 +
| style="text-align: right;" | 77
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|
 +
| ACID
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 4000 Gal
 +
| style="text-align: right;" | 0
 +
|
 +
| THE ABOVE IS THE LAST OF THREE (3) ACID ATTEMPTS ON DIFFERENT DAYS.  1ST ACID ATTEMPT USED 1200 GAL OF 15% HCL, W/ BREAKDOWN @ 2300 PSI, WITH PRESSURE DECREASE.  SQUEEZE CEMENTED THE PERFS, AND THEN RE-PERFED THE SAME INTERVAL W/ ACID JOB OF 1500 GAL OF 15% HCL, BREAKDOWN OF 1850 PSI, ATP = 640 PSI, ISIP = 600 PSI, AND 5 MIN SIP = 560 PSI.
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| Violations: 0
+
| 2014
 +
| [[DAVID R HILL INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| Latitude: 41.44256912
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| Longitude: -84.5666088
+
| 2014
 +
| [[DAVID R HILL INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| -1096358384
+
| 0192925173
 +
| 2009-05-14
 +
| Production Wells
 +
| No Violations
 +
| All equipment on site. Pits have been backfilled. Large piles of trees and brush on site. Some sediment in ditch at tile discharge but has not reached the creek.
 +
|-
 +
| 0259108517
 +
| 2011-08-18
 +
| Production Wells
 +
| No Violations
 +
| Well shut in. Some gas odor. No production equipment on well. 10 x 10 plastic around wellhead and taped to 4.5 casing. Will contact operator regarding status of well.
 +
|-
 +
| 0943433085
 +
| 2009-04-30
 +
| Production Wells
 +
| No Violations
 +
| Picked up cement tickets from surface casing cementing at 1:00 AM 4/30/09. Spoke to operator on site. No problems with cementing. Drilling has resumed and are now 4 joints below the bottom of the surface casing.
 +
|-
 +
| 1096358384
 
| 2009-04-22
 
| 2009-04-22
|  
+
| Production Wells
 +
| No Violations
 
| Site has been prepared for drilling. Trees have been cleared and pushed into piles. Stone base access road goes down slope to well site. Water was flowing down hill next to road and has caused some erosion and sedimentation.  Well will be near a creek. Spoke to John Suhar by phone and recommended straw bales or silt fence for site.
 
| Site has been prepared for drilling. Trees have been cleared and pushed into piles. Stone base access road goes down slope to well site. Water was flowing down hill next to road and has caused some erosion and sedimentation.  Well will be near a creek. Spoke to John Suhar by phone and recommended straw bales or silt fence for site.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1240852040
 
| 1240852040
 
| 2008-04-27
 
| 2008-04-27
|  
+
| Production Wells
 +
| No Violations
 
| Call from operator about artisian flow of water at depth of about 85 feet. Drove 92 feet of 16 inch pipe into a 20 inch hole and cemented around bottom of pipe. Next drilled 15 inch hole to depth of 164 feet and cemented 158 feet of conductor pipe. Water continued to flow on outside of 16 inch pipe. Operator dug trench approximately 6 feet deep and diverted water to ditch that discharges to creek. Area around 16 inch pipe was also dug to same depth. Gravel was placed around well casing and in trench, then 8 inch PVC pipe placed in trench to control flow. Trench was backfilled. Water again rose to surface around 16 inch pipe. Stone and larger rock along with bentonite was added around 16 inch pipe. Area around 16 inch pipe was capped with cement. It appears as though water has been contained to flow out through 8 inch PVC.
 
| Call from operator about artisian flow of water at depth of about 85 feet. Drove 92 feet of 16 inch pipe into a 20 inch hole and cemented around bottom of pipe. Next drilled 15 inch hole to depth of 164 feet and cemented 158 feet of conductor pipe. Water continued to flow on outside of 16 inch pipe. Operator dug trench approximately 6 feet deep and diverted water to ditch that discharges to creek. Area around 16 inch pipe was also dug to same depth. Gravel was placed around well casing and in trench, then 8 inch PVC pipe placed in trench to control flow. Trench was backfilled. Water again rose to surface around 16 inch pipe. Stone and larger rock along with bentonite was added around 16 inch pipe. Area around 16 inch pipe was capped with cement. It appears as though water has been contained to flow out through 8 inch PVC.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1241629932
 
| 1241629932
 
| 2009-04-27
 
| 2009-04-27
|  
+
| Production Wells
 +
| No Violations
 
| Received call from Don Kreager of David Hill Inc. While drilling conductor hole an artesian water flow was intercepted at about 85 feet depth. The hole was reamed out to 20 inches and a 16 inch casing was cemented in the bottom of the hole at depth of 97 feet to control the water inside the pipe. Stone was used to backfill the annulus side of the pipe. A trench was excavated about 4 feet in depth to allow a 8 inch plastic drain to be placed to remove the water from the wellhead. As the stone reached near the surface bagged clay was added to the stone. The stone and clay dropped several times during the process. Cement was poured at the surface to seal off water from leaking around the wellhead. Water from the drain at the well site discharged into a ditch near the creek.
 
| Received call from Don Kreager of David Hill Inc. While drilling conductor hole an artesian water flow was intercepted at about 85 feet depth. The hole was reamed out to 20 inches and a 16 inch casing was cemented in the bottom of the hole at depth of 97 feet to control the water inside the pipe. Stone was used to backfill the annulus side of the pipe. A trench was excavated about 4 feet in depth to allow a 8 inch plastic drain to be placed to remove the water from the wellhead. As the stone reached near the surface bagged clay was added to the stone. The stone and clay dropped several times during the process. Cement was poured at the surface to seal off water from leaking around the wellhead. Water from the drain at the well site discharged into a ditch near the creek.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1247169482
 
| 1247169482
 
| 2009-07-09
 
| 2009-07-09
|  
+
| Production Wells
| Pits have been backfilled and site has been rough graded but topsoil has not yet been replaced. Several pieces of equipment (water tanker, half tank, excavator and semi with trailer) remain on site. It appears as though work still to be done on well before production. Water discharging from pipe into ditch from artesian flow from well. Trees  windrowwed along edge of disturbed area are supposed to be buried.
+
| No Violations
|
+
|    Pits have been backfilled and site has been rough graded but topsoil has not yet been replaced. Several pieces of equipment (water tanker, half tank, excavator and semi with trailer) remain on site. It appears as though work still to be done on well before production. Water discharging from pipe into ditch from artesian flow from well. Trees  windrowwed along edge of disturbed area are supposed to be buried.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1270060692
 
| 1270060692
 
| 2010-03-31
 
| 2010-03-31
|  
+
| Preliminary Restoration
 +
| No Violations
 
| Area around well has been graded and revegetated. Trees and stumps have been pushed in windrow along tree line. Wood appears being cut for firewood. Plan indicates mulched or buried with landowner approval. Spoke to Don Kreager by phone. Well will be plugged in next few months. Will check with landowner for decision on final plan for disposal of wood and will obtain written consent. Also need to get consent to leave stone surface road to well.
 
| Area around well has been graded and revegetated. Trees and stumps have been pushed in windrow along tree line. Wood appears being cut for firewood. Plan indicates mulched or buried with landowner approval. Spoke to Don Kreager by phone. Well will be plugged in next few months. Will check with landowner for decision on final plan for disposal of wood and will obtain written consent. Also need to get consent to leave stone surface road to well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1337617914
 
| 1337617914
 
| 2012-04-25
 
| 2012-04-25
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| This well has never been put into production and needs to be plugged. A plug permit was issued and then expired in April of 2011. I spoke with a company represetative who indicated they were applying for another plug permit to plug the well this summer.
 
| This well has never been put into production and needs to be plugged. A plug permit was issued and then expired in April of 2011. I spoke with a company represetative who indicated they were applying for another plug permit to plug the well this summer.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1402061161
 
| 1402061161
 
| 2014-04-11
 
| 2014-04-11
|  
+
| Production Wells
 +
| No Violations
 
| At the time of the inspection the well is not in production and never was put into production. A permit to plug the well expires on 9-4-2014. I spoke with David Hill who indicated that Knox Energy, Bill Mitton, is contracted to plug the well before the permit expires.
 
| At the time of the inspection the well is not in production and never was put into production. A permit to plug the well expires on 9-4-2014. I spoke with David Hill who indicated that Knox Energy, Bill Mitton, is contracted to plug the well before the permit expires.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1410794424
 
| 1410794424
 
| 2014-09-15
 
| 2014-09-15
|  
+
| Final Restoration
 +
| No Violations
 
| At the time of the inspection the stone access lane along with stone around the well still needs removed before the land can be farmed. The plugging of the well was completed on 7-24-2014. Don Kreager of David R Hill Inc. was contacted regarding the restoration. He indicated the restoration would be completed, and any necessary waivers signed, before winter. The Final Restoration was not passed.
 
| At the time of the inspection the stone access lane along with stone around the well still needs removed before the land can be farmed. The plugging of the well was completed on 7-24-2014. Don Kreager of David R Hill Inc. was contacted regarding the restoration. He indicated the restoration would be completed, and any necessary waivers signed, before winter. The Final Restoration was not passed.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1532448113
 +
| 2018-07-24
 +
| Final Restoration
 +
| No Violations
 +
| Received landowner waiver to allow access road to remain. Final restoration has been approved.
 
|-
 
|-
| 192925173
+
| 1644011825
| 2009-05-14
+
| 2018-06-13
|  
+
| Final Restoration
| All equipment on site. Pits have been backfilled. Large piles of trees and brush on site. Some sediment in ditch at tile discharge but has not reached the creek.
+
| No Violations
|
+
| Stone access road still in place at the present time. Spoke with Mr. Hill and explained that landowner waiver will be needed in order to approve a final restoration of this site. Final restoration is not approved at this time.
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| 259108517
+
|}-->
| 2011-08-18
 
|
 
| Well shut in. Some gas odor. No production equipment on well. 10' x 10' plastic around wellhead and taped to 4.5 casing. Will contact operator regarding status of well.
 
|
 
|
 
|
 
|-
 
|-
 
| 943433085
 
| 2009-04-30
 
|
 
| Picked up cement tickets from surface casing cementing at 1:00 AM 4/30/09. Spoke to operator on site. No problems with cementing. Drilling has resumed and are now 4 joints below the bottom of the surface casing.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 20:38, 24 July 2019

Well Details

Well ID: 34-171-20065
Loading map...
Country: United States
State: Ohio
County: Williams
Municipality: Pulaski Township
Operator Name: DAVID R HILL INC
Well Pad ID:
Farm/Lease Name: W MUSSER
License Status: Final Restoration
License Date: 2018-07-24
Spud Date: 2009-04-23
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2009-05-03
Well Total Depth: 2739 ft
Configuration: Vertical
Latitude: 41.442312186
Longitude: -84.56670826

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2009-02-23 Proposed Formations:TRENTON THRU PRAIRIE DU CHIEN, Issued Date:2/23/2009, Expired Date:2/23/2010 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2009-05-03 WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED. PLUGGING AFFIDAVIT REC'D 11/20/2014. RECORD UPDATED PER SO.
Completion Report Received 2010-03-16 WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED. PLUGGING AFFIDAVIT REC'D 11/20/2014. RECORD UPDATED PER SO.
APP 2010-04-29 Proposed Formations:PRAIRIE DU CHIEN, Issued Date:4/29/2010, Expired Date:4/29/2011 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2012-09-04 Proposed Formations:TRENTON THRU PRAIRIE DE CHIEN, Issued Date:9/4/2012, Expired Date:9/4/2014 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-07-23 WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED. PLUGGING AFFIDAVIT REC'D 11/20/2014. RECORD UPDATED PER SO.
Construction Permit Expires 2014-09-04 WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED. PLUGGING AFFIDAVIT REC'D 11/20/2014. RECORD UPDATED PER SO.
Record Last Modified 2018-08-08 WELL WAS NOT PUT INTO PRODUCTION AFTER SEVERAL ATTEMPTS TO COMPLETE IT, NOR HAS IT BEEN PLUGGED. PLUGGING AFFIDAVIT REC'D 11/20/2014. RECORD UPDATED PER SO.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2010-07-08 1956 1975 77

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 4000 Gal 0 THE ABOVE IS THE LAST OF THREE (3) ACID ATTEMPTS ON DIFFERENT DAYS. 1ST ACID ATTEMPT USED 1200 GAL OF 15% HCL, W/ BREAKDOWN @ 2300 PSI, WITH PRESSURE DECREASE. SQUEEZE CEMENTED THE PERFS, AND THEN RE-PERFED THE SAME INTERVAL W/ ACID JOB OF 1500 GAL OF 15% HCL, BREAKDOWN OF 1850 PSI, ATP = 640 PSI, ISIP = 600 PSI, AND 5 MIN SIP = 560 PSI.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2014 DAVID R HILL INC 0 0 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2014 DAVID R HILL INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0192925173 2009-05-14 Production Wells No Violations All equipment on site. Pits have been backfilled. Large piles of trees and brush on site. Some sediment in ditch at tile discharge but has not reached the creek.
0259108517 2011-08-18 Production Wells No Violations Well shut in. Some gas odor. No production equipment on well. 10 x 10 plastic around wellhead and taped to 4.5 casing. Will contact operator regarding status of well.
0943433085 2009-04-30 Production Wells No Violations Picked up cement tickets from surface casing cementing at 1:00 AM 4/30/09. Spoke to operator on site. No problems with cementing. Drilling has resumed and are now 4 joints below the bottom of the surface casing.
1096358384 2009-04-22 Production Wells No Violations Site has been prepared for drilling. Trees have been cleared and pushed into piles. Stone base access road goes down slope to well site. Water was flowing down hill next to road and has caused some erosion and sedimentation. Well will be near a creek. Spoke to John Suhar by phone and recommended straw bales or silt fence for site.
1240852040 2008-04-27 Production Wells No Violations Call from operator about artisian flow of water at depth of about 85 feet. Drove 92 feet of 16 inch pipe into a 20 inch hole and cemented around bottom of pipe. Next drilled 15 inch hole to depth of 164 feet and cemented 158 feet of conductor pipe. Water continued to flow on outside of 16 inch pipe. Operator dug trench approximately 6 feet deep and diverted water to ditch that discharges to creek. Area around 16 inch pipe was also dug to same depth. Gravel was placed around well casing and in trench, then 8 inch PVC pipe placed in trench to control flow. Trench was backfilled. Water again rose to surface around 16 inch pipe. Stone and larger rock along with bentonite was added around 16 inch pipe. Area around 16 inch pipe was capped with cement. It appears as though water has been contained to flow out through 8 inch PVC.
1241629932 2009-04-27 Production Wells No Violations Received call from Don Kreager of David Hill Inc. While drilling conductor hole an artesian water flow was intercepted at about 85 feet depth. The hole was reamed out to 20 inches and a 16 inch casing was cemented in the bottom of the hole at depth of 97 feet to control the water inside the pipe. Stone was used to backfill the annulus side of the pipe. A trench was excavated about 4 feet in depth to allow a 8 inch plastic drain to be placed to remove the water from the wellhead. As the stone reached near the surface bagged clay was added to the stone. The stone and clay dropped several times during the process. Cement was poured at the surface to seal off water from leaking around the wellhead. Water from the drain at the well site discharged into a ditch near the creek.
1247169482 2009-07-09 Production Wells No Violations Pits have been backfilled and site has been rough graded but topsoil has not yet been replaced. Several pieces of equipment (water tanker, half tank, excavator and semi with trailer) remain on site. It appears as though work still to be done on well before production. Water discharging from pipe into ditch from artesian flow from well. Trees windrowwed along edge of disturbed area are supposed to be buried.
1270060692 2010-03-31 Preliminary Restoration No Violations Area around well has been graded and revegetated. Trees and stumps have been pushed in windrow along tree line. Wood appears being cut for firewood. Plan indicates mulched or buried with landowner approval. Spoke to Don Kreager by phone. Well will be plugged in next few months. Will check with landowner for decision on final plan for disposal of wood and will obtain written consent. Also need to get consent to leave stone surface road to well.
1337617914 2012-04-25 Drill / Deepen / Reopen No Violations This well has never been put into production and needs to be plugged. A plug permit was issued and then expired in April of 2011. I spoke with a company represetative who indicated they were applying for another plug permit to plug the well this summer.
1402061161 2014-04-11 Production Wells No Violations At the time of the inspection the well is not in production and never was put into production. A permit to plug the well expires on 9-4-2014. I spoke with David Hill who indicated that Knox Energy, Bill Mitton, is contracted to plug the well before the permit expires.
1410794424 2014-09-15 Final Restoration No Violations At the time of the inspection the stone access lane along with stone around the well still needs removed before the land can be farmed. The plugging of the well was completed on 7-24-2014. Don Kreager of David R Hill Inc. was contacted regarding the restoration. He indicated the restoration would be completed, and any necessary waivers signed, before winter. The Final Restoration was not passed.
1532448113 2018-07-24 Final Restoration No Violations Received landowner waiver to allow access road to remain. Final restoration has been approved.
1644011825 2018-06-13 Final Restoration No Violations Stone access road still in place at the present time. Spoke with Mr. Hill and explained that landowner waiver will be needed in order to approve a final restoration of this site. Final restoration is not approved at this time.

For data sources see[9]

References