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Well ID: 37-127-20016 | Loading map...
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Operator Name: NEWFIELD APPALACHIA PA LLC | |
First Permit Date: 2010-04-30 | |
Last Permit Date: 2010-04-30 | |
Spud Date: 2010-08-09 | |
Unconventional: No | |
Horizontal: No | |
Violations: None | |
Latitude: 41.677191 | |
Longitude: -75.082427 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2010-0 | DRILLING FLUID WASTE | 4507.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 | EUREKA RESOURCES (WILLIAMSPORT WATER TREATMENT) | WILLIAMSPORT | PA |
2010-0 | DRILL CUTTINGS | 506.0 | Tons | LANDFILL | 101247 | KEYSTONE SANITARY LANDFILL | DUNMORE | PA |
2010-0 | DRILLING FLUID WASTE | 1348.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0102784 | WASTE TREATMENT CORPORATION | WARREN | PA |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1912369 | 2010-09-02 | No Violations Noted | UDI rig on site. Plastic on site underneath substructure. Closed loop. Drilling to start saturday or sunday. Proper site id sign and permit on site. No violations observed. | |
1914998 | 2010-09-22 | No Violations Noted | UDI Rig 48. TIH at time of inspection. Have just replaced bit. Depth of drilling at 3079'. Reported cement returns to surface on both the 13 3/8" and 9 5/8" casing strings. Area under substructure and all equipment is covered in plastic and bermed to contain spills. No violations were observed. | |
1924115 | 2010-10-22 | No Violations Noted | Rig has been moved off location. Crews on site cleaning out frac tanks and cleaning up site. Well is shut in. Well has been loaded with mud temporarily. Operator planning on returning to well after winter. | |
1926589 | 2010-11-02 | No Violations Noted | Mike O'Donnell and I conducted an inspection of this site. We recommend that the facility update the E&S plan to accurately reflect the controls as installed. No violations noted today. | |
1946691 | 2011-01-28 | No Violations Noted | ||
2009344 | 2011-10-06 | No Violations Noted | DEP on site at 9 am. Operator has filed for Inactive Status. Site is secured by entrance gate, and chain-link fence is around well head. WEll is temoporarily plugged. No personnel or activity on site. E& S controls in place and appear to be working. Pad and acces are gravel based.. | |
2099637 | 2012-08-30 | No Violations Noted | On site @ 10 am. Met with Company Man Pat Parsons. At time of inspection - rigging up to begin plugging and abandoning well. Secondary containment in place. Checked cellar - no evidence of gas bubbling at surface. Once complete - well head will be removed and casing cut off below grade and backfilled. Cap will be installed on well with permit number welded on cap. No violations observed at time of inspection. | |
2102829 | 2012-09-26 | No Violations Noted | Inspection conducted on 9/26/12 to determine if silt sock will need to be replaced before reclamation activities in the form of earth moving are to commence. Yes, the silt sock needs to be replaced. Cellar is filled with water, unable to see well casing. Rat hole has a seal welded on top. | |
2155625 | 2013-04-09 | Wayne | Damascus Twp | No Violations Noted |