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| Well ID: 34-083-20163 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Knox | |
| Municipality: Howard Township | |
| Operator Name: MARAM ENERGY INC | |
| Well Pad ID: | |
| Farm/Lease Name: SIMPSON CHARLES & ZELLA | |
| License Status: Producing | |
| License Date: 2013-03-18 | |
| Spud Date: | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1937-10-09 | |
| Well Total Depth: 2688.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.420000 | |
| Longitude: -82.330000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Completed | 1937-10-09 | QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002 |
| Reached Total Depth | 1937-10-09 | QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002 |
| APP | 1999-12-15 | Proposed Formations:CLINTON, Issued Date:12/15/99, Expired Date:12/14/00 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2000-12-14 | Proposed Formations:CLINTON, Issued Date:12/14/2000, Expired Date:12/14/2001 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2002-02-15 | Proposed Formations:CLINTON, Issued Date:2/15/2002, Expired Date:2/15/2003 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2002-02-15 | QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002 |
| APP | 2010-07-09 | Proposed Formations:CLINTON, Issued Date:7/9/2010, Expired Date:7/9/2011 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2013-03-18 | Proposed Formations:, Issued Date:3/18/2013, Expired Date:3/18/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| Record Last Modified | 2014-08-13 | QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002 |
| Construction Permit Expires | 2015-03-18 | QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 0 | 0 | 0 |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | PERKINS SIDNEY | 0.00 | 0.00 | 0 |
| 2005 | MARAM ENERGY INC | 0.00 | 0.00 | 150 |
| 2006 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2007 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2008 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2009 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2010 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2011 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2012 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2013 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| 2014 | MARAM ENERGY INC | 0.00 | 0.00 | 0 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | PERKINS SIDNEY | Brine | 0 | 0 |
| 2005 | MARAM ENERGY INC | Brine | 0 | 150 |
| 2006 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2007 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2008 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2009 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2010 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2011 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2012 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2013 | MARAM ENERGY INC | Brine | 0 | 0 |
| 2014 | MARAM ENERGY INC | Brine | 90 | 0 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1022735037 | 2015-3-9 0:00:0 | PB | No Violations | |
| -1395882410 | 2014-12-15 0:00 | PB | No Violations | |
| -1839822235 | 2014-12-18 0:00 | PW | No Violations | |
| -1911254236 | 2015-3-4 0:00:0 | PB | No Violations | |
| -2020174091 | 2015-1-5 0:00:0 | PB | No Violations | |
| -2065072911 | 2015-2-9 0:00:0 | PB | No Violations | |
| -526820111 | 2015-3-16 0:00: | PB | No Violations | |
| -965730803 | 2015-5-21 0:00: | PB | No Violations | |
| 0288328235 | 2015-01-06 | Plug / Plug Back | No Violations | There was no one on site during this inspection. The service rig is setting idle on location. |
| 0526820111 | 2015-03-16 | Plug / Plug Back | No Violations | The service rig has moved off the well still needs more clay to finish the top of the plug, 8 inch cut off and well id plate. |
| 0693655615 | 2015-03-12 | Plug / Plug Back | No Violations | In the process of cutting off the drive pipe and welding on a 8 inch nipple to pull the surface casing went to get more clay to finish plugging the surface hole again the clay company has no clay they will try again tomorrow. |
| 0958557686 | 2015-03-11 | Plug / Plug Back | No Violations | Washing in clay from brush and stone plug to surface casing, preparing to pull 8 inch surface casing. |
| 0965730803 | 2015-05-21 | Plug / Plug Back | No Violations | Maram Energy moved their service rig back on location to finish plugging this well today. |
| 0967225577 | 2015-06-02 | Plug / Plug Back | No Violations | This well has finished being plugged, and the area has been reclaimed of all the production equipment has been removed, and all the debris have been cleaned up. The landowner is in the process of planting the area in crops as well. |
| 1022735037 | 2015-03-09 | Plug / Plug Back | No Violations | They are in the process of driving out a bridge that occurred when dropping in the stone for the brush and stone plug. |
| 1029132993 | 2014-12-24 | Plug / Plug Back | No Violations | Plugging with Maram Energy today pulling 3 inch after shooting it off. |
| 1395882410 | 2014-12-15 | Plug / Plug Back | No Violations | This well is in the process of being plugged and abandoned, the service rig is on site the pump jack has been removed the rods pulled, the pipe is scheduled to be shot off and pulled. This will also satisfy a prior compliance notice to plug this well once completed. |
| 1398375250 | 2014-04-24 | Final Restoration | No Violations | This inspection was for a final restoration. The well is still equipped with a pumping unit and a single tank. The well has not been produced for some time according to the production records on this well. The records also state this well was plugged in 2002. The well has no identification posted. The well needs to be plugged to be compliant with the law. |
| 1426519591 | 2015-03-13 | Plug / Plug Back | No Violations | Today they attempted to pull the 8 inch surface casing after several trys it is decided to leave the surface casing and plug to surface. |
| 1491937034 | 2015-02-24 | Plug / Plug Back | No Violations | Plugging operations are ongoing with this well the 3 inch has been recovered, the bottom hole clay plug has been set, the 5 inch production casing has been shot off at 1495 feet and the casing has been recovered. |
| 1839822235 | 2014-12-18 | Production Wells | Violations Noted | This well is in the process of being plugged and satisfies the Compliance Notice. |
| 1909045638 | 2015-03-03 | Plug / Plug Back | No Violations | Plugging operations were going on during this inspection clay was being washed in to finish the bottom plug after ripping and pulling the production casing. |
| 1911254236 | 2015-03-04 | Plug / Plug Back | No Violations | Plugging operations were on going. They were setting a brush and stone plug to finish washing the top plug after pulling the surface casing. |
| 2020174091 | 2015-01-05 | Plug / Plug Back | No Violations | Plugging operations are underway on this well the clay was delivered today. No one was on site during this inspection. |
| 2065072911 | 2015-02-09 | Plug / Plug Back | No Violations | I witnessed plugging operations on this well. Maram Energy plugging with clay. Approximately 230 shovels of clay were washed in. The 5.5 casing will be shot later this week. Refer to plug report for details. Time of inspection: 1:15 PM. Weather: 25 degrees F, Cloudy |
| 288328235 | 2015-1-6 0:00:0 | PB | No Violations | |
| 693655615 | 2015-3-12 0:00: | PB | No Violations | |
| 958557686 | 2015-3-11 0:00: | PB | No Violations | |
| 967225577 | 2015-6-2 0:00:0 | PB | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 1839822235 | US-OH-118372 | 2014-12-29 | Failure to legibly identify well | |
| 1839822235 | US-OH-118373 | 2014-12-29 | Well shall be plugged |
For data sources see[8]