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34-069-20058

Well Details

Well ID: 34-069-20058
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County: Henry
Municipality:
Operator Name: OGE ENERGY LTD
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1975-10-29
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.33920904
Longitude: -83.95704684

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1991-0 0.0 0.0
1999-0 5188.0 71.0
2000-0 3444.0 110.0
2001-0 4102.0 429.0
2002-0 53.0 6.0
2003-0 0.0 0.0
2004-0 0.0 0.0
2005-0 2854.0 0.0
2006-0 1844.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1128629877 2015-02-11 At the time of the inspection the well was still shut in and has not produced since the previous inspection on 1-31-2013. The well is capable of production but no Production Records have been filed since 2006. No Hydrogen Sulfide was detected but this is a known Hydrogen Sulfide area so precaution should be taken during any service or plugging work. There has been no response from OGE Energy to previous Compliance Notice #1220415853 issued on 9-8-2011. This well is hereby ordered to be plugged and the land restored by 9-11-2015. Field Visit or Inspection
-1128629877 2015-02-11 At the time of the inspection the well was still shut in and has not produced since the previous inspection on 1-31-2013. The well is capable of production but no Production Records have been filed since 2006. No Hydrogen Sulfide was detected but this is a known Hydrogen Sulfide area so precaution should be taken during any service or plugging work. There has been no response from OGE Energy to previous Compliance Notice #1220415853 issued on 9-8-2011. This well is hereby ordered to be plugged and the land restored by 9-11-2015. Field Visit or Inspection
-1128629877 2015-02-11 At the time of the inspection the well was still shut in and has not produced since the previous inspection on 1-31-2013. The well is capable of production but no Production Records have been filed since 2006. No Hydrogen Sulfide was detected but this is a known Hydrogen Sulfide area so precaution should be taken during any service or plugging work. There has been no response from OGE Energy to previous Compliance Notice #1220415853 issued on 9-8-2011. This well is hereby ordered to be plugged and the land restored by 9-11-2015.
1220415853 2011-08-05 Well located in bean field. No lane to well. 4 casing with casing head, 2 tubing, and rods. No pumpjack on well. Well shut in on annulus and tubing. 72 psi still on guage on production lines. No guage on well. I.D. on site still identifies previous owner Aurora Energy. No production records since 2006.
1363115432 2013-01-31 At the time of the inspection the well was shut in and the gauge indicates 20 psi on the production line. There was no gauge on the annulus and no sign of any leaks. The corrective action from the Compliance Notice issued in 2011 has not been completed. The inspection was done at the request of Eric Vendel from The Ohio Division of Oil and Gas.
273667047 2012-01-04 No change from last inspection. NOV's from last inspection on 8/5/2011 still need resolved.
-292804802 2015-04-29 At the time of the inspection, gauge on 2 inch tubing reads 20 psi and production and surface casing is in poor condition

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.