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34-063-20352

Well Details

Well ID: 34-063-20352
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County: Hancock
Municipality:
Operator Name: INNEX OIL AND GAS INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2006-10-27
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 41.15393718
Longitude: -83.61037872

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2007-0 0.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0
2013-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1181229868 2007-06-07 Preliminary restoration done. Storage facilities in place, pits closed and an agricultural crop has been planted on the site. Identification has been posted at the storage site.
-1203696497 2013-03-11 At the time of my inspection the tubing and submersible pump were removed from the well. The 1.5 tubing was ran back in the hole but more tubing will be needed to reach the plugging depth of 1175'.
1223567817 2008-10-09 Chk well and storsag, Ok.
1286895145 2010-10-12 Status is shut in, the well is not in production at this time. Is equipped to produce.
1310406908 2011-07-11 Tank Battery clean w/ no leaks. Well closed to separator but unsure if open to tanks. 4 at well is open but unsure if 1.5 is open at wellhead. I.D. at tank still for Hunt Petroleum and not current owner, Innex Oil & Gas Inc. No ID at wellhead. Believe well is still shut in. No production reported.
1317385309 2011-09-30 New ID posted. Tank battery emptied by Frantz Oil Co. and disposed of at their injection well. Innex is looking to apply for a Temporarily Inactive Status.
1323883873 2011-12-14 Temporary Inactive Status inspection. Site clean and ID posted. Tanks removed from location but meter and seperator left in 75' x 20' containment dike. Well shut in and production lines clean.
1363269308 2013-03-13 At the time of the inspection, 1200' of 1.5 tubing was ran in the well. Petroset Cementing pumped 35 sacks of 50/50 poz mix down the well with good circulation throughout the job. Please see Plug Report for details.
1363283952 2013-03-14 At the time of the inspection the rig was set back on the well and the cement was tagged at 790'. All remaining fluids were removed to 500' in preparation for the top plug.
1363351913 2013-03-15 At the time of the inspection the top plug was set from 500' to the surface with two yards of 9 sack grout inside 4.5 casing. The 4.5 casing was cemented to the surface when the well was drilled.
-1386359541 2013-03-28 At the time of the inspection the well was cut off and the identification plate was put on top. The hole was then filled and the area was graded for farm use. All production lines and the tank battery were removed.
2008027874 2011-10-11 Tank battery removed but stone dike still in place. The small seperator located in the dike is still plumbed back to well which is shut in. ID is posted. Owner indicates they will plug well or apply for Temporary Inactive Status.
2042364872 2011-09-14 Well still shut in. Talked with Chuck Knox who indicated new signs will arrive this week and will be posted promptly. Also, the tank battery will be cleaned up. Innex is looking into applying for Temporarily Inactive Status.
-2143093831 2013-03-08 At the time of my inspection a service rig from Second Oil Co. was on location along with a half-tank and other equipment. A plug permit was received and preparations are being made for the plugging of the well.
-428169811 2007-11-28 Preliminary restoration done.
-542010586 2015-03-10 This well was plugged and abandoned on 3-19-2013 and the Final Restoration was completed shortly after that. The stone laid for the entrance along with the electrical hookup was requested to be left by the farmer contracted to farm the land. A Landowner Waiver, Form 5, was needed to complete the Final Restoration and was received on 3-9-2015. Final Restoration Passed.
-877674373 2013-11-28 At the time of the inspection the area had been graded back for farm use by the plugging contractor. The site is currently being planted by the landowner. Waiting on a Landowner Waiver for the lane and electric lines/outlet.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.