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37-063-23713

Well Details

Well ID: 37-063-23713
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Operator Name: CNX GAS CO LLC
First Permit Date: 1977-03-24
Last Permit Date: 1977-03-24
Spud Date: 1977-03-26
Unconventional: No
Horizontal: No
Violations: None
Latitude: 40.474902
Longitude: -79.254413

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 2626.63 365.0 0.0 0.0 0.0 0.0
2012-0 2679.0 366.0 0.0 0.0 28.5 366.0
2011-0 0.0 0.0 0.0 0.0 0.0 0.0
2011-0 2116.94 365.0 0.0 0.0 0.0 0.0
2010-0 2706.0 365.0 0.0 0.0 0.0 0.0
2009-0 2281.95 365.0 0.0 0.0 20.0 365.0
2008-0 3783.29 365.0 0.0 0.0 0.0 0.0
2007-0 4273.0 365.0 0.0 0.0 0.0 0.0
2006-0 2855.0 365.0 0.0 0.0 0.0 0.0
2005-0 1320.0 365.0 0.0 0.0 0.0 0.0
2003-0 1942.0 365.0 0.0 0.0 0.0 0.0
2002-0 3387.0 365.0 0.0 0.0 77.01 0.0
2001-0 2328.0 365.0 0.0 0.0 0.0 0.0
2000-0 1985.0 365.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-0 PRODUCED FLUID 35.0 Bbl INJECTION DISPOSAL WELL 34-155-21447 KLEESE #2 (SWIW #19) - KLEESE DEVELOPMENT ASSOCS VIENNA OH
2002-0 BRINE 23.63 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT FRANKLIN BRINE TREATMENT
2002-0 BRINE 23.63 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT TUNNELTON LIQUIDS CO.
2003-0 BRINE 23.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT TUNNELTON LIQUIDS COMPANY
2009-0 BRINE 25.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT PA BRINE TRT - JOSEPHINE PLT -INDIANA CO
2012-0 PRODUCED FLUID 35.0 Bbl INJECTION DISPOSAL WELL 34-155-21447 KLEESE #2 (SWIW #19) - KLEESE DEVELOPMENT ASSOCS VIENNA OH

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1855430 2010-01-07 No Violations Noted Well was drilled on 3/24/77 to depth of 3781 ft. Well head consisted of 8¿ pipe reduced to 4 ¿pipe and reduced to 2¿ production which contained three shut off valves. Dual data logger showed 180 psi/5 psi. Production equipment consisted of separator (200 psi) and brine tank. The 100 bbl tank contained 30 bbl of brine fluid. At the time of inspection no E&S issues and IW releases at the site.

References