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37-063-20694

Well Details

Well ID: 37-063-20694
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Operator Name: EXCO RESOURCES PA INC
First Permit Date: 1965-11-29
Last Permit Date: 1965-11-29
Spud Date: 1965-12-31
Unconventional: No
Horizontal: No
Violations: None
Latitude: 40.648164
Longitude: -79.030493

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-0 2484.0 365.0 0.0 0.0 0.0 0.0
2009-0 6631.0 365.0 0.0 0.0 0.0 0.0
2008-0 8376.0 365.0 0.0 0.0 0.0 0.0
2007-0 0.0 0.0 0.0 0.0 0.0 0.0
2006-0 5503.8 365.0 0.0 0.0 0.0 0.0
2005-0 4289.0 365.0 0.0 0.0 0.0 0.0
2004-0 4862.0 365.0 0.0 0.0 0.0 365.0
2003-0 5453.0 365.0 0.0 0.0 0.0 0.0
2002-0 7591.0 365.0 0.0 0.0 0.0 0.0
2001-0 8317.0 328.0 0.0 0.0 0.0 0.0
2000-0 6644.0 365.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2000-0 BRINE 371.0 Bbl INJECTION DISPOSAL WELL SPENCER LADN #2
2001-0 BRINE 106.0 Bbl INJECTION DISPOSAL WELL SPENCER DW
2005-0 BRINE 110.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT FRANKLIN BRINE--INDIANA PLT
2005-0 BRINE 110.0 Bbl INJECTION DISPOSAL WELL SPENCER LAND CO #2 DISP WELL (033-22059)
2006-0 BRINE 72.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT PA BRINE TRT - JOSEPHINE PLT -INDIANA CO
2008-0 BRINE 805.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT PA BRINE TRT - JOSEPHINE PLT -INDIANA CO
2009-0 BRINE 190.0 Bbl INJECTION DISPOSAL WELL IRVIN A SALT WATER DISPOSAL
2010-0 PRODUCED FLUID 100.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PAS2D205BCLE IRVIN A SALTWATER DISPOSAL PA
2010-0 PRODUCED FLUID 80.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY JOSEPHINE PA
2010-0 PRODUCED FLUID 400.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR DRILLING OR PLUGGING PA

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
566351 1993-11-19 Violation(s) Noted NO ID;E&S OK;3 TANKS 102378
566538 1994-04-06 No Violations Noted TAG ON; E&S OK
1886320 2010-05-19 No Violations Noted Remarks: Alternate method of plugging approved for well, previously in 2008 rig was unable to remove packer in hole at 6,886 ft. Presently operator plugged well through existing tubing string below packer set depth plugging over Oriskany formation. During plugging tubing string was cemented in place. Cement was present on inside of tubing at 5,108 ft. with log indicated cement top on annulus at 1987 ft. Tubing string and 5 ½ production string were shot off at 1/987 ft. Well was circulated with continuous plug from 1,987 ft to surface.
1887964 2010-05-19 No Violations Noted plugging/E&S ok/pit&tag ok
1889526 2010-06-07 In Compliance with Policy alt meth of plugging review/approval
1969555 2011-04-28 No Violations Noted

References