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| Well ID: 34-115-24484 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Morgan | |
| Municipality: Deerfield Township | |
| Operator Name: ECLIPSE RESOURCES-OHIO LLC | |
| Well Pad ID: | |
| Farm/Lease Name: SULLIVAN JOHN T | |
| License Status: Final Restoration | |
| License Date: 2014-06-26 | |
| Spud Date: 2002-07-25 | |
| Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS | |
| Final Drill Date: 2002-07-29 | |
| Well Total Depth: 4237.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.710000 | |
| Longitude: -81.970000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2002-05-09 | Proposed Formations:CLINTON, Issued Date:5/9/2002, Expired Date:5/9/2003 6:00:00 AM, Drilling unit acres:78, Proposed Well Type:OG, Proposed Well Class:POOL |
| Original Spud | 2002-07-25 | RBDMS Rec |
| Completed | 2002-07-29 | RBDMS Rec |
| Reached Total Depth | 2002-07-29 | RBDMS Rec |
| Completion Report Received | 2002-11-26 | RBDMS Rec |
| APP | 2010-04-05 | Proposed Formations:CLINTON, Issued Date:4/5/2010, Expired Date:4/5/2011 6:00:00 AM, Drilling unit acres:78, Proposed Well Type:OG, Proposed Well Class: |
| Change of Owner | 2014-02-06 | Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC |
| APP | 2014-06-26 | Proposed Formations:CLINTON, Issued Date:6/26/2014, Expired Date:6/25/2016 12:00:00 PM, Drilling unit acres:78, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2014-08-22 | RBDMS Rec |
| Construction Permit Expires | 2016-06-25 | RBDMS Rec |
| Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2003-01-23 | 4162 | 4181 | 20 |
| 4162 | 4181 | 20 | |
| 4162 | 4181 | 20 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 15 | 2428 Bbl | 20000 | 500 GALLONS HCL ACID |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2002 | OXFORD OIL | 0.00 | 0.00 | 48 |
| 2003 | OXFORD OIL | 6006.00 | 51.00 | 365 |
| 2004 | OXFORD OIL | 5424.00 | 20.00 | 365 |
| 2005 | OXFORD OIL | 3320.00 | 37.00 | 365 |
| 2006 | OXFORD OIL | 2953.00 | 28.00 | 365 |
| 2007 | OXFORD OIL | 3086.00 | 32.00 | 365 |
| 2008 | OXFORD OIL | 2706.00 | 31.00 | 0 |
| 2009 | OXFORD OIL | 3101.00 | 0.00 | 0 |
| 2010 | OXFORD OIL | 3430.00 | 31.00 | 365 |
| 2011 | OXFORD OIL | 2926.00 | 55.00 | 0 |
| 2012 | OXFORD OIL | 2185.00 | 0.00 | 0 |
| 2013 | ECLIPSE RESOURCES-OHIO LLC | 1082.00 | 27.00 | 365 |
| 2014 | ECLIPSE RESOURCES-OHIO LLC | 5.00 | 0.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2002 | OXFORD OIL | Brine | 0 | 48 |
| 2003 | OXFORD OIL | Brine | 1930 | 365 |
| 2004 | OXFORD OIL | Brine | 1381 | 365 |
| 2005 | OXFORD OIL | Brine | 1285 | 365 |
| 2006 | OXFORD OIL | Brine | 1423 | 365 |
| 2007 | OXFORD OIL | Brine | 1424 | 365 |
| 2008 | OXFORD OIL | Brine | 1251 | |
| 2009 | OXFORD OIL | Brine | 1332 | |
| 2010 | OXFORD OIL | Brine | 1322 | 365 |
| 2011 | OXFORD OIL | Brine | 1200 | |
| 2012 | OXFORD OIL | Brine | 1067 | |
| 2013 | ECLIPSE RESOURCES-OHIO LLC | Brine | 670 | 365 |
| 2014 | ECLIPSE RESOURCES-OHIO LLC | Brine | 18 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1300796479 | 2014-8-15 0:00: | PB | No Violations | |
| 0128888737 | 2014-12-31 | Final Restoration | No Violations | Location meets 1509.072 final restoration requirements. |
| 0245595530 | 2004-04-05 | Production Wells | No Violations | No violations noted on the day of my inspection. |
| 128888737 | 2014-12-31 0:00 | FR | No Violations | 0.50 |
| 1300796479 | 2014-08-15 | Plug / Plug Back | No Violations | Operator successfully removed the casing head and Timco came on location this morning and shot the 5.5 casing off at 3475. They pulled one joint then had equipment issues and are down for the rest of the day. |
| 1407774651 | 2014-08-11 | Plug / Plug Back | No Violations | I was on location with Francis Brothers Well Services to witness Formation Cement Company set a 300 bottom hole plug using 35 sacks of Class A cement through 2 3/8 tubing. The bottom was tagged at 4193 and the tubing was set at 4182. Wireline services will be out tomorrow to run a cement bond log in order to determine the top of cement on the 5.5 casing. |
| 1407858634 | 2014-08-12 | Plug / Plug Back | No Violations | Timco Wireline Services arrived on location to run a cement bond log to determine the top of cement on the 5.5. The top of the bottom hole plug was at 3792 and the top of 5.5 cement was at 3550. Timco shot off the 5.5 casing at 3508. The operator needs to work on getting the casing head loose and will then pull all of the 5.5. They will then run the 2 3/8 tubing back down hole to set the rest of the plugs on Thursday. |
| 1408633482 | 2014-08-21 | Plug / Plug Back | No Violations | Timco Wireline Services shot the casing off again at 3475 and pulled all of the 5.5 from the hole. They then ran the 2 3/8 tubing back down to 3108. Formation Cement Company arrived today to set the Big Lime plug from 2908-3108. Francis Brothers then pulled 57 joints up to 1412. Formation then set the Berea plug from 1202-1412. There was no circulation. They will sit on the plugs overnight and resume tomorrow. |
| 1408726796 | 2014-08-22 | Plug / Plug Back | No Violations | The Berea plug was tagged at 1413 and another 209 feet of Class A cement was placed on top of that from was placed on top from 1410-1202. The Bottom of the Surface casing plug was placed from 1045-869 feet and the Surface plug was placed from 106-0. circulation was established and the Surface plug did not fall. |
| 245595530 | 2004-4-5 0:00:0 | PW | No Violations |
For data sources see[9]