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Difference between revisions of "37-111-20016"

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[[Category:Wells]]

Revision as of 09:17, 29 June 2014

Well Details

Well ID: 37-111-20016
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First Permit Date: 2016-08-23
Last Permit Date: 2016-08-23
Spud Date: 1960-01-10
Unconventional: No
Horizontal: No
Violations: 2
Latitude: 40.080469
Longitude: -79.073922

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 9400.0 365.0 0.0 0.0 0.0 0.0
2012-0 5814.0 366.0 0.0 0.0 0.0 0.0
2011-0 0.0 0.0 0.0 0.0 0.0 0.0
2011-0 13806.0 365.0 0.0 0.0 0.0 0.0
2010-0 15170.0 365.0 0.0 0.0 0.0 0.0
2009-0 14927.0 365.0 0.0 0.0 0.0 0.0
2008-0 21547.0 365.0 0.0 0.0 0.0 0.0
2007-0 0.0 0.0 0.0 0.0 0.0 0.0
2006-0 22283.0 365.0 0.0 0.0 0.0 0.0
2006-0 0.0 0.0 0.0 0.0 0.0 0.0
2005-0 20105.0 365.0 0.0 0.0 0.0 0.0
2004-0 0.0 0.0 0.0 0.0 0.0 0.0
2003-0 21621.0 365.0 0.0 0.0 0.0 0.0
2002-0 23394.0 365.0 0.0 0.0 0.0 0.0
2001-0 27383.0 365.0 0.0 0.0 0.0 0.0
2000-0 23237.0 365.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-0 PRODUCED FLUID 49.0 Bbl INJECTION DISPOSAL WELL 34-155-23584 KOONTZ #1 DISPOSAL WELL WARREN OH
2012-0 PRODUCED FLUID 34.98 Bbl INJECTION DISPOSAL WELL 37-111-20006 MORRIS H CRITCHFIELD F76 DISP WELL PAS2D912BSOM FRIEDENS PA
2001-0 BRINE 477.0 Bbl MUNICIPAL SEWAGE TREATMENT PLANT JOHNSTOWN STP
2002-0 BRINE 515.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT FRANKLIN BRINE -- FRANKLIN PLT
2003-0 BRINE 87.0 Bbl INJECTION DISPOSAL WELL DOMINION EXPLOR & PROD - CRITC
2005-0 BRINE 393.0 Bbl INJECTION DISPOSAL WELL DOMINION EXP
2005-0 BRINE 393.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT JOHNSTOWN STP
2005-0 BRINE 393.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT TUNNELTON LIQUIDS COMPANY
2008-0 BRINE 677.0 Bbl INJECTION DISPOSAL WELL CRITCHFIELD #F76 DISP WELL (111-20006)
2008-0 BRINE 677.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT JOHNSTOWN STP
2008-0 BRINE 677.0 Bbl OTHER STORAGE PENDING DISPOSAL OR REUSE
2009-0 BRINE 342.0 Bbl OTHER J.P. GEARY #1 - 47-023-0034
2009-0 BRINE 342.0 Bbl MUNICIPAL SEWAGE TREATMENT PLANT JOHNSTOWN STP
2009-0 BRINE 342.0 Bbl OTHER STECKMAN RIDGE 37-009-20078
2009-0 BRINE 342.0 Bbl OTHER STECKMAN RIDGE 37-009-20082
2010-0 PRODUCED FLUID 95.0 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026034 JOHNSTOWN SEWAGE TREATMENT PLANT JOHNSTOWN PA
2011-0 PRODUCED FLUID 95.0 Bbl INJECTION DISPOSAL WELL 37-111-20006 MORRIS H CRITCHFIELD F76 DISP WELL PAS2D912BSOM FRIEDENS PA
2012-0 PRODUCED FLUID 49.0 Bbl INJECTION DISPOSAL WELL 34-155-23584 KOONTZ #1 DISPOSAL WELL WARREN OH
2012-0 PRODUCED FLUID 34.98 Bbl INJECTION DISPOSAL WELL 37-111-20006 MORRIS H CRITCHFIELD F76 DISP WELL PAS2D912BSOM FRIEDENS PA
2013-0 PRODUCED FLUID 39.15 Bbl INJECTION DISPOSAL WELL PAS2D912BSOM MORRIS H CRITCHFIELD F76 DISP WELL (111-20006) FRIEDENS PA

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
783334 1986-08-29 Violation(s) Noted 87230
783335 1986-08-29 Violation(s) Noted 87231
683487 1991-04-15 No Violations Noted RADIOACTIVE SMPLG; E&S, TNK OK
684212 1992-05-26 No Violations Noted E&S OK; TANK
1802941 2009-06-04 Violation(s) Noted Based on file records, well was completed on 3/12/60 to a depth of 8,560 ft. from grade and maintains an active permit status. During inspection, proper well tag was present at well head. Well assembly consisted of 24", 13", to 2" poduction line with 3 shut off valves with moderate corrosion. Dual data logger showed 135/55 readings. Site contained 100 bbl brine tank. No brine tank lid was located on tank. As indicated by pictures, hole located on brine intake line causing brine to discharge to side of tank and on the ground. Tank was filled to 1/2 capacity. No signs of E&S issues at the site. Heater, separator and brine float connected to the production equipment. 564249
1802941 2009-06-04 Violation(s) Noted Based on file records, well was completed on 3/12/60 to a depth of 8,560 ft. from grade and maintains an active permit status. During inspection, proper well tag was present at well head. Well assembly consisted of 24", 13", to 2" poduction line with 3 shut off valves with moderate corrosion. Dual data logger showed 135/55 readings. Site contained 100 bbl brine tank. No brine tank lid was located on tank. As indicated by pictures, hole located on brine intake line causing brine to discharge to side of tank and on the ground. Tank was filled to 1/2 capacity. No signs of E&S issues at the site. Heater, separator and brine float connected to the production equipment. 564250
1809386 2009-07-01 No Violations Noted New inlet brine tank line replaced. Well head assembly was painted and new lid for the brine tank was added. No E&S or IW issues at the site. System operating with dual pen data logger reading 450 psi/250 psi with 20 bbl of brine in tank

References