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Difference between revisions of "37-111-20061"

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[[Category:Wells]]

Revision as of 09:18, 29 June 2014

Well Details

Well ID: 37-111-20061
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Operator Name: ASHTOLA PROD CO
First Permit Date: 1977-06-24
Last Permit Date: 1977-06-24
Spud Date: 1977-09-11
Unconventional: No
Horizontal: No
Violations: 2
Latitude: 39.985883
Longitude: -79.108586

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2008-0 0.0 0.0 0.0 0.0 0.0 0.0
2007-0 0.0 0.0 0.0 0.0 0.0 0.0
2004-0 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1808489 2009-06-24 Violation(s) Noted As on records, well was completed on 10/13/77 to a depth of 9,201 ft from grade. Well tag present. Well appears to be abandoned with no production. Well head assembly consists of 36¿, 13¿, 4¿ flange to 2¿ production line with 4 gate valves. Production equipment consisted of 100 bbl brine tank, separator, heater, and data logger. Brine tank was heavily corroded. Data logger was not recording any flows. Separator equipment was also heavily corroded. No brine water in tank. No E&S issues at the site. 565900
1808489 2009-06-24 Violation(s) Noted As on records, well was completed on 10/13/77 to a depth of 9,201 ft from grade. Well tag present. Well appears to be abandoned with no production. Well head assembly consists of 36¿, 13¿, 4¿ flange to 2¿ production line with 4 gate valves. Production equipment consisted of 100 bbl brine tank, separator, heater, and data logger. Brine tank was heavily corroded. Data logger was not recording any flows. Separator equipment was also heavily corroded. No brine water in tank. No E&S issues at the site. 565901

References