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Difference between revisions of "34-111-21981"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-111-21981
 
| Well ID: 34-111-21981
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.82789817, -81.20218781 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.82, -81.2 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Monroe County, Ohio|Monroe]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Monroe_County,_Ohio|Monroe]]
 +
|-
 +
| Municipality: [[Malaga_Township,_Monroe_County,_Ohio|Malaga Township]]
 
|-
 
|-
 
| Operator Name: [[MCCORT BRIAN L]]
 
| Operator Name: [[MCCORT BRIAN L]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: KAHRIG RODNEY
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1980-11-17
 
|-
 
|-
 
| Spud Date: 1980-11-26
 
| Spud Date: 1980-11-26
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1980-12-02
 +
|-
 +
| Well Total Depth: 2479.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 39.820000
 +
|-
 +
| Longitude: -81.200000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| CO
 +
| 1980-11-17
 +
| 30  BANDS CO INC  GeoDate  11/17/80
 +
|-
 +
| Original Spud
 +
| 1980-11-26
 +
| R.I. 10-2-80, X=2364535.86, Y=668364.13
 +
|-
 +
| Completed
 +
| 1980-12-02
 +
| R.I. 10-2-80, X=2364535.86, Y=668364.13
 +
|-
 +
| Reached Total Depth
 +
| 1980-12-02
 +
| R.I. 10-2-80, X=2364535.86, Y=668364.13
 
|-
 
|-
| Violations: 0
+
| CO
 +
| 1993-08-06
 +
| 4597  BYERS DARROL C  GeoDate  11/17/80
 
|-
 
|-
| Latitude: 39.82789817
+
| Change of Owner
 +
| 2001-08-06
 +
| Operator changed from 4597, BYERS DARROL C to 7030, MCCORT BRIAN L
 
|-
 
|-
| Longitude: -81.20218781
+
| Record Last Modified
 +
| 2013-10-03
 +
| R.I. 10-2-80, X=2364535.86, Y=668364.13
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | CONDENSATE PRODUCTION DAYS
+
|-
!scope="col" | OIL QUANTITY
+
| 2006-09-11
!scope="col" | OIL PRODUCTION DAYS
+
| style="text-align: right;" | 2126
 +
| style="text-align: right;" | 2426
 +
| style="text-align: right;" | 32
 
|-
 
|-
| 1988-0
 
| style="text-align:right;" | 2335.0
 
 
|  
 
|  
 +
| style="text-align: right;" | 2126
 +
| style="text-align: right;" | 2426
 +
| style="text-align: right;" | 32
 +
|-
 
|  
 
|  
|  
+
| style="text-align: right;" | 2126
| style="text-align:right;" | 150.0
+
| style="text-align: right;" | 2426
|  
+
| style="text-align: right;" | 32
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
 +
|}-->
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1990-0
 
| style="text-align:right;" | 2788.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 1800 Bbl
 +
| style="text-align: right;" | 30000
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 85.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1988
 +
| [[BANDS COMPANY INC]]
 +
| style="text-align: right;" | 2335.00
 +
| style="text-align: right;" | 150.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1990
 +
| [[BANDS COMPANY INC]]
 +
| style="text-align: right;" | 2788.00
 +
| style="text-align: right;" | 85.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1991
 +
| [[BANDS COMPANY INC]]
 +
| style="text-align: right;" | 2290.00
 +
| style="text-align: right;" | 70.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1992
 +
| [[BANDS COMPANY INC]]
 +
| style="text-align: right;" | 1384.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[BANDS COMPANY INC]]
 +
| style="text-align: right;" | 1260.00
 +
| style="text-align: right;" | 73.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1994
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 2656.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1995
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 1663.00
 +
| style="text-align: right;" | 81.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1996
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 1473.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1997
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 116.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1998
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 1029.00
 +
| style="text-align: right;" | 83.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 997.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 981.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[BYERS DARROL C]]
 +
| style="text-align: right;" | 374.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 120
 +
|-
 +
| 2002
 +
| [[MCCORT BRIAN L]]
 +
| style="text-align: right;" | 969.00
 +
| style="text-align: right;" | 72.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1991-0
+
| 2003
| style="text-align:right;" | 2290.0
+
| [[MCCORT BRIAN L]]
|  
+
| style="text-align: right;" | 607.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 70.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[MCCORT BRIAN L]]
 +
| style="text-align: right;" | 87.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1992-0
+
| 2005
| style="text-align:right;" | 1384.0
+
| [[MCCORT BRIAN L]]
|
+
| style="text-align: right;" | 42.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 2006
 +
| [[MCCORT BRIAN L]]
 +
| style="text-align: right;" | 126.00
 +
| style="text-align: right;" | 66.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1993-0
+
| 2008
| style="text-align:right;" | 1260.0
+
| [[MCCORT BRIAN L]]
|  
+
| style="text-align: right;" | 33.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 14
| style="text-align:right;" | 73.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[MCCORT BRIAN L]]
 +
| style="text-align: right;" | 9.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 30
 
|-
 
|-
| 1994-0
+
| 2015
| style="text-align:right;" | 2656.0
+
| [[MCCORT BRIAN L]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[MCCORT BRIAN L]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1995-0
+
| 2017
| style="text-align:right;" | 1663.0
+
| [[MCCORT BRIAN L]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 81.0
 
|
 
 
|-
 
|-
 +
| 2018
 +
| [[MCCORT BRIAN L]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1996-0
+
|}
| style="text-align:right;" | 1473.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2020-11-16
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1988
 +
| [[BANDS COMPANY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1997-0
+
| 1990
| style="text-align:right;" | 116.0
+
| [[BANDS COMPANY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[BANDS COMPANY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 1992
| style="text-align:right;" | 1029.0
+
| [[BANDS COMPANY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 83.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[BANDS COMPANY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 1994
| style="text-align:right;" | 997.0
+
| [[BYERS DARROL C]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1995
 +
| [[BYERS DARROL C]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 1996
| style="text-align:right;" | 981.0
+
| [[BYERS DARROL C]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[BYERS DARROL C]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 1998
| style="text-align:right;" | 374.0
+
| [[BYERS DARROL C]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[BYERS DARROL C]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 2000
| style="text-align:right;" | 969.0
+
| [[BYERS DARROL C]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 72.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[BYERS DARROL C]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 120
 
|-
 
|-
| 2003-0
+
| 2002
| style="text-align:right;" | 607.0
+
| [[MCCORT BRIAN L]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[MCCORT BRIAN L]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2004-0
+
| 2004
| style="text-align:right;" | 87.0
+
| [[MCCORT BRIAN L]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[MCCORT BRIAN L]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 2006
| style="text-align:right;" | 42.0
+
| [[MCCORT BRIAN L]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[MCCORT BRIAN L]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 14
 
|-
 
|-
| 2006-0
+
| 2009
| style="text-align:right;" | 126.0
+
| [[MCCORT BRIAN L]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 30
| style="text-align:right;" | 66.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[MCCORT BRIAN L]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2008-0
+
| 2016
| style="text-align:right;" | 33.0
+
| [[MCCORT BRIAN L]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2017
 +
| [[MCCORT BRIAN L]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2009-0
+
| 2018
| style="text-align:right;" | 9.0
+
| [[MCCORT BRIAN L]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
 
| 1341930768
 
| 1341930768
 
| 2012-07-10
 
| 2012-07-10
|  
+
| Production Wells
| Inspection of the well head found 4.5'' production casing & 1.5'' tubing and the well set up to be produced by the means of a plunger lift system with the commercial valves closed and a domestic hook up present and the valve open . A single 100 barrel tank and separator are present with proper well identification.
+
| No Violations
|  
+
| Inspection of the well head found 4.5 production casing & 1.5 tubing and the well set up to be produced by the means of a plunger lift system with the commercial valves closed and a domestic hook up present and the valve open . A single 100 barrel tank and separator are present with proper well identification.
|  
+
|-
|  
+
| 1481152570
 +
| 2016-12-07
 +
| Production Wells
 +
| No Violations
 +
|  On this day I was notified by Troy Harmon  at 16:35 who indicated the landowner Rodney Kahrig called him for assistance because the production tank was leaking. I arrived at 16;55 and witnessed an area below the production tank where oil had contacted the earths surface but saturated into the tilled soil. The 100 barrel production tank had appeared to leak from the underneath. No fluid was found standing in quantities outside the dike and no fluid appeared to be migrating on the downward slope. The contractor Troy Harmon will mobilize the next morning and begin to remediate the soil and recover and fluid in quantities along with making the correct repairs to the production tank and dike area. The nearest stream was checked as a precautionary measure and no well related fluid was observed. The landowner Rodney Kahrig was interviewed and he reported that he last checked the well and pumped it approximately 7 days ago Mr. Kahrig also stated that he purchased the well off of Brian McCourt approximately 5 years ago.  At 17:00 pm I also called the listed phone number for Brian McCourt and talked with his grandson in regards to the oil spill with no response from Mr. McCourt at the time of my report at 18:35.
 +
|-
 +
| 1481217254
 +
| 2016-12-08
 +
| Production Wells
 +
| No Violations
 +
|  Status check inspection on the remedial clean up of the production fluid release from the 100 barrel production tank. On this day I witnessed Harmons Well Service on location with an excavator remediating the soil below the production tank with lime and dry sawdust. No standing fluid was observed and a cross section ditch was cut below the site with no surface fluid product being created during the clean up. A new 100 barrel production tank will be set and a dike erected. The registered well owner Brian McCort was attempted to be contacted multiple times at 740-228-2132 with the phone going straight to voicemail. Addressing the well head, the well is equipped with casing -tubing and rods and set up to be produced by the means of a pumping unit. The casing valve is open and is supplying domestic gas to the landowner Rodney Kahrig who indicated he is now the well owner.
 +
|-
 +
| 1481293992
 +
| 2016-12-09
 +
| Production Wells
 +
| No Violations
 +
|  Status check follow up on the recent production fluid release from the 100 barrel production tank. Upon inspection it was observed that the affected area has been remediated and a new 100 barrel production tank set with a earthen dike now constructed around the production facility.
 +
|-
 +
| 1572897552
 +
| 2019-11-4 0:00:
 +
| PW
 +
| No Violations
 +
| 0.50
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 21:42, 11 January 2021

Well Details

Well ID: 34-111-21981
Loading map...
Country: United States
State: Ohio
County: Monroe
Municipality: Malaga Township
Operator Name: MCCORT BRIAN L
Well Pad ID:
Farm/Lease Name: KAHRIG RODNEY
License Status: Producing
License Date: 1980-11-17
Spud Date: 1980-11-26
Spud Drilling Contractor:
Final Drill Date: 1980-12-02
Well Total Depth: 2479.00 ft
Configuration: Vertical
Latitude: 39.820000
Longitude: -81.200000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-11-17 30 BANDS CO INC GeoDate 11/17/80
Original Spud 1980-11-26 R.I. 10-2-80, X=2364535.86, Y=668364.13
Completed 1980-12-02 R.I. 10-2-80, X=2364535.86, Y=668364.13
Reached Total Depth 1980-12-02 R.I. 10-2-80, X=2364535.86, Y=668364.13
CO 1993-08-06 4597 BYERS DARROL C GeoDate 11/17/80
Change of Owner 2001-08-06 Operator changed from 4597, BYERS DARROL C to 7030, MCCORT BRIAN L
Record Last Modified 2013-10-03 R.I. 10-2-80, X=2364535.86, Y=668364.13

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2126 2426 32
2126 2426 32
2126 2426 32

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1800 Bbl 30000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1988 BANDS COMPANY INC 2335.00 150.00 365
1990 BANDS COMPANY INC 2788.00 85.00 365
1991 BANDS COMPANY INC 2290.00 70.00 365
1992 BANDS COMPANY INC 1384.00 0.00 365
1993 BANDS COMPANY INC 1260.00 73.00 365
1994 BYERS DARROL C 2656.00 0.00 365
1995 BYERS DARROL C 1663.00 81.00 365
1996 BYERS DARROL C 1473.00 0.00 365
1997 BYERS DARROL C 116.00 0.00 365
1998 BYERS DARROL C 1029.00 83.00 365
1999 BYERS DARROL C 997.00 0.00 365
2000 BYERS DARROL C 981.00 0.00 365
2001 BYERS DARROL C 374.00 0.00 120
2002 MCCORT BRIAN L 969.00 72.00 365
2003 MCCORT BRIAN L 607.00 0.00 365
2004 MCCORT BRIAN L 87.00 0.00 365
2005 MCCORT BRIAN L 42.00 0.00 365
2006 MCCORT BRIAN L 126.00 66.00 365
2008 MCCORT BRIAN L 33.00 0.00 14
2009 MCCORT BRIAN L 9.00 0.00 30
2015 MCCORT BRIAN L 0.00 0.00 0
2016 MCCORT BRIAN L 0.00 0.00 0
2017 MCCORT BRIAN L 0.00 0.00 0
2018 MCCORT BRIAN L 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1988 BANDS COMPANY INC Brine 0 365
1990 BANDS COMPANY INC Brine 0 365
1991 BANDS COMPANY INC Brine 0 365
1992 BANDS COMPANY INC Brine 0 365
1993 BANDS COMPANY INC Brine 0 365
1994 BYERS DARROL C Brine 0 365
1995 BYERS DARROL C Brine 0 365
1996 BYERS DARROL C Brine 0 365
1997 BYERS DARROL C Brine 0 365
1998 BYERS DARROL C Brine 0 365
1999 BYERS DARROL C Brine 0 365
2000 BYERS DARROL C Brine 0 365
2001 BYERS DARROL C Brine 0 120
2002 MCCORT BRIAN L Brine 0 365
2003 MCCORT BRIAN L Brine 0 365
2004 MCCORT BRIAN L Brine 0 365
2005 MCCORT BRIAN L Brine 0 365
2006 MCCORT BRIAN L Brine 0 365
2008 MCCORT BRIAN L Brine 0 14
2009 MCCORT BRIAN L Brine 0 30
2015 MCCORT BRIAN L Brine 0 0
2016 MCCORT BRIAN L Brine 0 0
2017 MCCORT BRIAN L Brine 0 0
2018 MCCORT BRIAN L Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1341930768 2012-07-10 Production Wells No Violations Inspection of the well head found 4.5 production casing & 1.5 tubing and the well set up to be produced by the means of a plunger lift system with the commercial valves closed and a domestic hook up present and the valve open . A single 100 barrel tank and separator are present with proper well identification.
1481152570 2016-12-07 Production Wells No Violations On this day I was notified by Troy Harmon at 16:35 who indicated the landowner Rodney Kahrig called him for assistance because the production tank was leaking. I arrived at 16;55 and witnessed an area below the production tank where oil had contacted the earths surface but saturated into the tilled soil. The 100 barrel production tank had appeared to leak from the underneath. No fluid was found standing in quantities outside the dike and no fluid appeared to be migrating on the downward slope. The contractor Troy Harmon will mobilize the next morning and begin to remediate the soil and recover and fluid in quantities along with making the correct repairs to the production tank and dike area. The nearest stream was checked as a precautionary measure and no well related fluid was observed. The landowner Rodney Kahrig was interviewed and he reported that he last checked the well and pumped it approximately 7 days ago Mr. Kahrig also stated that he purchased the well off of Brian McCourt approximately 5 years ago. At 17:00 pm I also called the listed phone number for Brian McCourt and talked with his grandson in regards to the oil spill with no response from Mr. McCourt at the time of my report at 18:35.
1481217254 2016-12-08 Production Wells No Violations Status check inspection on the remedial clean up of the production fluid release from the 100 barrel production tank. On this day I witnessed Harmons Well Service on location with an excavator remediating the soil below the production tank with lime and dry sawdust. No standing fluid was observed and a cross section ditch was cut below the site with no surface fluid product being created during the clean up. A new 100 barrel production tank will be set and a dike erected. The registered well owner Brian McCort was attempted to be contacted multiple times at 740-228-2132 with the phone going straight to voicemail. Addressing the well head, the well is equipped with casing -tubing and rods and set up to be produced by the means of a pumping unit. The casing valve is open and is supplying domestic gas to the landowner Rodney Kahrig who indicated he is now the well owner.
1481293992 2016-12-09 Production Wells No Violations Status check follow up on the recent production fluid release from the 100 barrel production tank. Upon inspection it was observed that the affected area has been remediated and a new 100 barrel production tank set with a earthen dike now constructed around the production facility.
1572897552 2019-11-4 0:00: PW No Violations 0.50

For data sources see[9]

References