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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-067-21036 | | Well ID: 34-067-21036 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 40.31, -80.92 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | | + | | County: [[Harrison_County,_Ohio|Harrison]] |
|- | |- | ||
− | | | + | | Municipality: [[Green_Township,_Harrison_County,_Ohio|Green Township]] |
|- | |- | ||
− | | | + | | Operator Name: [[STRATA PETROLEUM INC]] |
|- | |- | ||
− | | | + | | Well Pad ID: |
|- | |- | ||
− | | | + | | Farm/Lease Name: WILDLIFE MANAGEMENT |
+ | |- | ||
+ | | License Status: Final Restoration | ||
+ | |- | ||
+ | | License Date: 2018-01-30 | ||
|- | |- | ||
| Spud Date: 2008-06-23 | | Spud Date: 2008-06-23 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: [[G & L DRILLING]] |
+ | |- | ||
+ | | Final Drill Date: 2008-06-27 | ||
|- | |- | ||
− | | | + | | Well Total Depth: 1999.00 ft |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Latitude: 40.310000 |
|- | |- | ||
− | | | + | | Longitude: -80.920000 |
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
|- | |- | ||
− | | | + | | APP |
+ | | 2008-05-28 | ||
+ | | Proposed Formations:BEREA-DEVONIAN SHALE, Issued Date:5/28/2008, Expired Date:5/28/2009 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:EDPW | ||
+ | |- | ||
+ | | Reached Total Depth | ||
+ | | 2008-06-27 | ||
+ | | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. | ||
+ | |- | ||
+ | | Completion Report Received | ||
+ | | 2008-12-30 | ||
+ | | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. | ||
+ | |- | ||
+ | | APP | ||
+ | | 2018-01-30 | ||
+ | | Proposed Formations:BEREA, Issued Date:1/30/2018, Expired Date:1/30/2020 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class: | ||
+ | |- | ||
+ | | Plugged/Abandoned | ||
+ | | 2019-01-23 | ||
+ | | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2019-05-13 | ||
+ | | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 2020-01-30 | ||
+ | | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | == Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | | | ||
+ | | Not Treated | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | | ||
+ | | OPEN HOLE NATURAL PRODUCTION, NO PERFS; NO RESERVOIR PRESSURE REPORTED | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblStimulation Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Period |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Operator Name |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Gas Quantity (mcf) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Oil Quantity (bbl) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Production Days |
− | + | |- | |
− | + | | 2009 | |
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 4642.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 178 | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 3963.00 | ||
+ | | style="text-align: right;" | 6.00 | ||
+ | | style="text-align: right;" | 360 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 754.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 120 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2013 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Waste Data == | == Waste Data == | ||
− | {| class="wikitable sortable" | + | {| class="wikitable sortable" |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Period |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Operator Name |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Waste Type |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Quantity (bbl) |
− | + | !scope="col" style="text-align: center"| Production Days | |
− | + | |- | |
− | + | | 2009 | |
− | + | | [[STRATA PETROLEUM INC]] | |
− | + | | Brine | |
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 178 | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 360 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 120 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2013 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[STRATA PETROLEUM INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | ||
− | |||
|- | |- | ||
| -101583447 | | -101583447 | ||
− | | 2008- | + | | 2008-8-5 0:00:0 |
− | | | + | | CT |
− | | | + | | No Violations |
− | | | + | | 1.00 |
− | | | + | |- |
− | | | + | | -1199592965 |
+ | | 2016-11-23 0:00 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 2.00 | ||
|- | |- | ||
+ | | -1312149262 | ||
+ | | 2019-1-9 0:00:0 | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 1.00 | ||
|- | |- | ||
| -1727747950 | | -1727747950 | ||
− | | 2008- | + | | 2008-6-23 0:00: |
− | | | + | | DD |
− | | | + | | No Violations |
− | | | + | | 1.50 |
− | | | + | |- |
− | | | + | | -1839196492 |
+ | | 2019-1-10 0:00: | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 2.00 | ||
|- | |- | ||
+ | | -512782444 | ||
+ | | 2019-11-14 0:00 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 0.70 | ||
|- | |- | ||
| -540750421 | | -540750421 | ||
+ | | 2008-6-24 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 1.50 | ||
+ | |- | ||
+ | | -872456113 | ||
+ | | 2019-8-5 0:00:0 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -907710016 | ||
+ | | 2008-7-14 0:00: | ||
+ | | CT | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -963080467 | ||
+ | | 2008-6-30 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | 0101583447 | ||
+ | | 2008-08-05 | ||
+ | | Completion Testing | ||
+ | | No Violations | ||
+ | | Inspection revealed that the drilling pit has been closed . No violations at this time. | ||
+ | |- | ||
+ | | 0540750421 | ||
| 2008-06-24 | | 2008-06-24 | ||
− | | | + | | Drill / Deepen / Reopen |
+ | | No Violations | ||
| Inspection revealed that G & L Drilling filled the conductor hole full of cement and are trying to drill the cement at this time. They had a big rock that kept falling into the wellbore so they filled the hole with cement in an attempt to cement the rock in place so they could drill it out. | | Inspection revealed that G & L Drilling filled the conductor hole full of cement and are trying to drill the cement at this time. They had a big rock that kept falling into the wellbore so they filled the hole with cement in an attempt to cement the rock in place so they could drill it out. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 0558944275 | ||
+ | | 2019-01-23 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | Upon my arrival on the snow- covered location, I witnessed the rig loading the vac truck with fresh water. They were stringing out water hoses and cement hoses to set a cement plug in the well. They pumped a 200 foot (37 sks) Class A cement plug from 470 to 270 feet. They displaced cement with 4.8 barrels of fresh water. The rig crew started to pull the 4.5 inch diameter casing out of the well and it would not move. With the approval of ODNR District Supervisor, Mike Moreland, the rig crew shot the 4.5 inch diameter casing off at the depth of 203 feet. This left about 267 feet of 4.5 inch diameter casing in the well. The cement plug should range from 470 feet to 242 feet, with 4.5 inch diameter casing in it. Then there is 39 feet of 4.5 inch diameter casing on top, with no cement in it. The rig crew then pulled the remaining 203 feet of 4.5 inch casing up 3 feet and set another cement plug. They pumped a 200 foot (38 sks), Class A cement plug from 200 feet to ground level. The rig crew pulled 5 joints of 4.5 inch casing out of the well and topped off the well with remaining cement. The crew is going to rig down and move to another well to plug. They will then cut the 7 inch diameter casing off and reclaim both wells at the same time. | ||
+ | |- | ||
+ | | 0813350554 | ||
+ | | 2013-07-25 | ||
+ | | Preliminary Restoration | ||
+ | | No Violations | ||
+ | | Everything passed according to 1509.072A. | ||
|- | |- | ||
− | | | + | | 0907710016 |
| 2008-07-14 | | 2008-07-14 | ||
− | | | + | | Completion Testing |
− | | Inspection revealed that the 4 1/2 | + | | No Violations |
− | + | | Inspection revealed that the 4 1/2 casing got hung at app. 750 . The service rig ran tubing and are swabbing thru the tubing at this time. No violations at this time. | |
− | |||
− | |||
|- | |- | ||
+ | | 0963080467 | ||
+ | | 2008-06-30 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | Inspection revealed that G & L Drilling has TDed the well . Inspectiuon revealed no violations at this time. The crew advised that they didnt run 4 1/2 casing because the well was gasing and the operator didnt want to run casing while the well was gasing. The operator is going to run the production casing with a service rig. | ||
|- | |- | ||
− | | | + | | 1199592965 |
− | | | + | | 2016-11-23 |
− | | | + | | Production Wells |
− | | | + | | No Violations |
− | | | + | | On the day of my inspection I witnessed the permitted well bore is utilizing a pump jack for means of production. The well bore consists of 8.625 inch diameter surface casing, 4.5 inch diameter production casing and 1.5 inch diameter production tubing. At the time of my inspection the pumping unit did not have a prime move in place. All production valves were placed in the open position. Production equipment for the well bore consisted of a 100 barrel production tank and a 2 inch diameter meter run. The meter run showed no indications of recent use. The 100 barrel production tank was placed in an earthen dike that measured approximately 20*20 feet at an average height of 3 feet. RBDMS records indicate that the well has not produced commercially since 2012. I will perform a follow-up inspection to assure that the well is still idle before writing a compliance notice to the well owner. |
− | | | + | |- |
− | | | + | | 1219859728 |
+ | | 2017-10-31 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | On the day on my inspection I found this well equipped with a walking beam pumping unit. This inspection is a follow up to compliance notice #2105427973. Well is equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and rods. There is no motor on the pumping unit. Tubing valve is open, casing valves are shut. Production equipment includes a 100 barrel steel tank inside of containment. The tank has a bullet hole in the side of it. RBDMS indicates well was last produced in 2011. | ||
+ | |- | ||
+ | | 1312149262 | ||
+ | | 2019-01-09 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | On the day of my inspection I witnessed Unlimited was tripping 2.375 tubing from well. They pulled the rods yesterday and finished tripping tubing during my inspection. Their tally indicates they pulled 1741.55 feet of tubing. They are going to verify it is free of obstructions and trip it back in to set bottom plug tomorrow. | ||
+ | |- | ||
+ | | 1515510942 | ||
+ | | 2018-01-09 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | On the day on my inspection I found this well equipped with a walking beam pumping unit. This inspection is a follow up to compliance notice #2105427973. Well is equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and rods. There is no motor on the pumping unit. Tubing valve is open, casing valves are shut. Production equipment includes a 100 barrel steel tank inside of containment. The tank has a bullet hole in the side of it. RBDMS indicates well was last produced in 2011. I have been emailing with Mark Obrien who is supposed to be submitting plugging permits for these wells on behalf of the deceased owners wife. His last email dated 1/2/18 says I should receive them this week. | ||
+ | |- | ||
+ | | 1527015651 | ||
+ | | 2018-05-22 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | On the day on my inspection I found this well equipped with a walking beam pumping unit. This inspection is a follow up to compliance notice #2105427973. Well is equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and rods. There is no motor on the pumping unit. Tubing valve is open, casing valves are shut. Tubing pressure gauge reads 0 psi. Production equipment includes a 100 barrel steel tank inside of containment. The tank has a bullet hole in the side of it. RBDMS indicates well was last produced in 2011. Plugging report expires in January 2020. Email sent to Mark Obrien to see when he plans on having wells plugged. markhobrien@mac.com | ||
+ | |- | ||
+ | | 1547057835 | ||
+ | | 2019-01-09 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | On the day of my inspection I accompanied Jeff Adams. He is covering this plug job for me as I have another plug job ongoing. See his report for further details. | ||
+ | |- | ||
+ | | 1547061838 | ||
+ | | 2019-01-09 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | |||
+ | |- | ||
+ | | 1547733815 | ||
+ | | 2019-01-16 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | -680 to 580 feet. They displaced the cement with 9 barrels of fresh water. The rig crew pulled 5 more joints of casing out of the well. This should put at the depth of 470 feet. Shut plug job down for land owner issues. | ||
+ | |- | ||
+ | | 1557930806 | ||
+ | | 2019-05-13 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | On the day of my inspection I witnessed this well has been plugged. Mark Obrien had contacted me in regards to outstanding reclamation on this well. I spoke with Gary Lang, who is contractor responsible for the reclamation, to convey what was needed and that the weather is not conducive for reclamation this week. Currently the wellhead needs cut off and buried. Cement is near surface level. Small pit needs closed and tubing needs removed from site. Minor grading work and everything affected will need seeded. Landowner waiver for lease road will be necessary. | ||
+ | |- | ||
+ | | 1567526793 | ||
+ | | 2019-9-3 0:00:0 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | 1727747950 | ||
+ | | 2008-06-23 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | Inspection revealed that G & L drilling is reaming the conductor hole at 78 . They are having trouble running the conductor pipe . No violations at this time. | ||
|- | |- | ||
+ | | 1839196492 | ||
+ | | 2019-01-10 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | On the day of my inspection I witnessed unlimited try and pull the 4.5 inch diameter casing. Records indicate there is 970 feet of casing. They pulled 50k and were unable to pull the packer. They worked it up and down for a while. They will shoot it off tomorrow and their final plugs then. | ||
|- | |- | ||
| 2048903440 | | 2048903440 | ||
| 2008-06-25 | | 2008-06-25 | ||
− | | | + | | Drill / Deepen / Reopen |
+ | | No Violations | ||
| In spection revealed that G & L Drilling is trying to run conductor pipe . They are still having trouble running the conductor pipe past the rock that kept falling into the wellbore. No violations at this time. | | In spection revealed that G & L Drilling is trying to run conductor pipe . They are still having trouble running the conductor pipe past the rock that kept falling into the wellbore. No violations at this time. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 2105427973 | ||
+ | | 2017-03-15 | ||
+ | | Production Wells | ||
+ | | Violations Noted | ||
+ | -11-05(B), and plug the well within 180 days. The owner/operator will be notified if the plugging schedule is approved or denied. | ||
+ | |- | ||
+ | | 558944275 | ||
+ | | 2019-1-23 0:00: | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 5.90 | ||
+ | |- | ||
+ | | 730552060 | ||
+ | | 2019-8-5 0:00:0 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 1.00 | ||
|- | |- | ||
| 813350554 | | 813350554 | ||
− | | 2013- | + | | 2013-7-25 0:00: |
− | | | + | | PL |
− | | | + | | No Violations |
− | | | + | | 1.00 |
− | | | + | |- |
− | | | + | | 947522204 |
+ | | 2019-7-1 0:00:0 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | |} | ||
+ | ==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | | 2105427973 | ||
+ | | US-OH-121533 | ||
+ | | 2017-04-10 | ||
+ | | | ||
+ | | Well shall be plugged | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | ==References== | ||
+ | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-067-21036 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Green Township | |
Operator Name: STRATA PETROLEUM INC | |
Well Pad ID: | |
Farm/Lease Name: WILDLIFE MANAGEMENT | |
License Status: Final Restoration | |
License Date: 2018-01-30 | |
Spud Date: 2008-06-23 | |
Spud Drilling Contractor: G & L DRILLING | |
Final Drill Date: 2008-06-27 | |
Well Total Depth: 1999.00 ft | |
Configuration: Vertical | |
Latitude: 40.310000 | |
Longitude: -80.920000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2008-05-28 | Proposed Formations:BEREA-DEVONIAN SHALE, Issued Date:5/28/2008, Expired Date:5/28/2009 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2008-06-27 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Completion Report Received | 2008-12-30 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
APP | 2018-01-30 | Proposed Formations:BEREA, Issued Date:1/30/2018, Expired Date:1/30/2020 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2019-01-23 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Record Last Modified | 2019-05-13 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Construction Permit Expires | 2020-01-30 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 0 | OPEN HOLE NATURAL PRODUCTION, NO PERFS; NO RESERVOIR PRESSURE REPORTED |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | STRATA PETROLEUM INC | 4642.00 | 0.00 | 178 |
2010 | STRATA PETROLEUM INC | 3963.00 | 6.00 | 360 |
2011 | STRATA PETROLEUM INC | 754.00 | 0.00 | 120 |
2012 | STRATA PETROLEUM INC | 0.00 | 0.00 | 0 |
2013 | STRATA PETROLEUM INC | 0.00 | 0.00 | 0 |
2014 | STRATA PETROLEUM INC | 0.00 | 0.00 | 0 |
2015 | STRATA PETROLEUM INC | 0.00 | 0.00 | 0 |
2016 | STRATA PETROLEUM INC | 0.00 | 0.00 | 0 |
2017 | STRATA PETROLEUM INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | STRATA PETROLEUM INC | Brine | 0 | 178 |
2010 | STRATA PETROLEUM INC | Brine | 0 | 360 |
2011 | STRATA PETROLEUM INC | Brine | 0 | 120 |
2012 | STRATA PETROLEUM INC | Brine | 0 | 0 |
2013 | STRATA PETROLEUM INC | Brine | 0 | 0 |
2014 | STRATA PETROLEUM INC | Brine | 0 | 0 |
2015 | STRATA PETROLEUM INC | Brine | 0 | 0 |
2016 | STRATA PETROLEUM INC | Brine | 0 | 0 |
2017 | STRATA PETROLEUM INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-101583447 | 2008-8-5 0:00:0 | CT | No Violations | 1.00 |
-1199592965 | 2016-11-23 0:00 | PW | No Violations | 2.00 |
-1312149262 | 2019-1-9 0:00:0 | PB | No Violations | 1.00 |
-1727747950 | 2008-6-23 0:00: | DD | No Violations | 1.50 |
-1839196492 | 2019-1-10 0:00: | PB | No Violations | 2.00 |
-512782444 | 2019-11-14 0:00 | FR | No Violations | 0.70 |
-540750421 | 2008-6-24 0:00: | DD | No Violations | 1.50 |
-872456113 | 2019-8-5 0:00:0 | FR | No Violations | 1.00 |
-907710016 | 2008-7-14 0:00: | CT | No Violations | 1.00 |
-963080467 | 2008-6-30 0:00: | DD | No Violations | 1.00 |
0101583447 | 2008-08-05 | Completion Testing | No Violations | Inspection revealed that the drilling pit has been closed . No violations at this time. |
0540750421 | 2008-06-24 | Drill / Deepen / Reopen | No Violations | Inspection revealed that G & L Drilling filled the conductor hole full of cement and are trying to drill the cement at this time. They had a big rock that kept falling into the wellbore so they filled the hole with cement in an attempt to cement the rock in place so they could drill it out. |
0558944275 | 2019-01-23 | Plug / Plug Back | No Violations | Upon my arrival on the snow- covered location, I witnessed the rig loading the vac truck with fresh water. They were stringing out water hoses and cement hoses to set a cement plug in the well. They pumped a 200 foot (37 sks) Class A cement plug from 470 to 270 feet. They displaced cement with 4.8 barrels of fresh water. The rig crew started to pull the 4.5 inch diameter casing out of the well and it would not move. With the approval of ODNR District Supervisor, Mike Moreland, the rig crew shot the 4.5 inch diameter casing off at the depth of 203 feet. This left about 267 feet of 4.5 inch diameter casing in the well. The cement plug should range from 470 feet to 242 feet, with 4.5 inch diameter casing in it. Then there is 39 feet of 4.5 inch diameter casing on top, with no cement in it. The rig crew then pulled the remaining 203 feet of 4.5 inch casing up 3 feet and set another cement plug. They pumped a 200 foot (38 sks), Class A cement plug from 200 feet to ground level. The rig crew pulled 5 joints of 4.5 inch casing out of the well and topped off the well with remaining cement. The crew is going to rig down and move to another well to plug. They will then cut the 7 inch diameter casing off and reclaim both wells at the same time. |
0813350554 | 2013-07-25 | Preliminary Restoration | No Violations | Everything passed according to 1509.072A. |
0907710016 | 2008-07-14 | Completion Testing | No Violations | Inspection revealed that the 4 1/2 casing got hung at app. 750 . The service rig ran tubing and are swabbing thru the tubing at this time. No violations at this time. |
0963080467 | 2008-06-30 | Drill / Deepen / Reopen | No Violations | Inspection revealed that G & L Drilling has TDed the well . Inspectiuon revealed no violations at this time. The crew advised that they didnt run 4 1/2 casing because the well was gasing and the operator didnt want to run casing while the well was gasing. The operator is going to run the production casing with a service rig. |
1199592965 | 2016-11-23 | Production Wells | No Violations | On the day of my inspection I witnessed the permitted well bore is utilizing a pump jack for means of production. The well bore consists of 8.625 inch diameter surface casing, 4.5 inch diameter production casing and 1.5 inch diameter production tubing. At the time of my inspection the pumping unit did not have a prime move in place. All production valves were placed in the open position. Production equipment for the well bore consisted of a 100 barrel production tank and a 2 inch diameter meter run. The meter run showed no indications of recent use. The 100 barrel production tank was placed in an earthen dike that measured approximately 20*20 feet at an average height of 3 feet. RBDMS records indicate that the well has not produced commercially since 2012. I will perform a follow-up inspection to assure that the well is still idle before writing a compliance notice to the well owner. |
1219859728 | 2017-10-31 | Production Wells | No Violations | On the day on my inspection I found this well equipped with a walking beam pumping unit. This inspection is a follow up to compliance notice #2105427973. Well is equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and rods. There is no motor on the pumping unit. Tubing valve is open, casing valves are shut. Production equipment includes a 100 barrel steel tank inside of containment. The tank has a bullet hole in the side of it. RBDMS indicates well was last produced in 2011. |
1312149262 | 2019-01-09 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Unlimited was tripping 2.375 tubing from well. They pulled the rods yesterday and finished tripping tubing during my inspection. Their tally indicates they pulled 1741.55 feet of tubing. They are going to verify it is free of obstructions and trip it back in to set bottom plug tomorrow. |
1515510942 | 2018-01-09 | Production Wells | No Violations | On the day on my inspection I found this well equipped with a walking beam pumping unit. This inspection is a follow up to compliance notice #2105427973. Well is equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and rods. There is no motor on the pumping unit. Tubing valve is open, casing valves are shut. Production equipment includes a 100 barrel steel tank inside of containment. The tank has a bullet hole in the side of it. RBDMS indicates well was last produced in 2011. I have been emailing with Mark Obrien who is supposed to be submitting plugging permits for these wells on behalf of the deceased owners wife. His last email dated 1/2/18 says I should receive them this week. |
1527015651 | 2018-05-22 | Production Wells | No Violations | On the day on my inspection I found this well equipped with a walking beam pumping unit. This inspection is a follow up to compliance notice #2105427973. Well is equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and rods. There is no motor on the pumping unit. Tubing valve is open, casing valves are shut. Tubing pressure gauge reads 0 psi. Production equipment includes a 100 barrel steel tank inside of containment. The tank has a bullet hole in the side of it. RBDMS indicates well was last produced in 2011. Plugging report expires in January 2020. Email sent to Mark Obrien to see when he plans on having wells plugged. markhobrien@mac.com |
1547057835 | 2019-01-09 | Plug / Plug Back | No Violations | On the day of my inspection I accompanied Jeff Adams. He is covering this plug job for me as I have another plug job ongoing. See his report for further details. |
1547061838 | 2019-01-09 | Plug / Plug Back | No Violations | |
1547733815 | 2019-01-16 | Plug / Plug Back | No Violations
-680 to 580 feet. They displaced the cement with 9 barrels of fresh water. The rig crew pulled 5 more joints of casing out of the well. This should put at the depth of 470 feet. Shut plug job down for land owner issues. | |
1557930806 | 2019-05-13 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed this well has been plugged. Mark Obrien had contacted me in regards to outstanding reclamation on this well. I spoke with Gary Lang, who is contractor responsible for the reclamation, to convey what was needed and that the weather is not conducive for reclamation this week. Currently the wellhead needs cut off and buried. Cement is near surface level. Small pit needs closed and tubing needs removed from site. Minor grading work and everything affected will need seeded. Landowner waiver for lease road will be necessary. |
1567526793 | 2019-9-3 0:00:0 | FR | No Violations | 1.00 |
1727747950 | 2008-06-23 | Drill / Deepen / Reopen | No Violations | Inspection revealed that G & L drilling is reaming the conductor hole at 78 . They are having trouble running the conductor pipe . No violations at this time. |
1839196492 | 2019-01-10 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed unlimited try and pull the 4.5 inch diameter casing. Records indicate there is 970 feet of casing. They pulled 50k and were unable to pull the packer. They worked it up and down for a while. They will shoot it off tomorrow and their final plugs then. |
2048903440 | 2008-06-25 | Drill / Deepen / Reopen | No Violations | In spection revealed that G & L Drilling is trying to run conductor pipe . They are still having trouble running the conductor pipe past the rock that kept falling into the wellbore. No violations at this time. |
2105427973 | 2017-03-15 | Production Wells | Violations Noted
-11-05(B), and plug the well within 180 days. The owner/operator will be notified if the plugging schedule is approved or denied. | |
558944275 | 2019-1-23 0:00: | PB | No Violations | 5.90 |
730552060 | 2019-8-5 0:00:0 | FR | No Violations | 1.00 |
813350554 | 2013-7-25 0:00: | PL | No Violations | 1.00 |
947522204 | 2019-7-1 0:00:0 | FR | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
2105427973 | US-OH-121533 | 2017-04-10 | Well shall be plugged |
For data sources see[8]