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Difference between revisions of "34-067-21141"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-067-21141
 
| Well ID: 34-067-21141
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.17341456, -81.22683369 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.17, -81.22 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Harrison County, Ohio|Harrison]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[GULFPORT ENERGY CORPORATION]]
+
| County: [[Belmont_County,_Ohio|Belmont]]
 
|-
 
|-
| Well Pad ID:  
+
| Municipality: [[Flushing_Township,_Belmont_County,_Ohio|Flushing Township]]
 
|-
 
|-
| Farm/Lease Name:  
+
| Operator Name: [[GULFPORT APPALACHIA LLC]]
 
|-
 
|-
| First Permit Date:  
+
| Well Pad ID: [[US-OH-000602]]
 
|-
 
|-
| Last Permit Date:  
+
| Farm/Lease Name: CLAY
 +
|-
 +
| License Status: Producing
 +
|-
 +
| License Date: 2013-04-15
 
|-
 
|-
 
| Spud Date: 2013-03-05
 
| Spud Date: 2013-03-05
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[SIDEWINDER DRILLING INC]]
|-
 
| Configuration: Vertical
 
 
|-
 
|-
| Well Status: Producing
+
| Final Drill Date: 2013-05-08
 
|-
 
|-
| Violations: 0
+
| Well Total Depth: 13852.00 ft
 
|-
 
|-
| Latitude: 40.17341456
+
| Configuration: Horizontal
 
|-
 
|-
| Longitude: -81.22683369
+
| Latitude: 40.170000
 
|-
 
|-
 +
| Longitude: -81.220000
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | GAS QUANTITY
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comment
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 2013-12
+
| APP
| style="text-align:right;" | 171489.0
+
| 2013-02-27
|
+
| Proposed Formations:TRENTON, Issued Date:2/27/2013, Expired Date:2/27/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
|
 
|
 
| style="text-align:right;" | 18299.0
 
|
 
 
|-
 
|-
 +
| Correction to Well
 +
| 2013-03-22
 +
| CORRECTION TO X,Y COORDINATES.
 
|-
 
|-
| 2013-9
+
| APP
| style="text-align:right;" | 70720.0
+
| 2013-04-15
|
+
| Proposed Formations:POINT PLEASANT, Issued Date:4/15/2013, Expired Date:4/15/2015 12:00:00 PM, Drilling unit acres:629.659, Proposed Well Type:OG, Proposed Well Class:EDPW
|
 
|
 
| style="text-align:right;" | 9939.0
 
|
 
|-
 
 
|-
 
|-
| 2014-3
+
| Correction to Well
| style="text-align:right;" | 80434.0
+
| 2013-04-26
| style="text-align:right;" | 92.0
+
| CORRECTION TO CASING PROGRAM
|
 
|  
 
| style="text-align:right;" | 6069.0
 
| style="text-align:right;" | 92.0
 
 
|-
 
|-
|-
+
| Reached Total Depth
| 2014-1
+
| 2013-05-08
| style="text-align:right;" | 120695.0
 
| style="text-align:right;" | 84.0
 
 
|  
 
|  
|
 
| style="text-align:right;" | 8235.0
 
| style="text-align:right;" | 84.0
 
 
|-
 
|-
|-
+
| Completion Report Received
| 2014-2
+
| 2013-10-03
| style="text-align:right;" | 89983.0
 
| style="text-align:right;" | 78.0
 
 
|  
 
|  
|
 
| style="text-align:right;" | 7626.0
 
| style="text-align:right;" | 78.0
 
 
|-
 
|-
 +
| Correction to Well
 +
| 2013-10-11
 +
| CHANGE IN TARGET INFORMATION (FOOTAGE & X,Y COORDINATES) FROM AS DRILLED SURVEY PLAT.
 
|-
 
|-
| 2014-4
+
| Construction Permit Expires
| style="text-align:right;" | 65266.0
+
| 2015-04-15
| style="text-align:right;" | 88.0
 
 
|  
 
|  
|
 
| style="text-align:right;" | 2088.0
 
| style="text-align:right;" | 88.0
 
|-
 
 
|-
 
|-
| 2015-1
+
| Record Last Modified
| style="text-align:right;" | 45863.0
+
| 2017-10-24
| style="text-align:right;" | 78.0
 
|
 
 
|  
 
|  
| style="text-align:right;" | 2102.0
 
| style="text-align:right;" | 78.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Well and WellHistry Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== Inspection Data ==
+
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| -1168181237
+
|}-->
| 2013-10-15
+
== Fracking Activities ==
|  
+
==== Fracking Jobs ====
| The site passed preliminary restoration according to 1509.072A.
+
{| class="wikitable sortable" width="95%"
|  
+
!scope="col" style="text-align: center"| Job Number
|  
+
!scope="col" style="text-align: center"| Job Start Date
|  
+
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 
|-
 
|-
 +
| 1
 +
| 07/23/2013
 +
| 07/29/2013
 +
| style="text-align: right;" | 7879
 +
| style="text-align: right;" | 9,601,450.0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1364308472
+
|}
| 2013-03-26
+
==== Fluid Composition Data ====
|  
+
{| class="wikitable sortable" style="width: 100%"
| I am on site today to witness the running and cementing of the 13-3/8 inch casing string. Yost Drilling Rig # 7 has drilled a 17.5inch diameter hole to 1762 ft. and set 1722 ft of casing. Stingray Cementing service c/w 1390 sks of class A 15.6 lb cement. I witnessed 25 bbls of good cement returns to surface.
+
!scope="col" style="text-align: center"| Job Number
|  
+
!scope="col" style="text-align: center"| Trade Name
|  
+
!scope="col" style="text-align: center"| Supplier
|  
+
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
 +
|- valign="top"
 +
| rowspan="33"| 1
 +
| rowspan="2"| IC-250
 +
| rowspan="2"| Stingray
 +
| rowspan="2"| Corossion Inhibitor
 +
| Proprietary polycarboxylic acid mixture
 +
| NA
 +
| style="text-align: right;" | 20
 +
| style="text-align: right;" | 0.0002
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1364309314
+
| Water
| 2013-03-22
+
| 7732-18-5
|  
+
| style="text-align: right;" | 80
| On the day of my inspection I covered a surface job. 18.625 casing was ran and cemented with good cement returns. See cement ticket for details. No violations noted.
+
| style="text-align: right;" | 0.00081
|  
+
| style="text-align: right;" | 0
|
 
|  
 
 
|-
 
|-
 +
|- valign="top"
 +
| rowspan="1"| 40/70 White
 +
| rowspan="1"| Minerva/Cadiz
 +
| rowspan="1"| Proppant
 +
| Sand
 +
| 14808-60-7
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 13.5112
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1366824737
+
|- valign="top"
| 2013-04-24
+
| rowspan="1"| Fresh water
|  
+
| rowspan="1"| Stingray
| I am on site today to plug the 12-1/4 inch diameter section of the well back. Schlumberger Cementing is plugging back today from 6977 ft in 500 ft stages. 6977 ft to 6477 ft pull up 500 ft. 2 nd plug from 5977 ft to 5477 ft then pull up again 500 ft. 3 rd plug from 4977 ft to 4477 ft pull up 500 ft. Set 4 th plug from 3700 ft to 3277 ft. Shut in for 24 hours. Then Sidewinder M- 60 will re-drill this same section and try to keep from going outside the Hardline or drill corridor.
+
| rowspan="1"| Carrier
|  
+
| Water
|  
+
| 7732-18-5
|  
+
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 85.6551
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
|- valign="top"
 +
| rowspan="2"| Entegrate NE 1100
 +
| rowspan="2"| U.S. Water
 +
| rowspan="2"| Demulsifier
 +
| Water
 +
| 7732-18-5
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.02635
 +
| style="text-align: right;" | 0
 
|-
 
|-
| -19283136
+
| Ethylene/Propylene Oxide Polymer
| 2013-03-07
+
| NA
|  
+
| style="text-align: right;" | 40
| Stringray Cementing cemented 115' of 26 casing with 250Sacks of Class A cement.  See the Casing Ticket for more information.
+
| style="text-align: right;" | 0.01757
|  
+
| style="text-align: right;" | 0
|
 
|  
 
 
|-
 
|-
 +
|- valign="top"
 +
| rowspan="1"| 30/50 White
 +
| rowspan="1"| Minerva/Cadiz
 +
| rowspan="1"| Proppant
 +
| Sand
 +
| 14808-60-7
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 985016475
+
|- valign="top"
| 2013-03-29
+
| rowspan="2"| Clean Gel
|
+
| rowspan="2"| Stingray
| On the day of my inspection I picked up a cement ticket from previously witnessed 18.625 casing job. Mark Moreland was present to witness 13.375 cement job. No violations noted.
+
| rowspan="2"| Guar Gel
|
+
| Solvent naphtha, (petroleum)
|
+
| 64742-96-7
|
+
| style="text-align: right;" | 65
|-
+
| style="text-align: right;" | 0.0313095
|}
+
| style="text-align: right;" | 0
For data sources see<ref>{{cite web
 
| title = Ohio Department of Natural Resources RBDMS
 
| publisher = [http://oilandgas.ohiodnr.gov/]
 
| date = 2015-06-19
 
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 
| accessdate = 2015-06-20 }}</ref>
 
[[Category:Has Chemical Data]]
 
==Chemical Data==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | HF Fluid Concentration
 
!scope="col" | Ingredient
 
!scope="col" | Additive Concentration
 
!scope="col" | Trade Name
 
!scope="col" | Purpose
 
!scope="col" | CAS number
 
!scope="col" | Supplier
 
|-
 
| 65.0
 
| Solvent naphtha
 
| 64742.0
 
| Clean Gel
 
| Guar Gel
 
|  (petroleum)
 
| Stingray
 
 
|-
 
|-
|-
 
| 0.0168605
 
 
| heavy aliphatic
 
| heavy aliphatic
| 35.0
 
| Clean Gel
 
| Guar Gel
 
 
| NA
 
| NA
| Stingray
+
| style="text-align: right;" | 35
 +
| style="text-align: right;" | 0.0168605
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
|- valign="top"
 +
| rowspan="2"| X-linker
 +
| rowspan="2"| Stingray
 +
| rowspan="2"| Guar Gel
 +
| Ethylene Glycol
 +
| NA
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.00022
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00081
 
 
| Water
 
| Water
| 80.0
 
| IC-250
 
| Corossion Inhibitor
 
 
| 7732-18-5
 
| 7732-18-5
| Stingray
+
| style="text-align: right;" | 70
 +
| style="text-align: right;" | 0.00052
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="6"| Entegrate FR 7170
 +
| rowspan="6"| U.S. Water
 +
| rowspan="6"| Friction Reducer
 +
| Petroleum distillate hydrotreated light
 +
| 64742-47-8
 +
| style="text-align: right;" | 28
 +
| style="text-align: right;" | 0.02192
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| C12-C14 Alcohol ethoxylated
 +
| 68439-50-9
 +
| style="text-align: right;" | 3.1
 +
| style="text-align: right;" | 0.00243
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.0002
+
| Alcohols (C10-16), ethoxylated
| Proprietary polycarboxylic acid mixture
+
| 68002-97-1
| 20.0
+
| style="text-align: right;" | 3.1
| IC-250
+
| style="text-align: right;" | 0.00243
| Corossion Inhibitor
+
| style="text-align: right;" | 0
| NA
 
| Stingray
 
 
|-
 
|-
 +
| Ammonium chloride
 +
| 12125-02-9
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 0.01174
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.0225836
 
 
| Water
 
| Water
| 95.0
 
| BioClear 5000
 
| Biocide
 
 
| 7732-18-5
 
| 7732-18-5
| Weatherford
+
| style="text-align: right;" | 48
 +
| style="text-align: right;" | 0.03757
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| Alcohols (C12-16), ethoxylated
 +
| 68551-12-2
 +
| style="text-align: right;" | 3.1
 +
| style="text-align: right;" | 0.00243
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 5.0
+
|- valign="top"
| 2
+
| rowspan="2"| BioClear 5000
| 10222.0
+
| rowspan="2"| Weatherford
| BioClear 5000
+
| rowspan="2"| Biocide
| Biocide
+
| Water
| 2-dibromo-3-nitril o
+
| 7732-18-5
| Weatherford
+
| style="text-align: right;" | 95
 +
| style="text-align: right;" | 0.0225836
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| 2,2-dibromo-3-nitril oprop ionam ide
 +
| 10222-01-2
 +
| style="text-align: right;" | 5
 +
| style="text-align: right;" | 0.00119019
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.523055
+
|- valign="top"
 +
| rowspan="1"| 100 mesh
 +
| rowspan="1"| Minerva/Cadiz
 +
| rowspan="1"| Proppant
 
| Sand
 
| Sand
| 100.0
 
| 100 mesh
 
| Proppant
 
 
| 14808-60-7
 
| 14808-60-7
| Minerva/Cadiz
+
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.523055
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
|- valign="top"
 +
| rowspan="5"| Entecide QG40
 +
| rowspan="5"| U.S. Water
 +
| rowspan="5"| Breaker
 +
| Water
 +
| 7732-18-5
 +
| style="text-align: right;" | 56.4
 +
| style="text-align: right;" | 0.00207
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00052
+
| GLUTARALDEHYDE
 +
| 111-30-8
 +
| style="text-align: right;" | 27
 +
| style="text-align: right;" | 0.00099
 +
| style="text-align: right;" | 0
 +
|-
 +
| n-ALKYL DIMETHYL BENZYL AMMONIUM CHLORIDE
 +
| 68424-85-1
 +
| style="text-align: right;" | 5.5
 +
| style="text-align: right;" | 0.0002
 +
| style="text-align: right;" | 0
 +
|-
 +
| ETHANOL
 +
| 64-17-5
 +
| style="text-align: right;" | 2.8
 +
| style="text-align: right;" | 0.0001
 +
| style="text-align: right;" | 0
 +
|-
 +
| DIDECYL DIMETHYL AMMONIUM CHLORIDE
 +
| 7173-51-5
 +
| style="text-align: right;" | 8.3
 +
| style="text-align: right;" | 0.0003
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| Citric Acid 50%
 +
| rowspan="2"| Pace International
 +
| rowspan="2"| Acid
 
| Water
 
| Water
| 70.0
 
| X-linker
 
| Guar Gel
 
 
| 7732-18-5
 
| 7732-18-5
| Stingray
+
| style="text-align: right;" | 50
 +
| style="text-align: right;" | 0.125964
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| citric acid
 +
| 77-92-9
 +
| style="text-align: right;" | 50
 +
| style="text-align: right;" | 0.125964
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00022
+
|- valign="top"
| Ethylene Glycol
+
| rowspan="5"| Entegrate SC8060 WB
| 30.0
+
| rowspan="5"| U.S. Water
| X-linker
+
| rowspan="5"| Scale Inhibitor
| Guar Gel
+
| Methyl Alcohol
| NA
+
| 67-56-1
| Stingray
+
| style="text-align: right;" | 20
 +
| style="text-align: right;" | 0.00179
 +
| style="text-align: right;" | 0
 +
|-
 +
| Phosphoric Acid
 +
| 7664-38-2
 +
| style="text-align: right;" | 1
 +
| style="text-align: right;" | 0.00009000
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| Aminotrimethylene Phosphonic Acid
 +
| 6419-19-8
 +
| style="text-align: right;" | 10
 +
| style="text-align: right;" | 0.00089
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 85.6551
 
 
| Water
 
| Water
| 100.0
 
| Fresh water
 
| Carrier
 
 
| 7732-18-5
 
| 7732-18-5
| Stingray
+
| style="text-align: right;" | 59
 +
| style="text-align: right;" | 0.00527
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2-propenoic acid, sodium salt, polymer
 +
| 37350-42-8
 +
| style="text-align: right;" | 10
 +
| style="text-align: right;" | 0.00089
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Per Break
 +
| rowspan="1"| Stingray
 +
| rowspan="1"| Breaker
 +
| Ammonium Persulfate
 +
| 7727-54-0
 +
| style="text-align: right;" | 99
 +
| style="text-align: right;" | 0.00364
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = FracFocus Fracking Chemicals Database
 +
| date = 2019-04-02
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-06-19 }}</ref>
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
 +
| 2013-07-25
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 608958 Gal
 +
| style="text-align: right;" | 438889
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 4, 60 shots
 
|-
 
|-
| 0.0
+
| 2013-07-28
| Sand
+
| H2O
| 100.0
+
| style="text-align: right;" | 15
| 30/50 White
+
| style="text-align: right;" | 562590 Gal
| Proppant
+
| style="text-align: right;" | 1030575
| 14808-60-7
+
| [[STINGRAY PRESSURE PUMPING LLC]]
| Minerva/Cadiz
+
| stage 11, 60 shots
 +
|-
 +
| 2013-07-25
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 661416 Gal
 +
| style="text-align: right;" | 830897
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 3, 60 shots
 +
|-
 +
| 2013-07-27
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 429828 Gal
 +
| style="text-align: right;" | 799500
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 8, 60 shots
 +
|-
 +
| 2013-07-25
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 827694 Gal
 +
| style="text-align: right;" | 710000
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 5, 60 shots
 +
|-
 +
| 2013-07-26
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 609504 Gal
 +
| style="text-align: right;" | 1020000
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 7, 60 shots
 
|-
 
|-
 +
| 2013-07-24
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 829836 Gal
 +
| style="text-align: right;" | 1121000
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 1, 60 shots
 
|-
 
|-
| 3.1
+
| 2013-07-30
| Alcohols (C10-16)
+
| H2O
| 68002.0
+
| style="text-align: right;" | 15
| Entegrate FR 7170
+
| style="text-align: right;" | 446754 Gal
| Friction Reducer
+
| style="text-align: right;" | 423528
| ethoxylated
+
| [[STINGRAY PRESSURE PUMPING LLC]]
| U.S. Water
+
| stage 16, 60 shots
 
|-
 
|-
 +
| 2013-07-24
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 736218 Gal
 +
| style="text-align: right;" | 769725
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 2, 60 shots
 
|-
 
|-
| 0.01174
+
| 2013-07-30
| Ammonium chloride
+
| H2O
| 15.0
+
| style="text-align: right;" | 15
| Entegrate FR 7170
+
| style="text-align: right;" | 510216 Gal
| Friction Reducer
+
| style="text-align: right;" | 652823
| 12125-02-9
+
| [[STINGRAY PRESSURE PUMPING LLC]]
| U.S. Water
+
| stage 15, 60 shots
 
|-
 
|-
 +
| 2013-07-29
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 360192 Gal
 +
| style="text-align: right;" | 528866
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 14, 60 shots
 
|-
 
|-
| 0.02192
+
| 2013-07-27
| Petroleum distillate hydrotreated light
+
| H2O
| 28.0
+
| style="text-align: right;" | 15
| Entegrate FR 7170
+
| style="text-align: right;" | 593922 Gal
| Friction Reducer
+
| style="text-align: right;" | 990700
| 64742-47-8
+
| [[STINGRAY PRESSURE PUMPING LLC]]
| U.S. Water
+
| stage 9, 60 shots
 
|-
 
|-
 +
| 2013-07-26
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 824586 Gal
 +
| style="text-align: right;" | 851000
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 6, 60 shots
 
|-
 
|-
| 3.1
+
| 2013-07-28
| Alcohols (C12-16)
+
| H2O
| 68551.0
+
| style="text-align: right;" | 15
| Entegrate FR 7170
+
| style="text-align: right;" | 481068 Gal
| Friction Reducer
+
| style="text-align: right;" | 874071
| ethoxylated
+
| [[STINGRAY PRESSURE PUMPING LLC]]
| U.S. Water
+
| stage 12, 60 shots
 
|-
 
|-
 +
| 2013-07-27
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 559146 Gal
 +
| style="text-align: right;" | 1039117
 +
| [[STINGRAY PRESSURE PUMPING LLC]]
 +
| stage 10, 60 shots
 
|-
 
|-
| 0.03757
+
| 2013-07-29
| Water
+
| H2O
| 48.0
+
| style="text-align: right;" | 15
| Entegrate FR 7170
+
| style="text-align: right;" | 491274 Gal
| Friction Reducer
+
| style="text-align: right;" | 1022996
| 7732-18-5
+
| [[STINGRAY PRESSURE PUMPING LLC]]
| U.S. Water
+
| stage 13, 60 shots
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 0.00089
+
| 2013
| Aminotrimethylene Phosphonic Acid
+
| [[GULFPORT ENERGY CORPORATION]]
| 10.0
+
| style="text-align: right;" | 242209
| Entegrate SC8060 WB
+
| style="text-align: right;" | 28238
| Scale Inhibitor
+
| style="text-align: right;" | 122
| 6419-19-8
 
| U.S. Water
 
 
|-
 
|-
 +
| 2014
 +
| [[GULFPORT ENERGY CORPORATION]]
 +
| style="text-align: right;" | 356378
 +
| style="text-align: right;" | 24018
 +
| style="text-align: right;" | 342
 
|-
 
|-
| 9e-05
+
| 2015
| Phosphoric Acid
+
| [[GULFPORT ENERGY CORPORATION]]
| 1.0
+
| style="text-align: right;" | 176660
| Entegrate SC8060 WB
+
| style="text-align: right;" | 9263
| Scale Inhibitor
+
| style="text-align: right;" | 350
| 7664-38-2
 
| U.S. Water
 
 
|-
 
|-
 +
| 2016
 +
| [[GULFPORT ENERGY CORPORATION]]
 +
| style="text-align: right;" | 133434
 +
| style="text-align: right;" | 5053
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 0.00179
+
| 2017
| Methyl Alcohol
+
| [[GULFPORT ENERGY CORPORATION]]
| 20.0
+
| style="text-align: right;" | 116753
| Entegrate SC8060 WB
+
| style="text-align: right;" | 3897
| Scale Inhibitor
+
| style="text-align: right;" | 358
| 67-56-1
 
| U.S. Water
 
 
|-
 
|-
 +
| 2018
 +
| [[GULFPORT ENERGY CORPORATION]]
 +
| style="text-align: right;" | 95877
 +
| style="text-align: right;" | 2526
 +
| style="text-align: right;" | 344
 
|-
 
|-
| 37350.0
+
| 2019
| 2-propenoic acid
+
| [[GULFPORT ENERGY CORPORATION]]
| 0.0
+
| style="text-align: right;" | 20142
| Entegrate SC8060 WB
+
| style="text-align: right;" | 626
| Scale Inhibitor
+
| style="text-align: right;" | 90
| sodium salt
 
| U.S. Water
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 0.00527
+
| 2013
| Water
+
| [[GULFPORT ENERGY CORPORATION]]
| 59.0
+
| Brine
| Entegrate SC8060 WB
+
| style="text-align: right;" | 24957
| Scale Inhibitor
+
| style="text-align: right;" | 122
| 7732-18-5
 
| U.S. Water
 
 
|-
 
|-
 +
| 2014
 +
| [[GULFPORT ENERGY CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 1630
 +
| style="text-align: right;" | 342
 
|-
 
|-
| 0.00207
+
| 2015
| Water
+
| [[GULFPORT ENERGY CORPORATION]]
| 56.4
+
| Brine
| Entecide QG40
+
| style="text-align: right;" | 1056
| Breaker
+
| style="text-align: right;" | 350
| 7732-18-5
 
| U.S. Water
 
 
|-
 
|-
 +
| 2016
 +
| [[GULFPORT ENERGY CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 1335
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 0.00099
+
| 2017
| GLUTARALDEHYDE
+
| [[GULFPORT ENERGY CORPORATION]]
| 27.0
+
| Brine
| Entecide QG40
+
| style="text-align: right;" | 1330
| Breaker
+
| style="text-align: right;" | 358
| 111-30-8
 
| U.S. Water
 
 
|-
 
|-
 +
| 2018
 +
| [[GULFPORT ENERGY CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 982
 +
| style="text-align: right;" | 344
 
|-
 
|-
| 0.0003
+
| 2019
| DIDECYL DIMETHYL AMMONIUM CHLORIDE
+
| [[GULFPORT ENERGY CORPORATION]]
| 8.3
+
| Brine
| Entecide QG40
+
| style="text-align: right;" | 219
| Breaker
+
| style="text-align: right;" | 90
| 7173-51-5
 
| U.S. Water
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| 0.0001
+
| -1168181237
| ETHANOL
+
| 2013-10-15 0:00
| 2.8
+
| PL
| Entecide QG40
+
| No Violations
| Breaker
+
| 0.50
| 64-17-5
 
| U.S. Water
 
 
|-
 
|-
 +
| -19283136
 +
| 2013-3-7 0:00:0
 +
| DD
 +
| No Violations
 +
|
 
|-
 
|-
| 0.0002
+
| 0019283136
| n-ALKYL DIMETHYL BENZYL AMMONIUM CHLORIDE
+
| 2013-03-07
| 5.5
+
| Drill / Deepen /  Reopen
| Entecide QG40
+
| No Violations
| Breaker
+
| Stringray Cementing cemented 115 of 26 casing with 250Sacks of Class A cement. See the Casing Ticket for more information.
| 68424-85-1
 
| U.S. Water
 
 
|-
 
|-
 +
| 0578940290
 +
| 2018-10-01
 +
| Production Wells
 +
| No Violations
 +
| On the day of my inspection I am on location to follow-up ona phone call from Brad Burwell yesterday. While pulling out the original earthen tank containment Gulfport discovered some condensate and gotten underneath the containment through the years. Brad stated that the tanks do not have any signs of leakage. 17 roll off containers (40 cubic yards each) of material were removed from site. Brad said that Hall and associates were onsite to verify that all condensate had been removed. Largest excavation was a 15  feet by 15 feet by 8 feet deep. During my insepction I witnessed this area had been backfilled and graded. Operator stated they placed clean backfill material in one foot loose lifts and compacted it. A berm was not installed in this area after backfill and I mentioned to Brad that it needs installed to match the rest of the pad berm. Brad sent over emails and photographs. I forwarded them to engineering staff Paul Logan and Jerry Smith. This well has 300 surface annular pressure and 0 on the intermediate. Prodcution equipment includes four vertical seperators, four sand traps, four GPUs, one combustor,  one 50 barrel steel brine tank in its own earthen containment, as well as six 400 barrel steel tanks that have been removed from containment.
 
|-
 
|-
| 0.01757
+
| 0985016475
| Ethylene/Propylene Oxide Polymer
+
| 2013-03-29
| 40.0
+
| Drill / Deepen /  Reopen
| Entegrate NE 1100
+
| No Violations
| Demulsifier
+
| On the day of my inspection I picked up a cement ticket from previously witnessed 18.625 casing job. Mark Moreland was present to witness 13.375 cement job. No violations noted.
| NA
 
| U.S. Water
 
 
|-
 
|-
 +
| 1168181237
 +
| 2013-10-15
 +
| Preliminary Restoration
 +
| No Violations
 +
| The site passed preliminary restoration according to 1509.072A.
 
|-
 
|-
| 0.02635
+
| 1364308472
| Water
+
| 2013-03-26
| 60.0
+
| Drill / Deepen /  Reopen
| Entegrate NE 1100
+
| No Violations
| Demulsifier
+
| I am on site today to witness the running and cementing of the 13-3/8 inch casing string. Yost Drilling Rig # 7 has drilled a 17.5inch diameter hole to 1762 ft. and set 1722 ft of casing. Stingray Cementing service c/w 1390 sks of class A 15.6 lb cement. I witnessed 25 bbls of good cement returns to surface.
| 7732-18-5
 
| U.S. Water
 
 
|-
 
|-
 +
| 1364309314
 +
| 2013-03-22
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| On the day of my inspection I covered a surface job. 18.625 casing was ran and cemented with good cement returns. See cement ticket for details. No violations noted.
 
|-
 
|-
| 0.00364
+
| 1366824737
| Ammonium Persulfate
+
| 2013-04-24
| 99.0
+
| Plug / Plug Back
| Per Break
+
| No Violations
| Breaker
+
| I am on site today to plug the 12-1/4 inch diameter section of the well back. Schlumberger Cementing is plugging back today from 6977 ft in 500 ft stages. 6977 ft to 6477 ft pull up 500 ft. 2 nd plug from 5977 ft to 5477 ft then pull up again 500 ft. 3 rd plug from 4977 ft to 4477 ft pull up 500 ft. Set 4 th plug from 3700 ft to 3277 ft. Shut in for 24 hours. Then Sidewinder M- 60 will re-drill this same section and try to keep from going outside the Hardline or drill corridor.
| 7727-54-0
 
| Stingray
 
 
|-
 
|-
 +
| 2032651842
 +
| 2016-03-15
 +
| Preliminary Restoration
 +
| No Violations
 +
| I arrived on location accompanied by inspector Mark Moreland, where I witnessed the lease road gate was locked and the lease road in adequate condition. The pad is fenced and all man doors were locked.  The permitted well is producing off of a plunger lift system. RBDMS indicated that the well is in producing order. 
 +
The production equipment on the pad consists of the following:
 +
8 400 bbl. Production tanks
 +
4 Producing wells
 +
4 Sand separators
 +
 +
4 Line heaters
 +
1 Combustor
 +
1 Low-pressure Separator
 +
1 50 bbl. drip tank 
 +
The site passed preliminary restoration in accordance with ORC 1509.072 A.
 
|-
 
|-
| 13.5112
+
| 578940290
| Sand
+
| 2018-10-1 0:00:
| 100.0
+
| PW
| 40/70 White
+
| No Violations
| Proppant
+
| 1.00
| 14808-60-7
 
| Minerva/Cadiz
 
 
|-
 
|-
 +
| 686998393
 +
| 2019-11-6 0:00:
 +
| PW
 +
| No Violations
 +
| 1.00
 
|-
 
|-
| 0.125964
+
| 985016475
| Water
+
| 2013-3-29 0:00:
| 50.0
+
| DD
| Citric Acid 50%
+
| No Violations
| Acid
+
| 0.50
| 7732-18-5
 
| Pace International
 
 
|-
 
|-
 
|}
 
|}
For data sources see<ref>{{cite web | title = FracFocus Chemical Disclosure Registry |publisher = [http://www.fracfocusdata.org/DisclosureSearch/]| date = 2015-08-10 | url = http://wellwiki.org/wiki/Well_Chemicals_Data_Sources | accessdate = 2015-08-10 }}</ref>
+
<!--==== Violations Commited ====
== References ==
+
{| class="wikitable sortable" width="95%"
{{reflist}}
+
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]
 +
[[Category:FracFocus]]

Latest revision as of 00:05, 12 January 2021

Well Details

Well ID: 34-067-21141
Loading map...
Country: United States
State: Ohio
County: Belmont
Municipality: Flushing Township
Operator Name: GULFPORT APPALACHIA LLC
Well Pad ID: US-OH-000602
Farm/Lease Name: CLAY
License Status: Producing
License Date: 2013-04-15
Spud Date: 2013-03-05
Spud Drilling Contractor: SIDEWINDER DRILLING INC
Final Drill Date: 2013-05-08
Well Total Depth: 13852.00 ft
Configuration: Horizontal
Latitude: 40.170000
Longitude: -81.220000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-02-27 Proposed Formations:TRENTON, Issued Date:2/27/2013, Expired Date:2/27/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
Correction to Well 2013-03-22 CORRECTION TO X,Y COORDINATES.
APP 2013-04-15 Proposed Formations:POINT PLEASANT, Issued Date:4/15/2013, Expired Date:4/15/2015 12:00:00 PM, Drilling unit acres:629.659, Proposed Well Type:OG, Proposed Well Class:EDPW
Correction to Well 2013-04-26 CORRECTION TO CASING PROGRAM
Reached Total Depth 2013-05-08
Completion Report Received 2013-10-03
Correction to Well 2013-10-11 CHANGE IN TARGET INFORMATION (FOOTAGE & X,Y COORDINATES) FROM AS DRILLED SURVEY PLAT.
Construction Permit Expires 2015-04-15
Record Last Modified 2017-10-24

For data sources see[2]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 07/23/2013 07/29/2013 7879 9,601,450.0 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 IC-250 Stingray Corossion Inhibitor Proprietary polycarboxylic acid mixture NA 20 0.0002 0
Water 7732-18-5 80 0.00081 0
40/70 White Minerva/Cadiz Proppant Sand 14808-60-7 100 13.5112 0
Fresh water Stingray Carrier Water 7732-18-5 100 85.6551 0
Entegrate NE 1100 U.S. Water Demulsifier Water 7732-18-5 60 0.02635 0
Ethylene/Propylene Oxide Polymer NA 40 0.01757 0
30/50 White Minerva/Cadiz Proppant Sand 14808-60-7 100 0 0
Clean Gel Stingray Guar Gel Solvent naphtha, (petroleum) 64742-96-7 65 0.0313095 0
heavy aliphatic NA 35 0.0168605 0
X-linker Stingray Guar Gel Ethylene Glycol NA 30 0.00022 0
Water 7732-18-5 70 0.00052 0
Entegrate FR 7170 U.S. Water Friction Reducer Petroleum distillate hydrotreated light 64742-47-8 28 0.02192 0
C12-C14 Alcohol ethoxylated 68439-50-9 3.1 0.00243 0
Alcohols (C10-16), ethoxylated 68002-97-1 3.1 0.00243 0
Ammonium chloride 12125-02-9 15 0.01174 0
Water 7732-18-5 48 0.03757 0
Alcohols (C12-16), ethoxylated 68551-12-2 3.1 0.00243 0
BioClear 5000 Weatherford Biocide Water 7732-18-5 95 0.0225836 0
2,2-dibromo-3-nitril oprop ionam ide 10222-01-2 5 0.00119019 0
100 mesh Minerva/Cadiz Proppant Sand 14808-60-7 100 0.523055 0
Entecide QG40 U.S. Water Breaker Water 7732-18-5 56.4 0.00207 0
GLUTARALDEHYDE 111-30-8 27 0.00099 0
n-ALKYL DIMETHYL BENZYL AMMONIUM CHLORIDE 68424-85-1 5.5 0.0002 0
ETHANOL 64-17-5 2.8 0.0001 0
DIDECYL DIMETHYL AMMONIUM CHLORIDE 7173-51-5 8.3 0.0003 0
Citric Acid 50% Pace International Acid Water 7732-18-5 50 0.125964 0
citric acid 77-92-9 50 0.125964 0
Entegrate SC8060 WB U.S. Water Scale Inhibitor Methyl Alcohol 67-56-1 20 0.00179 0
Phosphoric Acid 7664-38-2 1 0.00009000 0
Aminotrimethylene Phosphonic Acid 6419-19-8 10 0.00089 0
Water 7732-18-5 59 0.00527 0
2-propenoic acid, sodium salt, polymer 37350-42-8 10 0.00089 0
Per Break Stingray Breaker Ammonium Persulfate 7727-54-0 99 0.00364 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2013-07-25 H2O 15 608958 Gal 438889 STINGRAY PRESSURE PUMPING LLC stage 4, 60 shots
2013-07-28 H2O 15 562590 Gal 1030575 STINGRAY PRESSURE PUMPING LLC stage 11, 60 shots
2013-07-25 H2O 15 661416 Gal 830897 STINGRAY PRESSURE PUMPING LLC stage 3, 60 shots
2013-07-27 H2O 15 429828 Gal 799500 STINGRAY PRESSURE PUMPING LLC stage 8, 60 shots
2013-07-25 H2O 15 827694 Gal 710000 STINGRAY PRESSURE PUMPING LLC stage 5, 60 shots
2013-07-26 H2O 15 609504 Gal 1020000 STINGRAY PRESSURE PUMPING LLC stage 7, 60 shots
2013-07-24 H2O 15 829836 Gal 1121000 STINGRAY PRESSURE PUMPING LLC stage 1, 60 shots
2013-07-30 H2O 15 446754 Gal 423528 STINGRAY PRESSURE PUMPING LLC stage 16, 60 shots
2013-07-24 H2O 15 736218 Gal 769725 STINGRAY PRESSURE PUMPING LLC stage 2, 60 shots
2013-07-30 H2O 15 510216 Gal 652823 STINGRAY PRESSURE PUMPING LLC stage 15, 60 shots
2013-07-29 H2O 15 360192 Gal 528866 STINGRAY PRESSURE PUMPING LLC stage 14, 60 shots
2013-07-27 H2O 15 593922 Gal 990700 STINGRAY PRESSURE PUMPING LLC stage 9, 60 shots
2013-07-26 H2O 15 824586 Gal 851000 STINGRAY PRESSURE PUMPING LLC stage 6, 60 shots
2013-07-28 H2O 15 481068 Gal 874071 STINGRAY PRESSURE PUMPING LLC stage 12, 60 shots
2013-07-27 H2O 15 559146 Gal 1039117 STINGRAY PRESSURE PUMPING LLC stage 10, 60 shots
2013-07-29 H2O 15 491274 Gal 1022996 STINGRAY PRESSURE PUMPING LLC stage 13, 60 shots

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 GULFPORT ENERGY CORPORATION 242209 28238 122
2014 GULFPORT ENERGY CORPORATION 356378 24018 342
2015 GULFPORT ENERGY CORPORATION 176660 9263 350
2016 GULFPORT ENERGY CORPORATION 133434 5053 365
2017 GULFPORT ENERGY CORPORATION 116753 3897 358
2018 GULFPORT ENERGY CORPORATION 95877 2526 344
2019 GULFPORT ENERGY CORPORATION 20142 626 90

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 GULFPORT ENERGY CORPORATION Brine 24957 122
2014 GULFPORT ENERGY CORPORATION Brine 1630 342
2015 GULFPORT ENERGY CORPORATION Brine 1056 350
2016 GULFPORT ENERGY CORPORATION Brine 1335 365
2017 GULFPORT ENERGY CORPORATION Brine 1330 358
2018 GULFPORT ENERGY CORPORATION Brine 982 344
2019 GULFPORT ENERGY CORPORATION Brine 219 90

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1168181237 2013-10-15 0:00 PL No Violations 0.50
-19283136 2013-3-7 0:00:0 DD No Violations
0019283136 2013-03-07 Drill / Deepen / Reopen No Violations Stringray Cementing cemented 115 of 26 casing with 250Sacks of Class A cement. See the Casing Ticket for more information.
0578940290 2018-10-01 Production Wells No Violations On the day of my inspection I am on location to follow-up ona phone call from Brad Burwell yesterday. While pulling out the original earthen tank containment Gulfport discovered some condensate and gotten underneath the containment through the years. Brad stated that the tanks do not have any signs of leakage. 17 roll off containers (40 cubic yards each) of material were removed from site. Brad said that Hall and associates were onsite to verify that all condensate had been removed. Largest excavation was a 15 feet by 15 feet by 8 feet deep. During my insepction I witnessed this area had been backfilled and graded. Operator stated they placed clean backfill material in one foot loose lifts and compacted it. A berm was not installed in this area after backfill and I mentioned to Brad that it needs installed to match the rest of the pad berm. Brad sent over emails and photographs. I forwarded them to engineering staff Paul Logan and Jerry Smith. This well has 300 surface annular pressure and 0 on the intermediate. Prodcution equipment includes four vertical seperators, four sand traps, four GPUs, one combustor, one 50 barrel steel brine tank in its own earthen containment, as well as six 400 barrel steel tanks that have been removed from containment.
0985016475 2013-03-29 Drill / Deepen / Reopen No Violations On the day of my inspection I picked up a cement ticket from previously witnessed 18.625 casing job. Mark Moreland was present to witness 13.375 cement job. No violations noted.
1168181237 2013-10-15 Preliminary Restoration No Violations The site passed preliminary restoration according to 1509.072A.
1364308472 2013-03-26 Drill / Deepen / Reopen No Violations I am on site today to witness the running and cementing of the 13-3/8 inch casing string. Yost Drilling Rig # 7 has drilled a 17.5inch diameter hole to 1762 ft. and set 1722 ft of casing. Stingray Cementing service c/w 1390 sks of class A 15.6 lb cement. I witnessed 25 bbls of good cement returns to surface.
1364309314 2013-03-22 Drill / Deepen / Reopen No Violations On the day of my inspection I covered a surface job. 18.625 casing was ran and cemented with good cement returns. See cement ticket for details. No violations noted.
1366824737 2013-04-24 Plug / Plug Back No Violations I am on site today to plug the 12-1/4 inch diameter section of the well back. Schlumberger Cementing is plugging back today from 6977 ft in 500 ft stages. 6977 ft to 6477 ft pull up 500 ft. 2 nd plug from 5977 ft to 5477 ft then pull up again 500 ft. 3 rd plug from 4977 ft to 4477 ft pull up 500 ft. Set 4 th plug from 3700 ft to 3277 ft. Shut in for 24 hours. Then Sidewinder M- 60 will re-drill this same section and try to keep from going outside the Hardline or drill corridor.
2032651842 2016-03-15 Preliminary Restoration No Violations I arrived on location accompanied by inspector Mark Moreland, where I witnessed the lease road gate was locked and the lease road in adequate condition. The pad is fenced and all man doors were locked. The permitted well is producing off of a plunger lift system. RBDMS indicated that the well is in producing order.
The production equipment on the pad consists of the following:

8 400 bbl. Production tanks 4 Producing wells 4 Sand separators

4 Line heaters 1 Combustor 1 Low-pressure Separator 1 50 bbl. drip tank The site passed preliminary restoration in accordance with ORC 1509.072 A.

578940290 2018-10-1 0:00: PW No Violations 1.00
686998393 2019-11-6 0:00: PW No Violations 1.00
985016475 2013-3-29 0:00: DD No Violations 0.50

For data sources see[9]

References