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Difference between revisions of "34-089-23793"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-089-23793
 
| Well ID: 34-089-23793
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.152835469, -82.4241856488 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.15, -82.42 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| Country: United States
 
|-
 
|-
| Municipality:
+
| State: Ohio
 
|-
 
|-
| Operator Name:
+
| County: [[Licking_County,_Ohio|Licking]]
 
|-
 
|-
| Well Pad ID:
+
| Municipality: [[Newton_Township,_Licking_County,_Ohio|Newton Township]]
 
|-
 
|-
| Farm/Lease Name:
+
| Operator Name: [[STEEN OREN]]
 
|-
 
|-
| First Permit Date:
+
| Well Pad ID:  
 
|-
 
|-
| Last Permit Date:
+
| Farm/Lease Name: VAN WEY
 +
|-
 +
| License Status: Final Restoration
 +
|-
 +
| License Date: 2003-07-09
 
|-
 
|-
 
| Spud Date: 1980-06-18
 
| Spud Date: 1980-06-18
 
|-
 
|-
| Unconventional:
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1980-07-02
 
|-
 
|-
| Horizontal:
+
| Well Total Depth: 1135.00 ft
 
|-
 
|-
| Producing: No
+
| Configuration: Vertical
 
|-
 
|-
| Violations: 4
+
| Latitude: 40.150000
 
|-
 
|-
| Latitude: 40.152835469
+
| Longitude: -82.420000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Longitude: -82.4241856488
+
| Completed
 +
| 1980-07-02
 +
| DEEPEN, RL 1-31-81  FDT=CINN.
 +
|-
 +
| Reached Total Depth
 +
| 1980-07-02
 +
| DEEPEN, RL 1-31-81  FDT=CINN.
 +
|-
 +
| Original Spud
 +
| 1981-01-15
 +
| DEEPEN, RL 1-31-81  FDT=CINN.
 +
|-
 +
| CO
 +
| 1981-01-21
 +
| 634  STEEN OREN  GeoDate  1/21/81
 +
|-
 +
| APP
 +
| 2003-07-09
 +
| Proposed Formations:BEREA, Issued Date:7/9/2003, Expired Date:7/8/2004 6:00:00 AM, Drilling unit acres:1, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Plugged/Abandoned
 +
| 2003-09-03
 +
| DEEPEN, RL 1-31-81  FDT=CINN.
 +
|-
 +
| Construction Permit Expires
 +
| 2004-07-08
 +
| DEEPEN, RL 1-31-81  FDT=CINN.
 +
|-
 +
| Record Last Modified
 +
| 2013-03-14
 +
| DEEPEN, RL 1-31-81  FDT=CINN.
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
|}
+
|-
== Waste Data ==
+
|}-->
 +
<!--== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | TYPE
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | QUANTITY
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | UNITS
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | DISPOSAL METHOD
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | WASTE FACILITY PERMIT ID
+
|-
!scope="col" | WASTE FACILITY NAME
+
|}-->
!scope="col" | FACILITY CITY
+
<!--== Waste Data ==
!scope="col" | FACILITY STATE
+
{| class="wikitable sortable"
|}
+
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
 
| 1033136967
 
| 1033136967
 
| 2002-09-26
 
| 2002-09-26
|
+
| Production Wells
 +
| Violations Noted
 
| Inspection revealed well has rods and tubing but no pumping unit and no storage tanks.                                                                                                                                                                              WEATHER CONDITIONS: Cloudy with drizzle.
 
| Inspection revealed well has rods and tubing but no pumping unit and no storage tanks.                                                                                                                                                                              WEATHER CONDITIONS: Cloudy with drizzle.
|
 
| NONE
 
|
 
|-
 
 
|-
 
|-
 
| 1045848190
 
| 1045848190
 
| 2003-02-21
 
| 2003-02-21
|
+
| Production Wells
| Follow-up revealed well not in production and no plugging permit received by this inspector as of this date.  WEATHER CONDITIONS: Cloudy with 15" of snow cover and 28 degrees.
+
| Violations Noted
|
+
| Follow-up revealed well not in production and no plugging permit received by this inspector as of this date.  WEATHER CONDITIONS: Cloudy with 15 of snow cover and 28 degrees.
| NONE
 
|
 
|-
 
 
|-
 
|-
 
| 1052917851
 
| 1052917851
 
| 2003-05-14
 
| 2003-05-14
|
+
| Production Wells
| Follow-up revealed owner is still idle and still in violation of NOV issued on 09-27-03 with a compliance date of 09-27-03 to have the well put back into production and/or plugged. Inspector has not received a plugging permit as of this inspection date.  Inspectors is requesting a Chief's Order.  WEATHER CONDITIONS: Sunny  50 degrees and muddy.
+
| Violations Noted
|
+
| Follow-up revealed owner is still idle and still in violation of NOV issued on 09-27-03 with a compliance date of 09-27-03 to have the well put back into production and/or plugged. Inspector has not received a plugging permit as of this inspection date.  Inspectors is requesting a Chiefs Order.  WEATHER CONDITIONS: Sunny  50 degrees and muddy.
| NONE
 
|
 
|-
 
 
|-
 
|-
 
| 1061472937
 
| 1061472937
 
| 2003-08-21
 
| 2003-08-21
|
+
| Production Wells
 +
| Violations Noted
 
| Follow-up inspection revealed Hazy Nethers rigged up over hole but no activity at this time.  Updated Lat/Lon this date.  WEATHER CONDITIONS: Hazy 75 degrees and dry.
 
| Follow-up inspection revealed Hazy Nethers rigged up over hole but no activity at this time.  Updated Lat/Lon this date.  WEATHER CONDITIONS: Hazy 75 degrees and dry.
|
 
| NONE
 
|
 
|-
 
 
|-
 
|-
 
| 1061916434
 
| 1061916434
 
| 2003-08-26
 
| 2003-08-26
|
+
| Production Wells
| Inspection revealed rig pulling rods and tubing. Total Depth of tubing 1160'. After talking to Hass they are going to plug through the 2" tubing with cement. No date set as of this date to start plugging.  WEATHER CONDITIONS: Cloudy and 85 degrees.
+
| No Violations
|
+
| Inspection revealed rig pulling rods and tubing. Total Depth of tubing 1160. After talking to Hass they are going to plug through the 2 tubing with cement. No date set as of this date to start plugging.  WEATHER CONDITIONS: Cloudy and 85 degrees.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1064242099
 
| 1064242099
 
| 2003-09-22
 
| 2003-09-22
|
+
| Final Restoration
 +
| No Violations
 
| Location meets final restoration requirements. Well location is located in an active sand and gravel pit. No vegetation is required.  WEATHER CONDITIONS: Raining and 70 degrees.
 
| Location meets final restoration requirements. Well location is located in an active sand and gravel pit. No vegetation is required.  WEATHER CONDITIONS: Raining and 70 degrees.
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 1033136967
 +
| US-OH-100411
 +
| 2002-09-27
 +
|
 +
| Well shall be plugged
 +
|-
 +
| 1045848190
 +
| US-OH-100722
 +
| 2003-02-21
 +
|
 +
| Well shall be plugged
 +
|-
 +
| 1052917851
 +
| US-OH-100911
 +
| 2003-05-14
 +
|
 +
| Well shall be plugged
 +
|-
 +
| 1061472937
 +
| US-OH-101201
 +
| 2003-08-21
 +
|
 +
| Well shall be plugged
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 03:22, 12 January 2021

Well Details

Well ID: 34-089-23793
Loading map...
Country: United States
State: Ohio
County: Licking
Municipality: Newton Township
Operator Name: STEEN OREN
Well Pad ID:
Farm/Lease Name: VAN WEY
License Status: Final Restoration
License Date: 2003-07-09
Spud Date: 1980-06-18
Spud Drilling Contractor:
Final Drill Date: 1980-07-02
Well Total Depth: 1135.00 ft
Configuration: Vertical
Latitude: 40.150000
Longitude: -82.420000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1980-07-02 DEEPEN, RL 1-31-81 FDT=CINN.
Reached Total Depth 1980-07-02 DEEPEN, RL 1-31-81 FDT=CINN.
Original Spud 1981-01-15 DEEPEN, RL 1-31-81 FDT=CINN.
CO 1981-01-21 634 STEEN OREN GeoDate 1/21/81
APP 2003-07-09 Proposed Formations:BEREA, Issued Date:7/9/2003, Expired Date:7/8/2004 6:00:00 AM, Drilling unit acres:1, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2003-09-03 DEEPEN, RL 1-31-81 FDT=CINN.
Construction Permit Expires 2004-07-08 DEEPEN, RL 1-31-81 FDT=CINN.
Record Last Modified 2013-03-14 DEEPEN, RL 1-31-81 FDT=CINN.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1033136967 2002-09-26 Production Wells Violations Noted Inspection revealed well has rods and tubing but no pumping unit and no storage tanks. WEATHER CONDITIONS: Cloudy with drizzle.
1045848190 2003-02-21 Production Wells Violations Noted Follow-up revealed well not in production and no plugging permit received by this inspector as of this date. WEATHER CONDITIONS: Cloudy with 15 of snow cover and 28 degrees.
1052917851 2003-05-14 Production Wells Violations Noted Follow-up revealed owner is still idle and still in violation of NOV issued on 09-27-03 with a compliance date of 09-27-03 to have the well put back into production and/or plugged. Inspector has not received a plugging permit as of this inspection date. Inspectors is requesting a Chiefs Order. WEATHER CONDITIONS: Sunny 50 degrees and muddy.
1061472937 2003-08-21 Production Wells Violations Noted Follow-up inspection revealed Hazy Nethers rigged up over hole but no activity at this time. Updated Lat/Lon this date. WEATHER CONDITIONS: Hazy 75 degrees and dry.
1061916434 2003-08-26 Production Wells No Violations Inspection revealed rig pulling rods and tubing. Total Depth of tubing 1160. After talking to Hass they are going to plug through the 2 tubing with cement. No date set as of this date to start plugging. WEATHER CONDITIONS: Cloudy and 85 degrees.
1064242099 2003-09-22 Final Restoration No Violations Location meets final restoration requirements. Well location is located in an active sand and gravel pit. No vegetation is required. WEATHER CONDITIONS: Raining and 70 degrees.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1033136967 US-OH-100411 2002-09-27 Well shall be plugged
1045848190 US-OH-100722 2003-02-21 Well shall be plugged
1052917851 US-OH-100911 2003-05-14 Well shall be plugged
1061472937 US-OH-101201 2003-08-21 Well shall be plugged

For data sources see[3]

References