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Difference between revisions of "34-089-24716"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-089-24716
 
| Well ID: 34-089-24716
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.17194612, -82.24832614 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.17, -82.24 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Licking County, Ohio|Licking]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Licking_County,_Ohio|Licking]]
 +
|-
 +
| Municipality: [[Fallsbury_Township,_Licking_County,_Ohio|Fallsbury Township]]
 
|-
 
|-
 
| Operator Name: [[KING PETROLEUM 2]]
 
| Operator Name: [[KING PETROLEUM 2]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: HICKMAN RICHARD W
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1983-04-20
 
|-
 
|-
 
| Spud Date: 1983-08-12
 
| Spud Date: 1983-08-12
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[VERNON KING DRLG]]
 +
|-
 +
| Final Drill Date: 1983-09-12
 +
|-
 +
| Well Total Depth: 791.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 40.170000
 +
|-
 +
| Longitude: -82.240000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| CO
 +
| 1983-04-20
 +
| 1161  HICKMAN RICHARD W  GeoDate  4/20/83
 +
|-
 +
| Oil and Gas
 +
| 1983-04-20
 +
| Issued Date 4/20/83 Expired Date 10/17/83 Acres 0040000 Tool Type CT Proposed Formation BEREA Proposed Depth 00791 Proposed Drill Depth 00791
 +
|-
 +
| Original Spud
 +
| 1983-08-12
 +
 
|-
 
|-
| Violations: 0
+
| Completed
 +
| 1983-09-12
 +
 
|-
 
|-
| Latitude: 40.17194612
+
| Reached Total Depth
 +
| 1983-09-12
 +
 
|-
 
|-
| Longitude: -82.24832614
+
| Construction Permit Expires
 +
| 1983-10-17
 +
 +
|-
 +
| Completion Report Received
 +
| 1983-10-18
 +
 +
|-
 +
| CO
 +
| 1991-12-05
 +
| 1493  KING PETROLEUM  GeoDate  4/20/83
 +
|-
 +
| Record Last Modified
 +
| 2017-02-15
 +
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1984-0
 
| style="text-align:right;" | 562.0
 
 
|  
 
|  
 +
| GEL
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 100 Lbs
 +
| style="text-align: right;" | 0
 
|  
 
|  
|  
+
| SHOT: GELATIN
| style="text-align:right;" | 0.0
+
|-
|  
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1984
 +
| [[HICKMAN RICHARD W]]
 +
| style="text-align: right;" | 562.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[HICKMAN RICHARD W]]
 +
| style="text-align: right;" | 200.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1986
 +
| [[HICKMAN RICHARD W]]
 +
| style="text-align: right;" | 203.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1987
 +
| [[HICKMAN RICHARD W]]
 +
| style="text-align: right;" | 185.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1988
 +
| [[HICKMAN RICHARD W]]
 +
| style="text-align: right;" | 122.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1989
 +
| [[HICKMAN RICHARD W]]
 +
| style="text-align: right;" | 26.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2014
 +
| [[KING PETROLEUM 2]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2016
 +
| [[KING PETROLEUM 2]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2018
 +
| [[KING PETROLEUM 2]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1985-0
+
| 1984
| style="text-align:right;" | 200.0
+
| [[HICKMAN RICHARD W]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1985
 +
| [[HICKMAN RICHARD W]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1986-0
+
| 1986
| style="text-align:right;" | 203.0
+
| [[HICKMAN RICHARD W]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1987
 +
| [[HICKMAN RICHARD W]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1987-0
+
| 1988
| style="text-align:right;" | 185.0
+
| [[HICKMAN RICHARD W]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1989
 +
| [[HICKMAN RICHARD W]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1988-0
+
| 2014
| style="text-align:right;" | 122.0
+
| [[KING PETROLEUM 2]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[KING PETROLEUM 2]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1989-0
+
| 2018
| style="text-align:right;" | 26.0
+
| [[KING PETROLEUM 2]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| -140846604
 +
| 2019-7-16 0:00:
 +
| PW
 +
| No Violations
 +
| 0.10
 +
|-
 +
| -1457938019
 +
| 2020-8-26 0:00:
 +
| PW
 +
| No Violations
 +
| 1.00
 +
|-
 +
| -221245149
 +
| 2018-4-2 0:00:0
 +
| PW
 +
| No Violations
 +
| 0.50
 +
|-
 +
| -276750540
 +
| 2020-2-26 0:00:
 +
| PW
 +
| No Violations
 +
| 0.10
 
|-
 
|-
| PL13804
+
| 000PL13804
|
 
 
|  
 
|  
 +
| Preliminary Restoration
 +
| No Violations
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
 +
|-
 +
| 0221245149
 +
| 2018-04-02
 +
| Production Wells
 +
| Violations Noted
 +
| My inspection revealed that the well was equipped with a pumping unit but no motor. Identification was not posted at the well. The well did not show signs that it has produced recently. I did not find a tank battery associated with the well. The last year for reported commercial production was 1989. After the inspection I spoke to the landowner Mrs. Booher and she claimed that the Berea wells on the property were owned by her and her husband Mr. Delmar Booher. Mrs. Booher told me that the wells are no longer in use. I advised Mrs. Booher that they will need to register the wells with the DOGRM. I placed a phone call to Mr. Jim King and he told me that he has never owned the Berea wells on the property. The well owner/operator shall submit a written plugging schedule to Brandon Mitchell at 5880 Memory Road Zanesville, Ohio 43701-9553 within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. Time of inspection: 12:55 PM. Weather: 37 degrees F, Partly sunny
 +
|-
 +
| 0337938468
 +
| 2018-10-19
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-up on this well today. I issued a compliance notice to King Petroleum 2 on 4/3/2018 as the well was in violation of ORC 1509.12(B). My inspection this date revealed that the well has not been plugged or placed into production. I took two photos of the well. I called Jim King at 11:54 AM and discussed the well with him. Mr. King said that he does not own the well but might be willing to plug it. Time of inspection: 11:05 AM. Weather: 43 degrees F, Sunny
 +
|-
 +
| 1059354481
 +
| 2018-10-23
 +
| Production Wells
 +
| No Violations
 +
| I conducted an inspection of this well with a prospective plugging contractor. The plugging contractor said he will contact Mr. King about plugging the well.
 +
|-
 +
| 337938468
 +
| 2018-10-19 0:00
 +
| PW
 +
| No Violations
 +
| 0.20
 +
|-
 +
| PL13804
 
|  
 
|  
 +
| PL
 +
| No Violations
 
|  
 
|  
|  
+
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 0221245149
 +
| US-OH-122201
 +
| 2018-04-03
 +
| 9-9-05(A)10
 +
| Failure to legibly identify well
 +
|-
 +
| 0221245149
 +
| US-OH-122202
 +
| 2018-04-03
 +
| NONE
 +
| Well shall be plugged
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 03:29, 12 January 2021

Well Details

Well ID: 34-089-24716
Loading map...
Country: United States
State: Ohio
County: Licking
Municipality: Fallsbury Township
Operator Name: KING PETROLEUM 2
Well Pad ID:
Farm/Lease Name: HICKMAN RICHARD W
License Status: Producing
License Date: 1983-04-20
Spud Date: 1983-08-12
Spud Drilling Contractor: VERNON KING DRLG
Final Drill Date: 1983-09-12
Well Total Depth: 791.00 ft
Configuration: Vertical
Latitude: 40.170000
Longitude: -82.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1983-04-20 1161 HICKMAN RICHARD W GeoDate 4/20/83
Oil and Gas 1983-04-20 Issued Date 4/20/83 Expired Date 10/17/83 Acres 0040000 Tool Type CT Proposed Formation BEREA Proposed Depth 00791 Proposed Drill Depth 00791
Original Spud 1983-08-12
Completed 1983-09-12
Reached Total Depth 1983-09-12
Construction Permit Expires 1983-10-17
Completion Report Received 1983-10-18
CO 1991-12-05 1493 KING PETROLEUM GeoDate 4/20/83
Record Last Modified 2017-02-15

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 100 Lbs 0 SHOT: GELATIN

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 HICKMAN RICHARD W 562.00 0.00 0
1985 HICKMAN RICHARD W 200.00 0.00 0
1986 HICKMAN RICHARD W 203.00 0.00 365
1987 HICKMAN RICHARD W 185.00 0.00 365
1988 HICKMAN RICHARD W 122.00 0.00 365
1989 HICKMAN RICHARD W 26.00 0.00 365
2014 KING PETROLEUM 2 0.00 0.00 0
2016 KING PETROLEUM 2 0.00 0.00 0
2018 KING PETROLEUM 2 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 HICKMAN RICHARD W Brine 0 0
1985 HICKMAN RICHARD W Brine 0 0
1986 HICKMAN RICHARD W Brine 0 365
1987 HICKMAN RICHARD W Brine 0 365
1988 HICKMAN RICHARD W Brine 0 365
1989 HICKMAN RICHARD W Brine 0 365
2014 KING PETROLEUM 2 Brine 0 0
2016 KING PETROLEUM 2 Brine 0 0
2018 KING PETROLEUM 2 Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-140846604 2019-7-16 0:00: PW No Violations 0.10
-1457938019 2020-8-26 0:00: PW No Violations 1.00
-221245149 2018-4-2 0:00:0 PW No Violations 0.50
-276750540 2020-2-26 0:00: PW No Violations 0.10
000PL13804 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0221245149 2018-04-02 Production Wells Violations Noted My inspection revealed that the well was equipped with a pumping unit but no motor. Identification was not posted at the well. The well did not show signs that it has produced recently. I did not find a tank battery associated with the well. The last year for reported commercial production was 1989. After the inspection I spoke to the landowner Mrs. Booher and she claimed that the Berea wells on the property were owned by her and her husband Mr. Delmar Booher. Mrs. Booher told me that the wells are no longer in use. I advised Mrs. Booher that they will need to register the wells with the DOGRM. I placed a phone call to Mr. Jim King and he told me that he has never owned the Berea wells on the property. The well owner/operator shall submit a written plugging schedule to Brandon Mitchell at 5880 Memory Road Zanesville, Ohio 43701-9553 within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. Time of inspection: 12:55 PM. Weather: 37 degrees F, Partly sunny
0337938468 2018-10-19 Production Wells No Violations I conducted a compliance notice follow-up on this well today. I issued a compliance notice to King Petroleum 2 on 4/3/2018 as the well was in violation of ORC 1509.12(B). My inspection this date revealed that the well has not been plugged or placed into production. I took two photos of the well. I called Jim King at 11:54 AM and discussed the well with him. Mr. King said that he does not own the well but might be willing to plug it. Time of inspection: 11:05 AM. Weather: 43 degrees F, Sunny
1059354481 2018-10-23 Production Wells No Violations I conducted an inspection of this well with a prospective plugging contractor. The plugging contractor said he will contact Mr. King about plugging the well.
337938468 2018-10-19 0:00 PW No Violations 0.20
PL13804 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0221245149 US-OH-122201 2018-04-03 9-9-05(A)10 Failure to legibly identify well
0221245149 US-OH-122202 2018-04-03 NONE Well shall be plugged

For data sources see[8]

References