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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-121-24425 | | Well ID: 34-121-24425 | ||
− | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39. | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.88, -81.42 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 11: | Line 11: | ||
| County: [[Noble_County,_Ohio|Noble]] | | County: [[Noble_County,_Ohio|Noble]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Seneca_Township,_Noble_County,_Ohio|Seneca Township]] |
|- | |- | ||
| Operator Name: [[ANTERO RESOURCES CORPORATION]] | | Operator Name: [[ANTERO RESOURCES CORPORATION]] | ||
Line 29: | Line 29: | ||
| Final Drill Date: 2014-03-10 | | Final Drill Date: 2014-03-10 | ||
|- | |- | ||
− | | Well Total Depth: 17018 ft | + | | Well Total Depth: 17018.00 ft |
|- | |- | ||
| Configuration: Horizontal | | Configuration: Horizontal | ||
|- | |- | ||
− | | Latitude: 39. | + | | Latitude: 39.880000 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.420000 |
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Well History == | == Well History == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 85: | Line 85: | ||
| title = Risk Based Data Management System - Well and WellHistry Tables | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Perforation Treatments == | == Perforation Treatments == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 96: | Line 96: | ||
|- | |- | ||
| 2015-02-13 | | 2015-02-13 | ||
+ | | style="text-align: right;" | 8045 | ||
+ | | style="text-align: right;" | 16933 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | | ||
+ | | style="text-align: right;" | 8045 | ||
+ | | style="text-align: right;" | 16933 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | | ||
| style="text-align: right;" | 8045 | | style="text-align: right;" | 8045 | ||
| style="text-align: right;" | 16933 | | style="text-align: right;" | 16933 | ||
Line 104: | Line 114: | ||
| title = Risk Based Data Management System - Perfs Table | | title = Risk Based Data Management System - Perfs Table | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Fracking Activities == | == Fracking Activities == | ||
==== Fracking Jobs ==== | ==== Fracking Jobs ==== | ||
Line 381: | Line 391: | ||
| title = Risk Based Data Management System - tblStimulation Table | | title = Risk Based Data Management System - tblStimulation Table | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 432: | Line 442: | ||
| title = Risk Based Data Management System - Production Table - Oil and Gas Data | | title = Risk Based Data Management System - Production Table - Oil and Gas Data | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
<ref>{{cite web | <ref>{{cite web | ||
| title = Combined Production - Oil and Gas Data | | title = Combined Production - Oil and Gas Data | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Waste Data == | == Waste Data == | ||
{| class="wikitable sortable" | {| class="wikitable sortable" | ||
Line 489: | Line 499: | ||
| title = Risk Based Data Management System - Production Table - Brine Data | | title = Risk Based Data Management System - Production Table - Brine Data | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
<ref>{{cite web | <ref>{{cite web | ||
| title = Combined Production - Brine Data | | title = Combined Production - Brine Data | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Inspection Data == | == Inspection Data == | ||
==== Inspections Performed ==== | ==== Inspections Performed ==== | ||
Line 506: | Line 516: | ||
!scope="col" style="text-align: center"| Inspection Result | !scope="col" style="text-align: center"| Inspection Result | ||
!scope="col" style="text-align: center"| Inspection Comments | !scope="col" style="text-align: center"| Inspection Comments | ||
+ | |- | ||
+ | | -1313369788 | ||
+ | | 2014-3-10 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 0.20 | ||
+ | |- | ||
+ | | -1994424449 | ||
+ | | 2017-3-10 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.50 | ||
+ | |- | ||
+ | | -223738586 | ||
+ | | 2018-11-26 0:00 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -698828612 | ||
+ | | 2017-12-27 0:00 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.20 | ||
+ | |- | ||
+ | | -801559389 | ||
+ | | 2014-1-31 0:00: | ||
+ | | CS | ||
+ | | No Violations | ||
+ | | 2.00 | ||
|- | |- | ||
| 0223738586 | | 0223738586 | ||
Line 572: | Line 612: | ||
| No Violations | | No Violations | ||
| My inspection finds Patterson Drilling ran 6656 of N-80 9.625 casing. Allied cemented the casing in place with 913 sks of Featherweight cement and 202 sks of Class A cement. | | My inspection finds Patterson Drilling ran 6656 of N-80 9.625 casing. Allied cemented the casing in place with 913 sks of Featherweight cement and 202 sks of Class A cement. | ||
+ | |- | ||
+ | | 1566308140 | ||
+ | | 2019-8-20 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.80 | ||
|- | |- | ||
| 1988428012 | | 1988428012 | ||
Line 584: | Line 630: | ||
| No Violations | | No Violations | ||
| The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. The production equipment consisted of three gas production units, eight 400 barrel tanks, two compressors, and two combustors. Identification was present and production records were current. | | The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. The production equipment consisted of three gas production units, eight 400 barrel tanks, two compressors, and two combustors. Identification was present and production records were current. | ||
+ | |- | ||
+ | | 244048604 | ||
+ | | 2013-10-21 0:00 | ||
+ | | CS | ||
+ | | No Violations | ||
+ | | 4.00 | ||
+ | |- | ||
+ | | 266665216 | ||
+ | | 2016-5-18 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | 596434982 | ||
+ | | 2014-3-3 0:00:0 | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 2.00 | ||
+ | |- | ||
+ | | 664341020 | ||
+ | | 2014-1-21 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | 714062856 | ||
+ | | 2020-10-29 0:00 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.40 | ||
|- | |- | ||
|} | |} | ||
Line 598: | Line 674: | ||
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
==References== | ==References== | ||
<references/> | <references/> |
Well ID: 34-121-24425 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Seneca Township | |
Operator Name: ANTERO RESOURCES CORPORATION | |
Well Pad ID: US-OH-000730 | |
Farm/Lease Name: VORHIES UNIT | |
License Status: Producing | |
License Date: 2013-05-23 | |
Spud Date: 2013-10-04 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2014-03-10 | |
Well Total Depth: 17018.00 ft | |
Configuration: Horizontal | |
Latitude: 39.880000 | |
Longitude: -81.420000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2013-05-23 | Proposed Formations:POINT PLEASANT, Issued Date:5/23/2013, Expired Date:5/23/2015 12:00:00 PM, Drilling unit acres:732.3, Proposed Well Type:OG, Proposed Well Class:EDPW |
Correction to Well | 2014-03-07 | CORRECTION TO PROPOSED TOTAL DEPTH, TARGET AND TAKE-POINT INFORMATION (FOOTAGE AND COORDINATES) FROM AS DRILLED SURVEY PLAT. |
Reached Total Depth | 2014-03-10 | |
Correction to Well | 2014-03-21 | CORRECTION TO TARGET INFORMATION (FOOTAGE AND COORDINATES) FROM AS DRILLED SURVEY PLAT. |
Correction to Well | 2014-06-13 | CHANGE IN TARGET AND TAKE-POINT INFORMATION (FOOTAGE AND COORDINATES) FROM AS DRILLED SURVEY PLAT. |
Completion Report Received | 2015-02-12 | |
Construction Permit Expires | 2015-05-23 | |
Record Last Modified | 2017-10-23 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2015-02-13 | 8045 | 16933 | 0 |
8045 | 16933 | 0 | |
8045 | 16933 | 0 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 05/01/2014 | 05/14/2014 | 7588 | 12,593,800.0 | 575405 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Water | Antero Resources | Base Fluid | Water | 7732-18-5 | 100 | 89.941 | 105,033,000.0 |
AP One | U.S. Well Services, LLC | Gel Breakers | Ammonium Persulfate | 7727-54-0 | 100 | 0.00138 | 1610 | |
Sand | U.S. Well Services, LLC | Proppant | Crystalline Silica, quartz | 14808-60-7 | 100 | 9.67044 | 11,293,100.0 | |
WFRA-405 | U.S. Well Services, LLC | Friction Reducer | Water | 7732-18-5 | 40 | 0.02995 | 34974.6 | |
Ethoxylated alcohol blend | Proprietary | 5 | 0.00374 | 4371.83 | ||||
Petroleum Distillates | 64742-47-8 | 22 | 0.02411 | 28154.6 | ||||
Anionic Polyacrylamide | Proprietary | 0 | 0.02995 | 34974.6 | ||||
Crystalline Salt | 12125-02-9 | 5 | 0.00374 | 4371.83 | ||||
AI-300 | U.S. Well Services, LLC | Acid Corrosion Inhibitor | Tar bases, quinoline derivs, benzyl chloride-quaternized | 72480-70-7 | 13 | 0.00011 | 132.706 | |
Triethyl Phosphate | 78-40-0 | 3 | 0.00002000 | 21.5973 | ||||
Cinnamaldehyde | 104-55-2 | 5 | 0.00012 | 134.528 | ||||
Water | 7732-18-5 | 20 | 0.00004000 | 45.5364 | ||||
Ethylene Glycol | 107-21-1 | 31 | 0.00042 | 496.13 | ||||
Ethoxylated Nonylphenol | 68412-54-4 | 5 | 0.00003000 | 35.9954 | ||||
N,N-Dimethylformamide | 68-12-2 | 15 | 0.00013 | 153.349 | ||||
2-Butoxyethanol | 111-76-2 | 7 | 0.0001 | 117.224 | ||||
Isopropyl Alcohol | 67-63-0 | 3 | 0.00001000 | 17.152 | ||||
HCL Acid (12.6%-18.0%) | U.S. Well Services, LLC | Bulk Acid | Water | 7732-18-5 | 87.5 | 0.16231 | 189545 | |
Hydrogen Chloride | 7641-01-1 | 18 | 0.03877 | 45276.2 | ||||
SI-1000 | U.S. Well Services, LLC | Scale Inhibitor | Anionic Copolymer | Proprietary | 0 | 0.00444 | 5190.47 | |
Ethylene Glycol | 107-21-1 | 20 | 0.00402 | 4691.77 | ||||
Water | 7732-18-5 | 30 | 0.00335 | 3912.54 | ||||
LGC-15 | U.S. Well Services, LLC | Gelling Agents | Suspending agent (solid) | 14808-60-7 | 3 | 0.00519 | 6062.85 | |
Surfactant | 68439-51-0 | 3 | 0.00204 | 2378.5 | ||||
Petroleum Distillates | 64742-47-8 | 60 | 0.03215 | 37543 | ||||
Guar Gum | 9000-30-0 | 50 | 0.03395 | 39641.7 | ||||
K-BAC 1020 | U.S. Well Services, LLC | Anti-Bacterial Agent | 2,2-dibromo-3-nitrilopropionamide | 10222-01-2 | 20 | 0.00539 | 6295.93 | |
Deionized Water | 7732-18-5 | 28 | 0.00308 | 3596.21 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2014-05-14 | H2O | 15 | 5576 Bbl | 230730 | US Well Services Inc | STAGE 51/51
60 SHOTS |
2014-05-01 | H2O | 1 | 6704 Bbl | 215040 | US Well Services Inc | STAGE 1/51
60 SHOTS STAGES 2-50 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | ANTERO RESOURCES CORPORATION | 892088 | 47756 | 171 |
2015 | ANTERO RESOURCES CORPORATION | 982291 | 32196 | 365 |
2016 | ANTERO RESOURCES CORPORATION | 537889 | 9949 | 359 |
2017 | ANTERO RESOURCES CORPORATION | 373659 | 5543 | 365 |
2018 | ANTERO RESOURCES CORPORATION | 250383 | 2701 | 359 |
2019 | ANTERO RESOURCES CORPORATION | 56054 | 396 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | ANTERO RESOURCES CORPORATION | Brine | 12587 | 171 |
2015 | ANTERO RESOURCES CORPORATION | Brine | 6423 | 365 |
2016 | ANTERO RESOURCES CORPORATION | Brine | 2459 | 359 |
2017 | ANTERO RESOURCES CORPORATION | Brine | 1517 | 365 |
2018 | ANTERO RESOURCES CORPORATION | Brine | 1065 | 359 |
2019 | ANTERO RESOURCES CORPORATION | Brine | 126 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1313369788 | 2014-3-10 0:00: | DD | No Violations | 0.20 |
-1994424449 | 2017-3-10 0:00: | PW | No Violations | 0.50 |
-223738586 | 2018-11-26 0:00 | PW | No Violations | 1.00 |
-698828612 | 2017-12-27 0:00 | PW | No Violations | 0.20 |
-801559389 | 2014-1-31 0:00: | CS | No Violations | 2.00 |
0223738586 | 2018-11-26 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with 5.5-inch diameter production casing and 2.875-inch diameter tubing equipped with a plunger lift system. At the time of my inspection annular pressure monitoring was in place, and the 13.375-inch diameter casing had 180 pounds per square inch, the 9.625-inch diameter casing had 0 pounds per square inch. Production equipment included a Gas Processing Unit, as well as 8- 400-barrel steel production fluid tanks, and 2 combustors that were shared with the other producing wells on the pad. There was secondary containment around the production fluid tanks, and the Gas Processing Units. The well pad was contained within an earthen dike, there were multiple Emergency Shutoff Devices on location. There was a midstream valve site near located to the south of the pad. Identification tags were present, and production was up to date. |
0244048604 | 2013-10-21 | Casing String Witnessed | No Violations | My inspection today finds the rig ran 13.375 casing to 1869. Allied cemented the casing in place with 1592 sks of class A cement with 2% floseal. |
0266665216 | 2016-05-18 | Production Wells | No Violations | My inspection today finds the well is equipped in a manner consistent with being capable of production. The production valves are open. The tank battery consists of eight 400 barrel tanks set in a plastic lined steel containment system. Antero personnel Zac Cornish and Josh Horn are on location. I am accompanied by a number of division staff. |
0596434982 | 2014-03-03 | Drill / Deepen / Reopen | No Violations | My inspection finds the rig is drilling a 8.5 hole at 15380. Inspection of the site found no violations. |
0664341020 | 2014-01-21 | Drill / Deepen / Reopen | No Violations | My inspection today finds the rig is currently drilling an 8.5 hole at a depth of 7515. |
0698828612 | 2017-12-27 | Production Wells | No Violations | The purpose of my inspection was a status check on a production well. The well was equipped with a production tree style wellhead with a plunger lift system. Production valves were in the open position. Pressure monitoring was present. The production equipment consisted of eight 400 barrel tanks within steel line containment, three gas production units, one vapor recovery tower, two compressors, one vent scrubber, and two combustors. The identification was located at the wellhead. |
0801559389 | 2014-01-31 | Casing String Witnessed | No Violations | My inspection finds the Franks is running casing with Patterson rig 316. The current depth is 8224. The rig is experiencing mud weight loss due to excessive gas, they are circulating 13 pound mud to ensure well control. |
1170461646 | 2013-10-07 | Drill / Deepen / Reopen | No Violations | My inspection today finds the 26 casing has been cemented in place. The cellar has been covered for safety. |
1313369788 | 2014-03-10 | Drill / Deepen / Reopen | No Violations | I received an e-mail from the company representative stating that they are rigging down and preparing to leave the county. |
1435925854 | 2014-11-05 | Preliminary Restoration | No Violations | My inspection today finds the well is equipped with tubing and is produced by open flow through a choke. The tank battery is comprised of eight 400 barrel tanks located in a steel framed and plastic lined containment. The well site meets preliminary restoration requirements. |
1544066039 | 2014-02-26 | Casing String Witnessed | No Violations | My inspection finds Patterson Drilling ran 6656 of N-80 9.625 casing. Allied cemented the casing in place with 913 sks of Featherweight cement and 202 sks of Class A cement. |
1566308140 | 2019-8-20 0:00: | PW | No Violations | 0.80 |
1988428012 | 2013-12-24 | Drill / Deepen / Reopen | No Violations | Patterson rig 316 has rigged up and is currently making up their bottom hole assembly. Containment is in place as required. |
1994424449 | 2017-03-10 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. The production equipment consisted of three gas production units, eight 400 barrel tanks, two compressors, and two combustors. Identification was present and production records were current. |
244048604 | 2013-10-21 0:00 | CS | No Violations | 4.00 |
266665216 | 2016-5-18 0:00: | PW | No Violations | 1.00 |
596434982 | 2014-3-3 0:00:0 | DD | No Violations | 2.00 |
664341020 | 2014-1-21 0:00: | DD | No Violations | 1.00 |
714062856 | 2020-10-29 0:00 | PW | No Violations | 0.40 |
For data sources see[10]