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Difference between revisions of "34-121-24611"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-121-24611
 
| Well ID: 34-121-24611
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.898851458, -81.27383376 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.89, -81.27 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 11: Line 11:
 
| County: [[Noble_County,_Ohio|Noble]]
 
| County: [[Noble_County,_Ohio|Noble]]
 
|-
 
|-
| Municipality: [[Beaver Township,_Noble_County,_Ohio|Beaver Township]]
+
| Municipality: [[Beaver_Township,_Noble_County,_Ohio|Beaver Township]]
 
|-
 
|-
 
| Operator Name: [[ANTERO RESOURCES  CORPORATION]]
 
| Operator Name: [[ANTERO RESOURCES  CORPORATION]]
Line 29: Line 29:
 
| Final Drill Date: 2016-12-20
 
| Final Drill Date: 2016-12-20
 
|-
 
|-
| Well Total Depth: 16803 ft
+
| Well Total Depth: 16803.00 ft
 
|-
 
|-
 
| Configuration: Horizontal
 
| Configuration: Horizontal
 
|-
 
|-
| Latitude: 39.898851458
+
| Latitude: 39.890000
 
|-
 
|-
| Longitude: -81.27383376
+
| Longitude: -81.270000
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Well History ==
 
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 77: Line 77:
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<!--== Perforation Treatments ==
 
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Comments
 
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| -1547056269
 +
| 2018-9-18 0:00:
 +
| DD
 +
| No Violations
 +
| 0.20
 +
|-
 +
| -159621927
 +
| 2018-1-4 0:00:0
 +
| DD
 +
| No Violations
 +
| 1.00
 +
|-
 +
| -170564787
 +
| 2017-7-11 0:00:
 +
| CT
 +
| No Violations
 +
| 0.50
 +
|-
 +
| -388233333
 +
| 2017-8-31 0:00:
 +
| DD
 +
| No Violations
 +
| 1.00
 
|-
 
|-
 
| 0134448409
 
| 0134448409
Line 203: Line 227:
 
| No Violations
 
| No Violations
 
| I arrived on location to witness Express Energy Services set conductor casing on the WEHR UNIT 3H. Prior to my arrival Inspector Conrad had approved them to set the conductor to 80 feet. We set the conductor using 257 sacks of class A cement with 2% NaCl and about a half a pound of flake. The weight of the cement was 15.6 pounds and had a 1.18 yield with a 32.19 mix. We used a total of 43.35 barrels of fluid for displacement. When we finished setting the casing we had a 10 foot shoe. After we had finished setting the conductor we had about 18 barrels of cement come back to surface and 47 barrels of water come to surface giving us a total of 65 barrels total to surface.
 
| I arrived on location to witness Express Energy Services set conductor casing on the WEHR UNIT 3H. Prior to my arrival Inspector Conrad had approved them to set the conductor to 80 feet. We set the conductor using 257 sacks of class A cement with 2% NaCl and about a half a pound of flake. The weight of the cement was 15.6 pounds and had a 1.18 yield with a 32.19 mix. We used a total of 43.35 barrels of fluid for displacement. When we finished setting the casing we had a 10 foot shoe. After we had finished setting the conductor we had about 18 barrels of cement come back to surface and 47 barrels of water come to surface giving us a total of 65 barrels total to surface.
 +
|-
 +
| 134448409
 +
| 2017-6-3 0:00:0
 +
| CT
 +
| No Violations
 +
|
 
|-
 
|-
 
| 1500305558
 
| 1500305558
Line 221: Line 251:
 
| No Violations
 
| No Violations
 
| The Wehr pad has a total of 7 wells, 6 production wells, and 1 well that has not been completed Antero Operations Manager contacted me on 1/5/18 and stated that they would like to get the well plugged on using the drilling permit that expires 10/3/18. I have not received a plugging proposal. The 5.5-inch diameter production casing reportedly has a defective spot roughly 2200 feet in depth. During my inspection the well was equipped with a frac valve in the closed position on the 5.5-inch diameter production casing. Gauges indicate that there was 400 pounds per square inch on the 13.375-inch diameter surface casing and 1600 pounds per square inch on the 9.625-inch diameter intermediate casing.
 
| The Wehr pad has a total of 7 wells, 6 production wells, and 1 well that has not been completed Antero Operations Manager contacted me on 1/5/18 and stated that they would like to get the well plugged on using the drilling permit that expires 10/3/18. I have not received a plugging proposal. The 5.5-inch diameter production casing reportedly has a defective spot roughly 2200 feet in depth. During my inspection the well was equipped with a frac valve in the closed position on the 5.5-inch diameter production casing. Gauges indicate that there was 400 pounds per square inch on the 13.375-inch diameter surface casing and 1600 pounds per square inch on the 9.625-inch diameter intermediate casing.
 +
|-
 +
| 1603125352
 +
| 2020-10-19 0:00
 +
| CT
 +
| No Violations
 +
| 0.20
 
|-
 
|-
 
| 2110079674
 
| 2110079674
Line 227: Line 263:
 
| No Violations
 
| No Violations
 
|  Status check inspection found the well drilling process was completed and during the stimulation process the 5.5 diameter production casing was damaged or split at or around 2,200. The company reported they did try to set a casing patch to isolate the split in the casing. Also reported was (2) stages were stimulated prior to the casing failure. 2 cast iron bridge plugs were reported set in the 5.5 diameter production casing. Annular pressure monitoring is in place and installed on the well head A&B sections with 2 diameter riser pipes equipped with valves and gauges being present. The 2riser pipes are tied into a main 2 sales line that is ran to the production tank battery area. The A section gauge reads 450 pounds pressure and the B section gauge reads 1,750 pounds pressure. A completion master valve is present atop the B section flow cross however no gauge is present to indicate the 5.5 diameter casing internal pressure. On this day I contacted Antero Completion Supervisor Tim Neil who indicated the company has plans to plug the well.
 
|  Status check inspection found the well drilling process was completed and during the stimulation process the 5.5 diameter production casing was damaged or split at or around 2,200. The company reported they did try to set a casing patch to isolate the split in the casing. Also reported was (2) stages were stimulated prior to the casing failure. 2 cast iron bridge plugs were reported set in the 5.5 diameter production casing. Annular pressure monitoring is in place and installed on the well head A&B sections with 2 diameter riser pipes equipped with valves and gauges being present. The 2riser pipes are tied into a main 2 sales line that is ran to the production tank battery area. The A section gauge reads 450 pounds pressure and the B section gauge reads 1,750 pounds pressure. A completion master valve is present atop the B section flow cross however no gauge is present to indicate the 5.5 diameter casing internal pressure. On this day I contacted Antero Completion Supervisor Tim Neil who indicated the company has plans to plug the well.
 +
|-
 +
| 410177289
 +
| 2017-10-11 0:00
 +
| DD
 +
| No Violations
 +
| 0.50
 +
|-
 +
| 531973000
 +
| 2016-10-20 0:00
 +
| CS
 +
| No Violations
 +
| 5.00
 +
|-
 +
| 815221556
 +
| 2019-12-24 0:00
 +
| PW
 +
| No Violations
 +
| 0.50
 +
|-
 +
| 956215398
 +
| 2016-12-20 0:00
 +
| DD
 +
| No Violations
 +
| 3.50
 +
|-
 +
| 975832742
 +
| 2017-6-3 0:00:0
 +
| CT
 +
| No Violations
 +
| 0.50
 
|-
 
|-
 
|}
 
|}
Line 241: Line 307:
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Ohio Wells]]
 
[[Category:Ohio Wells]]

Latest revision as of 04:07, 12 January 2021

Well Details

Well ID: 34-121-24611
Loading map...
Country: United States
State: Ohio
County: Noble
Municipality: Beaver Township
Operator Name: ANTERO RESOURCES CORPORATION
Well Pad ID: US-OH-001402
Farm/Lease Name: WEHR UNIT
License Status: Well Drilled
License Date: 2016-10-03
Spud Date: 2016-09-08
Spud Drilling Contractor: FRONTIER DRILLING
Final Drill Date: 2016-12-20
Well Total Depth: 16803.00 ft
Configuration: Horizontal
Latitude: 39.890000
Longitude: -81.270000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2016-08-29 Proposed Formations:POINT PLEASANT, Issued Date:8/29/2016, Expired Date:8/29/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2016-10-03 Proposed Formations:POINT PLEASANT, Issued Date:10/3/2016, Expired Date:10/3/2018 12:00:00 PM, Drilling unit acres:475.503, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2016-12-20
Correction to Well 2017-03-03 UPDATE TARGET/TAKEPOINT/ACREAGE PER AS-DRILLED PLAT RCVD 2-13-17-ALE
Record Last Modified 2017-11-14
Construction Permit Expires 2018-10-03

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1547056269 2018-9-18 0:00: DD No Violations 0.20
-159621927 2018-1-4 0:00:0 DD No Violations 1.00
-170564787 2017-7-11 0:00: CT No Violations 0.50
-388233333 2017-8-31 0:00: DD No Violations 1.00
0134448409 2017-06-03 Completion Testing No Violations Status check inspection found the well drilling process now complete and the company has reported they were unsuccessful in getting wireline to go to the bottom of the well bore to begin the stimulation process by perforating the well bore 5.5 diameter production casing. A service rig will be brought in at a later date.
0159621927 2018-01-04 Drill / Deepen / Reopen No Violations
0170564787 2017-07-11 Completion Testing No Violations The purpose of my inspection was a status check on completion operations. During my inspection the well was equipped with a Frac Valve in the closed position. This well has not been hydraulically stimulated.
0388233333 2017-08-31 Drill / Deepen / Reopen No Violations The purpose of my inspection was a status check. The well was equipped with a Frac valve in the closed position with no lines attached. The additional six wells on the pad were all in production.
0410177289 2017-10-11 Drill / Deepen / Reopen No Violations The purpose of my inspection was a status check. The status of the well had not changed since last inspection; the well was equipped with a Frac valve in the closed position with no lines attached. The additional six wells on the pad were all in production.
0531973000 2016-10-20 Casing String Witnessed No Violations On the day of my inspection I witnessed that Frontier Drilling Rig #32 had drilled a 17.5 inch diameter hole to the depth of 1052 feet. Wyoming Casing Crew ran 1042 feet of 13.375 inch 54.5 pound per foot J-55 casing. C & J Energy Services was on site and gained circulation with 183 barrels of fresh water, pumped 25 barrels of gel, 10 barrels of fresh water and cemented casing with 1009 sacks of Class A cement weighing 15.6 pounds per gallon and a yield of 1.19 cubic foot per sack cement. Cement additives included 2% calcium chloride and .25 pound per sack of cello-flake. Cement weight was verified by pressurized mud scales. Cement was displaced with 155 barrels of fresh water and circulated to surface with good returns of 47 barrels. The plug was landed at 420 pounds per square inch and pressured to 920 pounds per square inch for 5 minutes and the floats held with 1bbl back. Mix water was tested revealing chlorides of 61 parts per million, pH 7 and 60 degrees.
0956215398 2016-12-20 Drill / Deepen / Reopen No Violations On the day of my inspection I witnessed that Frontier Drilling Rig #32 had reached total depth of their lateral with an 8.75 inch diameter bit at 16803 feet and was cleaning the wellbore with 10.5 pound per gallon (ppg) mud simulating 11.9 ppg. Frontier Drilling Rig #32 is planning on circulating 6 bottoms up before tripping out of the wellbore and running 5.5 inch diameter production casing with cementing to follow. I completed walk around with Antero Consultant Steve Guffey revealing proper containment was in place.
0975832742 2017-06-03 Completion Testing No Violations Status check inspection on the well completion process found no stimulation of the well has been conducted and the company is awaiting a service rig to be mobilized onto the well to conduct a downhole clean out run.
1129926828 2016-09-09 Casing String Witnessed No Violations I arrived on location to witness Express Energy Services set conductor casing on the WEHR UNIT 3H. Prior to my arrival Inspector Conrad had approved them to set the conductor to 80 feet. We set the conductor using 257 sacks of class A cement with 2% NaCl and about a half a pound of flake. The weight of the cement was 15.6 pounds and had a 1.18 yield with a 32.19 mix. We used a total of 43.35 barrels of fluid for displacement. When we finished setting the casing we had a 10 foot shoe. After we had finished setting the conductor we had about 18 barrels of cement come back to surface and 47 barrels of water come to surface giving us a total of 65 barrels total to surface.
134448409 2017-6-3 0:00:0 CT No Violations
1500305558 2017-07-17 Drill / Deepen / Reopen No Violations Status check inspection found the well has defective 5.5 diameter production casing and is slated to be plugged. The remainder of the 6 wells on the pad are now in production. The company production men on site indicated the wells were dispersing the sand trap separators into a open top gas buster tank. I advised them to move the water truck pick up point to a safe area that was not downwind of the gas buster tank to avoid gas fumes from the engine from being introduced into the trucks engine while it was loading product.
1534117886 2017-03-06 Preliminary Restoration No Violations Preliminary Restoration status check inspection accompanied by ODNR County Inspector Austin Gutridge. The area affected by the well pad construction meets ORC 1509.072 with vegetation established and erosion control in place. The lease road is stoned and in good repair. Signage is posted at the well pad entrance. Halliburton crews are on site preparing to begin the well stimulation 5.5 diameter production casing toe preparations.
1547056269 2018-09-18 Drill / Deepen / Reopen No Violations The Wehr pad has a total of 7 wells, 6 production wells, and 1 well that has not been completed Antero Operations Manager contacted me on 1/5/18 and stated that they would like to get the well plugged on using the drilling permit that expires 10/3/18. I have not received a plugging proposal. The 5.5-inch diameter production casing reportedly has a defective spot roughly 2200 feet in depth. During my inspection the well was equipped with a frac valve in the closed position on the 5.5-inch diameter production casing. Gauges indicate that there was 400 pounds per square inch on the 13.375-inch diameter surface casing and 1600 pounds per square inch on the 9.625-inch diameter intermediate casing.
1603125352 2020-10-19 0:00 CT No Violations 0.20
2110079674 2019-02-13 Completion Testing No Violations Status check inspection found the well drilling process was completed and during the stimulation process the 5.5 diameter production casing was damaged or split at or around 2,200. The company reported they did try to set a casing patch to isolate the split in the casing. Also reported was (2) stages were stimulated prior to the casing failure. 2 cast iron bridge plugs were reported set in the 5.5 diameter production casing. Annular pressure monitoring is in place and installed on the well head A&B sections with 2 diameter riser pipes equipped with valves and gauges being present. The 2riser pipes are tied into a main 2 sales line that is ran to the production tank battery area. The A section gauge reads 450 pounds pressure and the B section gauge reads 1,750 pounds pressure. A completion master valve is present atop the B section flow cross however no gauge is present to indicate the 5.5 diameter casing internal pressure. On this day I contacted Antero Completion Supervisor Tim Neil who indicated the company has plans to plug the well.
410177289 2017-10-11 0:00 DD No Violations 0.50
531973000 2016-10-20 0:00 CS No Violations 5.00
815221556 2019-12-24 0:00 PW No Violations 0.50
956215398 2016-12-20 0:00 DD No Violations 3.50
975832742 2017-6-3 0:00:0 CT No Violations 0.50

For data sources see[3]

References