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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-153-20894 | | Well ID: 34-153-20894 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 41.02, -81.56 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | Country: United States |
+ | |- | ||
+ | | State: Ohio | ||
+ | |- | ||
+ | | County: <County> | ||
|- | |- | ||
| Municipality: | | Municipality: | ||
Line 13: | Line 17: | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: AKZO SALT {SMP #3) |
|- | |- | ||
− | | | + | | License Status: Plugged and Abandoned |
|- | |- | ||
− | | | + | | License Date: 2014-10-29 |
|- | |- | ||
| Spud Date: 1981-03-20 | | Spud Date: 1981-03-20 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: [[PERKINS DRLG]] |
+ | |- | ||
+ | | Final Drill Date: 1981-04-03 | ||
+ | |- | ||
+ | | Well Total Depth: 3141.00 ft | ||
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Well Status: | + | | Latitude: 41.020000 |
+ | |- | ||
+ | | Longitude: -81.560000 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | CO | ||
+ | | 1981-03-18 | ||
+ | | 1053 AKZO NOBEL SALT INC GeoDate 3/18/81 | ||
+ | |- | ||
+ | | Original Spud | ||
+ | | 1981-03-21 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | | Completed | ||
+ | | 1981-04-03 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | | Reached Total Depth | ||
+ | | 1981-04-03 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | | Annulus Pressure Monitoring Approved | ||
+ | | 1995-09-11 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | | Last Compliance Report | ||
+ | | 2005-10-18 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | | APP | ||
+ | | 2014-10-29 | ||
+ | | Proposed Formations:SALINA, Issued Date:10/29/2014, Expired Date:10/28/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SMP | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 2015-10-29 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | | Plugged/Abandoned | ||
+ | | 2015-11-06 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2017-02-10 | ||
+ | | GL=967.3, DF=993.3 CLASS=BRINE WELL | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
|- | |- | ||
− | | | + | | 1999-09-01 |
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | |
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | |
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Perfs Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | -1272075487 | |
+ | | 2015-11-3 0:00: | ||
+ | | SM | ||
+ | | No Violations | ||
+ | | | ||
+ | |- | ||
+ | | -2130303279 | ||
+ | | 2009-6-8 0:00:0 | ||
+ | | SM | ||
+ | | No Violations | ||
+ | | | ||
+ | |- | ||
+ | | -585181124 | ||
+ | | 2003-6-18 0:00: | ||
+ | | SM | ||
+ | | No Violations | ||
+ | | | ||
+ | |- | ||
+ | | 0238042556 | ||
+ | | 2004-10-19 | ||
+ | | Solution Mining Project | ||
+ | | No Violations | ||
+ | | Status check inspection - no violations at this time. | ||
+ | |- | ||
+ | | 0585181124 | ||
+ | | 2003-06-18 | ||
+ | | Solution Mining Project | ||
+ | | No Violations | ||
+ | | Solution mining status check - no violations at this time. | ||
|- | |- | ||
| 1129555155 | | 1129555155 | ||
| 2005-10-11 | | 2005-10-11 | ||
− | | | + | | Solution Mining Project |
+ | | No Violations | ||
| The purpose of this inspection was to complete the 5 year mechanical integrity test of the 8-5/8 casing. The reference well was the 7 casing in this well. The following data was collected. | | The purpose of this inspection was to complete the 5 year mechanical integrity test of the 8-5/8 casing. The reference well was the 7 casing in this well. The following data was collected. | ||
Time Test Press. Ref. Press Difference Time Test Press. Ref. Press. Difference | Time Test Press. Ref. Press Difference Time Test Press. Ref. Press. Difference | ||
Line 55: | Line 229: | ||
12:03 513.648 150.717 362.931 | 12:03 513.648 150.717 362.931 | ||
13:03 513.683 150.752 362.931 Test Passed | 13:03 513.683 150.752 362.931 Test Passed | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 1272075487 | ||
+ | | 2015-11-03 | ||
+ | | Solution Mining Project | ||
+ | | No Violations | ||
+ | | I was on location to observe the plugging of the Akzo # 56 solution mining well. The 7 tubing was hung in the 8.625 production casing, stretch calcutions indicated a freepoint at about 1000 down. After circulating and reciprocating the 7 tubing, it became free after pulling 105,000 lbs ( ~ 43,300 lbs over string weght ) After dragging out for the first five (5) joints of 7 Key Well Services was able to remove 67 joints of 7 ( 23lb/ft with slim hole collars ). Approximate tally was 2680. Preparations were be made to test the mechanical integrity of the 8.625 production casing. No violations identified during this inspection. | ||
+ | |- | ||
+ | | 1447167470 | ||
+ | | 2015-11-04 | ||
+ | | Solution Mining Project | ||
+ | | No Violations | ||
+ | | I was on the Akzo # 56 location to observe the setting of the mechanical bridge plug and the Mechanical Ingetrity Testing dry run test. Baker Hughes Services previously ran a Segmented Bond Tool - Gamma Ray Log for cement bond evaluation. The bond quality was deemed adequate to proceed with the placement of the Bridge Plug and MIT pretest. Key Energy Services (KES) ran 2.875 tubing with a Mechanical Bridge Plug ( MBP) to be set at 2496 GL. The MBP was set with pressure pumped down the tubing at 3300 psi. KES removed the tubing from the 8.625 casing to recover the setting tool on the end of the tubing. KES ran the tubing back into the casing to run the simulated M I T procedure. Pressure was increased on the 8.625 casing to 580 psi. The five (5) pressure decline allowance calculated to be 29 psi. The pressure decline exceeded the allowable within 30 seconds. A number of leaks were repaired and the casing was pressurized twice again with the same decline profile. This testing was a dry run to identify possible pressure losses. Cargill Inc. personnel ( Mike Schumacher ) shut down for the day to wait for Universal Well Services to be on location on the next morning. No violations identified during this inspection. | ||
+ | |- | ||
+ | | 1460992851 | ||
+ | | 2015-10-30 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | A total of 2460 feet of seven inch tubing was recovered previously. The casing was scraped. A Weatherford DB-8 bridge plug was set at 2440 feet. The plug passed a pressure test. The well was plugged in stages, through tubing, from the bridge plug to the surface. A total of 926 sacks of Type-1 cement were used. All conditions were acceptable. | ||
+ | |- | ||
+ | | 1746858019 | ||
+ | | 2015-11-17 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | I was on the Akzo # 56 site to witness the topping off of the 8.625 casing with nine (9) sack grout. After the initial top plug fell back to 22 down the casing Cargill Inc. filled the open pipe with approximately one (1) cubic yard of nine (9) sack grout to the top. Orrville Ready Mix supplied the grout. R G Smith were welding the required I D plate as I left location. No violations identified during this inspection. | ||
|- | |- | ||
− | | | + | | 2130303279 |
| 2009-06-08 | | 2009-06-08 | ||
− | | | + | | Solution Mining Project |
+ | | No Violations | ||
| Annual status check inspection found no violations at this time. | | Annual status check inspection found no violations at this time. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 238042556 | | 238042556 | ||
− | | 2004-10-19 | + | | 2004-10-19 0:00 |
− | | | + | | SM |
− | | | + | | No Violations |
− | |||
− | |||
| | | | ||
|- | |- | ||
+ | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
|- | |- | ||
− | | - | + | |}--> |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-153-20894 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: CARGILL INC | |
Well Pad ID: | |
Farm/Lease Name: AKZO SALT {SMP #3) | |
License Status: Plugged and Abandoned | |
License Date: 2014-10-29 | |
Spud Date: 1981-03-20 | |
Spud Drilling Contractor: PERKINS DRLG | |
Final Drill Date: 1981-04-03 | |
Well Total Depth: 3141.00 ft | |
Configuration: Vertical | |
Latitude: 41.020000 | |
Longitude: -81.560000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-03-18 | 1053 AKZO NOBEL SALT INC GeoDate 3/18/81 |
Original Spud | 1981-03-21 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
Completed | 1981-04-03 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
Reached Total Depth | 1981-04-03 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
Annulus Pressure Monitoring Approved | 1995-09-11 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
Last Compliance Report | 2005-10-18 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
APP | 2014-10-29 | Proposed Formations:SALINA, Issued Date:10/29/2014, Expired Date:10/28/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SMP |
Construction Permit Expires | 2015-10-29 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
Plugged/Abandoned | 2015-11-06 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
Record Last Modified | 2017-02-10 | GL=967.3, DF=993.3 CLASS=BRINE WELL |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1999-09-01 | 0 | 0 | |
0 | 0 | ||
0 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1272075487 | 2015-11-3 0:00: | SM | No Violations | |
-2130303279 | 2009-6-8 0:00:0 | SM | No Violations | |
-585181124 | 2003-6-18 0:00: | SM | No Violations | |
0238042556 | 2004-10-19 | Solution Mining Project | No Violations | Status check inspection - no violations at this time. |
0585181124 | 2003-06-18 | Solution Mining Project | No Violations | Solution mining status check - no violations at this time. |
1129555155 | 2005-10-11 | Solution Mining Project | No Violations | The purpose of this inspection was to complete the 5 year mechanical integrity test of the 8-5/8 casing. The reference well was the 7 casing in this well. The following data was collected.
Time Test Press. Ref. Press Difference Time Test Press. Ref. Press. Difference 08:03 513.496 150.532 362.964 14:03 513.694 150.782 362.912 09:03 513.534 150.587 362.947 15:03 513.719 150.792 362.927 10:03 513.570 150.636 362.934 16:03 513.732 150.795 362.937 11:03 513.605 150.681 362.924 12:03 513.648 150.717 362.931 13:03 513.683 150.752 362.931 Test Passed |
1272075487 | 2015-11-03 | Solution Mining Project | No Violations | I was on location to observe the plugging of the Akzo # 56 solution mining well. The 7 tubing was hung in the 8.625 production casing, stretch calcutions indicated a freepoint at about 1000 down. After circulating and reciprocating the 7 tubing, it became free after pulling 105,000 lbs ( ~ 43,300 lbs over string weght ) After dragging out for the first five (5) joints of 7 Key Well Services was able to remove 67 joints of 7 ( 23lb/ft with slim hole collars ). Approximate tally was 2680. Preparations were be made to test the mechanical integrity of the 8.625 production casing. No violations identified during this inspection. |
1447167470 | 2015-11-04 | Solution Mining Project | No Violations | I was on the Akzo # 56 location to observe the setting of the mechanical bridge plug and the Mechanical Ingetrity Testing dry run test. Baker Hughes Services previously ran a Segmented Bond Tool - Gamma Ray Log for cement bond evaluation. The bond quality was deemed adequate to proceed with the placement of the Bridge Plug and MIT pretest. Key Energy Services (KES) ran 2.875 tubing with a Mechanical Bridge Plug ( MBP) to be set at 2496 GL. The MBP was set with pressure pumped down the tubing at 3300 psi. KES removed the tubing from the 8.625 casing to recover the setting tool on the end of the tubing. KES ran the tubing back into the casing to run the simulated M I T procedure. Pressure was increased on the 8.625 casing to 580 psi. The five (5) pressure decline allowance calculated to be 29 psi. The pressure decline exceeded the allowable within 30 seconds. A number of leaks were repaired and the casing was pressurized twice again with the same decline profile. This testing was a dry run to identify possible pressure losses. Cargill Inc. personnel ( Mike Schumacher ) shut down for the day to wait for Universal Well Services to be on location on the next morning. No violations identified during this inspection. |
1460992851 | 2015-10-30 | Plug / Plug Back | No Violations | A total of 2460 feet of seven inch tubing was recovered previously. The casing was scraped. A Weatherford DB-8 bridge plug was set at 2440 feet. The plug passed a pressure test. The well was plugged in stages, through tubing, from the bridge plug to the surface. A total of 926 sacks of Type-1 cement were used. All conditions were acceptable. |
1746858019 | 2015-11-17 | Plug / Plug Back | No Violations | I was on the Akzo # 56 site to witness the topping off of the 8.625 casing with nine (9) sack grout. After the initial top plug fell back to 22 down the casing Cargill Inc. filled the open pipe with approximately one (1) cubic yard of nine (9) sack grout to the top. Orrville Ready Mix supplied the grout. R G Smith were welding the required I D plate as I left location. No violations identified during this inspection. |
2130303279 | 2009-06-08 | Solution Mining Project | No Violations | Annual status check inspection found no violations at this time. |
238042556 | 2004-10-19 0:00 | SM | No Violations |
For data sources see[4]