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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-031-26823 | | Well ID: 34-031-26823 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 40.26, -81.97 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | Operator Name: [[ | + | | County: [[Coshocton_County,_Ohio|Coshocton]] |
+ | |- | ||
+ | | Municipality: [[Jackson_Township,_Coshocton_County,_Ohio|Jackson Township]] | ||
+ | |- | ||
+ | | Operator Name: [[DIVERSIFIED PRODUCTION LLC]] | ||
|- | |- | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: OXFORD-PEABODY |
|- | |- | ||
− | | | + | | License Status: Producing |
|- | |- | ||
− | | | + | | License Date: 2001-03-22 |
|- | |- | ||
| Spud Date: 2001-04-07 | | Spud Date: 2001-04-07 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: [[PROFESSIONAL WELL SVC-PWS]] |
+ | |- | ||
+ | | Final Drill Date: 2001-04-11 | ||
+ | |- | ||
+ | | Well Total Depth: 3916.00 ft | ||
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Well Status: | + | | Latitude: 40.260000 |
+ | |- | ||
+ | | Longitude: -81.970000 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | APP | ||
+ | | 2001-03-22 | ||
+ | | 79 OXFORD OIL COMPANY Proposed Formation CLINTON Issued Date 3/22/01 Expired Date 3/22/02 6:00:00 AM | ||
+ | |- | ||
+ | | Original Spud | ||
+ | | 2001-04-07 | ||
+ | | RBDMS Rec | ||
+ | |- | ||
+ | | Completed | ||
+ | | 2001-04-11 | ||
+ | | RBDMS Rec | ||
|- | |- | ||
− | | | + | | Reached Total Depth |
+ | | 2001-04-11 | ||
+ | | RBDMS Rec | ||
|- | |- | ||
− | | | + | | Completion Report Received |
+ | | 2001-12-10 | ||
+ | | RBDMS Rec | ||
|- | |- | ||
− | | | + | | Construction Permit Expires |
+ | | 2002-03-22 | ||
+ | | RBDMS Rec | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2014-02-06 | ||
+ | | Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2016-08-02 | ||
+ | | Operator changed from 9216, ECLIPSE RESOURCES-OHIO LLC to 8685, M & R INVESTMENTS OHIO LLC | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2017-02-15 | ||
+ | | RBDMS Rec | ||
|- | |- | ||
|} | |} | ||
− | == | + | For data sources see<ref>{{cite web |
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Perforation Treatments == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Perforation Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Interval Top (ft) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Interval Base (ft) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Number of Shots |
− | + | |- | |
− | + | | 2002-01-25 | |
− | + | | style="text-align: right;" | 3744 | |
+ | | style="text-align: right;" | 3788 | ||
+ | | style="text-align: right;" | 24 | ||
|- | |- | ||
− | |||
− | |||
| | | | ||
+ | | style="text-align: right;" | 3744 | ||
+ | | style="text-align: right;" | 3788 | ||
+ | | style="text-align: right;" | 24 | ||
+ | |- | ||
| | | | ||
− | | | + | | style="text-align: right;" | 3744 |
− | | style="text-align:right;" | | + | | style="text-align: right;" | 3788 |
− | | | + | | style="text-align: right;" | 24 |
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Perfs Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
|- | |- | ||
+ | |}--> | ||
+ | == Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
|- | |- | ||
− | |||
− | |||
| | | | ||
+ | | H2O | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 2641 Bbl | ||
+ | | style="text-align: right;" | 23500 | ||
| | | | ||
| | | | ||
− | |||
− | |||
|- | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblStimulation Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 2001 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 2364.00 | ||
+ | | style="text-align: right;" | 269.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2002 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 5237.00 | ||
+ | | style="text-align: right;" | 253.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2003 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 3395.00 | ||
+ | | style="text-align: right;" | 147.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2004 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 2813.00 | ||
+ | | style="text-align: right;" | 107.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2005 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 1717.00 | ||
+ | | style="text-align: right;" | 61.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2006 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 1040.00 | ||
+ | | style="text-align: right;" | 102.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2007 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 811.00 | ||
+ | | style="text-align: right;" | 46.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2008 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 768.00 | ||
+ | | style="text-align: right;" | 64.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2009 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 783.00 | ||
+ | | style="text-align: right;" | 62.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[MACKENCO INC]] | ||
+ | | style="text-align: right;" | 339.00 | ||
+ | | style="text-align: right;" | 536.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 491.00 | ||
+ | | style="text-align: right;" | 42.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[OXFORD OIL]] | ||
+ | | style="text-align: right;" | 440.00 | ||
+ | | style="text-align: right;" | 24.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2013 | ||
+ | | [[ECLIPSE RESOURCES-OHIO LLC]] | ||
+ | | style="text-align: right;" | 400.00 | ||
+ | | style="text-align: right;" | 38.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[ECLIPSE RESOURCES-OHIO LLC]] | ||
+ | | style="text-align: right;" | 748.00 | ||
+ | | style="text-align: right;" | 41.00 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2015 |
− | | style="text-align:right;" | | + | | [[ECLIPSE RESOURCES-OHIO LLC]] |
− | | | + | | style="text-align: right;" | 465.00 |
− | + | | style="text-align: right;" | 48.00 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2016 | ||
+ | | [[M & R INVESTMENTS OHIO LLC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2017 |
− | | style="text-align:right;" | | + | | [[M & R INVESTMENTS OHIO LLC]] |
− | | | + | | style="text-align: right;" | 359.00 |
− | + | | style="text-align: right;" | 0.00 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2018 | ||
+ | | [[M & R INVESTMENTS OHIO LLC]] | ||
+ | | style="text-align: right;" | 104.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | |} |
− | | style="text-align: | + | For data sources see<ref>{{cite web |
− | | | + | | title = Risk Based Data Management System - Production Table - Oil and Gas Data |
− | | | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | | + | | date = 2020-11-16 |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | |
− | + | | accessdate = 2020-11-16 }}</ref> | |
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
|- | |- | ||
+ | | 2001 | ||
+ | | [[OXFORD OIL]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 1506 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2002 |
− | | style="text-align:right;" | | + | | [[OXFORD OIL]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 191 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2003 | ||
+ | | [[OXFORD OIL]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 58 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2004 |
− | | style="text-align:right;" | | + | | [[OXFORD OIL]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 33 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2005 | ||
+ | | [[OXFORD OIL]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 25 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2006 |
− | | style="text-align:right;" | | + | | [[OXFORD OIL]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 36 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2007 | ||
+ | | [[OXFORD OIL]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 26 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2008 |
− | | style="text-align:right;" | | + | | [[OXFORD OIL]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 22 | |
− | + | | style="text-align: right;" | | |
− | | style="text-align:right;" | ||
− | | | ||
|- | |- | ||
+ | | 2009 | ||
+ | | [[OXFORD OIL]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 8 | ||
+ | | style="text-align: right;" | | ||
|- | |- | ||
− | | 2010 | + | | 2010 |
− | | style="text-align:right;" | | + | | [[OXFORD OIL]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 21 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2011 | ||
+ | | [[OXFORD OIL]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 47 | ||
+ | | style="text-align: right;" | | ||
|- | |- | ||
− | | | + | | 2012 |
− | | style="text-align:right;" | | + | | [[OXFORD OIL]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 3 | |
− | + | | style="text-align: right;" | | |
− | | style="text-align:right;" | ||
− | | | ||
|- | |- | ||
+ | | 2013 | ||
+ | | [[ECLIPSE RESOURCES-OHIO LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 2 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2014 |
− | | style="text-align:right;" | | + | | [[ECLIPSE RESOURCES-OHIO LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2015 | ||
+ | | [[ECLIPSE RESOURCES-OHIO LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2016 |
− | | style="text-align:right;" | | + | | [[M & R INVESTMENTS OHIO LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2017 | ||
+ | | [[M & R INVESTMENTS OHIO LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2018 |
− | + | | [[M & R INVESTMENTS OHIO LLC]] | |
− | + | | Brine | |
− | | | + | | style="text-align: right;" | 0 |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | | style="text-align:right;" | 365 | ||
|- | |- | ||
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = Ohio Department of Natural Resources | + | | title = Risk Based Data Management System - Production Table - Brine Data |
− | | | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | ||
− | |||
|- | |- | ||
− | | | + | | -1311785326 |
− | | | + | | 2005-5-5 0:00:0 |
− | | | + | | PW |
+ | | No Violations | ||
| | | | ||
+ | |- | ||
+ | | -151730607 | ||
+ | | 2015-9-8 0:00:0 | ||
+ | | PW | ||
+ | | No Violations | ||
| | | | ||
+ | |- | ||
+ | | -250209884 | ||
+ | | 2012-9-20 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
| | | | ||
+ | |- | ||
+ | | 0151730607 | ||
+ | | 2015-09-08 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | On the day of my inspection I found that the wellhead was equipped with a pumping unit. The motor was intact and the valves were open. The tank battery consisted of one 100 barrel tank, one 20 barrel poly tank, one separator and an earthen dike. Identification was posted and I found no leaks or spills. | ||
+ | |- | ||
+ | | 0250209884 | ||
+ | | 2012-09-20 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | On the day of my inspection I found that the well head was equipped with a pumping unit and connected to a tank battery that consisted of one 100 barrel stock tank, one 30 barrel poly brine tank, one separator and an earthen dike. Proper identification was posted and I found no leaks or spills around the well head or tank battery. This well shares a tank battery with permits 6819 and 6820. No violations at this time. | ||
+ | |- | ||
+ | | 1036432597 | ||
+ | | 2002-11-04 | ||
+ | | Preliminary Restoration | ||
+ | | No Violations | ||
| | | | ||
− | |||
|- | |- | ||
| 1273072201 | | 1273072201 | ||
| 2010-05-05 | | 2010-05-05 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| Well capable of production . | | Well capable of production . | ||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 1311785326 |
− | |||
| 2005-05-05 | | 2005-05-05 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| Well in production . | | Well in production . | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1397499607 | | 1397499607 | ||
| 2014-04-14 | | 2014-04-14 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| I received notification from Eclipse that they had found a flow line leak at this well. When I arrived at the location I met with Dale Smith, who was in charge of the clean up. They shut the well in and identified the leak in the flow line.. The crew installed temporary clamps on the line so they could flush it out with water. There was an estimated one barrel of oil that escaped the flow line. There were two areas approximately 10 ft in diameter where the oil had pooled in a grassy field. I did not observe any contamination beyond those two spots. The crew was in the process of removing all of the contaminated soil and transporting it back to their yard in order to dispose of it at an approved landfill. Dale Smith claimed that they were going to replace the line once they got the soil out of there. I will follow up when he notifies me that the clean up is completed. | | I received notification from Eclipse that they had found a flow line leak at this well. When I arrived at the location I met with Dale Smith, who was in charge of the clean up. They shut the well in and identified the leak in the flow line.. The crew installed temporary clamps on the line so they could flush it out with water. There was an estimated one barrel of oil that escaped the flow line. There were two areas approximately 10 ft in diameter where the oil had pooled in a grassy field. I did not observe any contamination beyond those two spots. The crew was in the process of removing all of the contaminated soil and transporting it back to their yard in order to dispose of it at an approved landfill. Dale Smith claimed that they were going to replace the line once they got the soil out of there. I will follow up when he notifies me that the clean up is completed. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1399295125 | | 1399295125 | ||
| 2014-05-02 | | 2014-05-02 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| On the day of my inspection I found that Eclipse Resources had a crew on location finishing the clean up of the flow line leak. They had the leaks identified and repaired. They were removing the last of the contamination and preparing to restore the affected area. | | On the day of my inspection I found that Eclipse Resources had a crew on location finishing the clean up of the flow line leak. They had the leaks identified and repaired. They were removing the last of the contamination and preparing to restore the affected area. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1399299380 | | 1399299380 | ||
| 2014-05-05 | | 2014-05-05 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| On the day of my inspection I found that the contaminated soil had been removed from the site. All equipment and debris had been removed from the site. The soil was graded out to the approximate original contour. | | On the day of my inspection I found that the contaminated soil had been removed from the site. All equipment and debris had been removed from the site. The soil was graded out to the approximate original contour. | ||
− | |||
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− | |||
− | |||
|- | |- | ||
| 1740748101 | | 1740748101 | ||
| 2014-04-21 | | 2014-04-21 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| On the day of my inspection I found that the well was shut in and the existing flow line had been flushed and clamped. There were no active leaks. There were oil absorbent pads spread around the area in the standing puddles of rain water. The pads were mostly clean. The only water that I found that still showed some oil was down in the ditches where the flow line leaks had been dug up. They had absorbent pads in those puddles as well. The contaminated soil had been removed from the site and there was an earthen berm in place to prevent any residual contamination from escaping the immediate area. | | On the day of my inspection I found that the well was shut in and the existing flow line had been flushed and clamped. There were no active leaks. There were oil absorbent pads spread around the area in the standing puddles of rain water. The pads were mostly clean. The only water that I found that still showed some oil was down in the ditches where the flow line leaks had been dug up. They had absorbent pads in those puddles as well. The contaminated soil had been removed from the site and there was an earthen berm in place to prevent any residual contamination from escaping the immediate area. | ||
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− | |||
|- | |- | ||
| 2108304709 | | 2108304709 | ||
| 2009-08-12 | | 2009-08-12 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| Well capable of production . | | Well capable of production . | ||
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− | |||
− | |||
|- | |- | ||
+ | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
|- | |- | ||
− | | - | + | |}--> |
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For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-031-26823 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Jackson Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: OXFORD-PEABODY | |
License Status: Producing | |
License Date: 2001-03-22 | |
Spud Date: 2001-04-07 | |
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS | |
Final Drill Date: 2001-04-11 | |
Well Total Depth: 3916.00 ft | |
Configuration: Vertical | |
Latitude: 40.260000 | |
Longitude: -81.970000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2001-03-22 | 79 OXFORD OIL COMPANY Proposed Formation CLINTON Issued Date 3/22/01 Expired Date 3/22/02 6:00:00 AM |
Original Spud | 2001-04-07 | RBDMS Rec |
Completed | 2001-04-11 | RBDMS Rec |
Reached Total Depth | 2001-04-11 | RBDMS Rec |
Completion Report Received | 2001-12-10 | RBDMS Rec |
Construction Permit Expires | 2002-03-22 | RBDMS Rec |
Change of Owner | 2014-02-06 | Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC |
Change of Owner | 2016-08-02 | Operator changed from 9216, ECLIPSE RESOURCES-OHIO LLC to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2002-01-25 | 3744 | 3788 | 24 |
3744 | 3788 | 24 | |
3744 | 3788 | 24 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2641 Bbl | 23500 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | OXFORD OIL | 2364.00 | 269.00 | 365 |
2002 | OXFORD OIL | 5237.00 | 253.00 | 365 |
2003 | OXFORD OIL | 3395.00 | 147.00 | 365 |
2004 | OXFORD OIL | 2813.00 | 107.00 | 365 |
2005 | OXFORD OIL | 1717.00 | 61.00 | 365 |
2006 | OXFORD OIL | 1040.00 | 102.00 | 365 |
2007 | OXFORD OIL | 811.00 | 46.00 | 365 |
2008 | OXFORD OIL | 768.00 | 64.00 | 0 |
2009 | OXFORD OIL | 783.00 | 62.00 | 0 |
2010 | MACKENCO INC | 339.00 | 536.00 | 365 |
2011 | OXFORD OIL | 491.00 | 42.00 | 0 |
2012 | OXFORD OIL | 440.00 | 24.00 | 0 |
2013 | ECLIPSE RESOURCES-OHIO LLC | 400.00 | 38.00 | 365 |
2014 | ECLIPSE RESOURCES-OHIO LLC | 748.00 | 41.00 | 365 |
2015 | ECLIPSE RESOURCES-OHIO LLC | 465.00 | 48.00 | 365 |
2016 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
2017 | M & R INVESTMENTS OHIO LLC | 359.00 | 0.00 | 365 |
2018 | M & R INVESTMENTS OHIO LLC | 104.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | OXFORD OIL | Brine | 1506 | 365 |
2002 | OXFORD OIL | Brine | 191 | 365 |
2003 | OXFORD OIL | Brine | 58 | 365 |
2004 | OXFORD OIL | Brine | 33 | 365 |
2005 | OXFORD OIL | Brine | 25 | 365 |
2006 | OXFORD OIL | Brine | 36 | 365 |
2007 | OXFORD OIL | Brine | 26 | 365 |
2008 | OXFORD OIL | Brine | 22 | |
2009 | OXFORD OIL | Brine | 8 | |
2010 | OXFORD OIL | Brine | 21 | 365 |
2011 | OXFORD OIL | Brine | 47 | |
2012 | OXFORD OIL | Brine | 3 | |
2013 | ECLIPSE RESOURCES-OHIO LLC | Brine | 2 | 365 |
2014 | ECLIPSE RESOURCES-OHIO LLC | Brine | 0 | 365 |
2015 | ECLIPSE RESOURCES-OHIO LLC | Brine | 0 | 365 |
2016 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
2017 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1311785326 | 2005-5-5 0:00:0 | PW | No Violations | |
-151730607 | 2015-9-8 0:00:0 | PW | No Violations | |
-250209884 | 2012-9-20 0:00: | PW | No Violations | |
0151730607 | 2015-09-08 | Production Wells | No Violations | On the day of my inspection I found that the wellhead was equipped with a pumping unit. The motor was intact and the valves were open. The tank battery consisted of one 100 barrel tank, one 20 barrel poly tank, one separator and an earthen dike. Identification was posted and I found no leaks or spills. |
0250209884 | 2012-09-20 | Production Wells | No Violations | On the day of my inspection I found that the well head was equipped with a pumping unit and connected to a tank battery that consisted of one 100 barrel stock tank, one 30 barrel poly brine tank, one separator and an earthen dike. Proper identification was posted and I found no leaks or spills around the well head or tank battery. This well shares a tank battery with permits 6819 and 6820. No violations at this time. |
1036432597 | 2002-11-04 | Preliminary Restoration | No Violations | |
1273072201 | 2010-05-05 | Production Wells | No Violations | Well capable of production . |
1311785326 | 2005-05-05 | Production Wells | No Violations | Well in production . |
1397499607 | 2014-04-14 | Production Wells | No Violations | I received notification from Eclipse that they had found a flow line leak at this well. When I arrived at the location I met with Dale Smith, who was in charge of the clean up. They shut the well in and identified the leak in the flow line.. The crew installed temporary clamps on the line so they could flush it out with water. There was an estimated one barrel of oil that escaped the flow line. There were two areas approximately 10 ft in diameter where the oil had pooled in a grassy field. I did not observe any contamination beyond those two spots. The crew was in the process of removing all of the contaminated soil and transporting it back to their yard in order to dispose of it at an approved landfill. Dale Smith claimed that they were going to replace the line once they got the soil out of there. I will follow up when he notifies me that the clean up is completed. |
1399295125 | 2014-05-02 | Production Wells | No Violations | On the day of my inspection I found that Eclipse Resources had a crew on location finishing the clean up of the flow line leak. They had the leaks identified and repaired. They were removing the last of the contamination and preparing to restore the affected area. |
1399299380 | 2014-05-05 | Production Wells | No Violations | On the day of my inspection I found that the contaminated soil had been removed from the site. All equipment and debris had been removed from the site. The soil was graded out to the approximate original contour. |
1740748101 | 2014-04-21 | Production Wells | No Violations | On the day of my inspection I found that the well was shut in and the existing flow line had been flushed and clamped. There were no active leaks. There were oil absorbent pads spread around the area in the standing puddles of rain water. The pads were mostly clean. The only water that I found that still showed some oil was down in the ditches where the flow line leaks had been dug up. They had absorbent pads in those puddles as well. The contaminated soil had been removed from the site and there was an earthen berm in place to prevent any residual contamination from escaping the immediate area. |
2108304709 | 2009-08-12 | Production Wells | No Violations | Well capable of production . |
For data sources see[9]