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Difference between revisions of "34-031-27203"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-031-27203
 
| Well ID: 34-031-27203
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.2400204947, -81.8982970632 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.23, -81.89 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| Country: United States
 
|-
 
|-
| Municipality:
+
| State: Ohio
 
|-
 
|-
| Operator Name:
+
| County: [[Coshocton_County,_Ohio|Coshocton]]
 
|-
 
|-
| Well Pad ID:
+
| Municipality: [[Jackson_Township,_Coshocton_County,_Ohio|Jackson Township]]
 
|-
 
|-
| Farm/Lease Name:
+
| Operator Name: [[JOHN  F WILLIAMS OIL FIELD SER]]
 
|-
 
|-
| First Permit Date:
+
| Well Pad ID:  
 
|-
 
|-
| Last Permit Date:
+
| Farm/Lease Name: MAGNESS ELEANOR
 +
|-
 +
| License Status: Producing
 +
|-
 +
| License Date: 2012-08-16
 
|-
 
|-
 
| Spud Date: 2012-09-11
 
| Spud Date: 2012-09-11
 
|-
 
|-
| Unconventional:
+
| Spud Drilling Contractor: [[MARIC DRILLING CO.]]
 +
|-
 +
| Final Drill Date: 2013-01-12
 +
|-
 +
| Well Total Depth: 4046.00 ft
 +
|-
 +
| Configuration: Vertical
 +
|-
 +
| Latitude: 40.230000
 +
|-
 +
| Longitude: -81.890000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| APP
 +
| 2012-08-16
 +
| Proposed Formations:CLINTON, Issued Date:8/16/2012, Expired Date:8/16/2014 12:00:00 PM, Drilling unit acres:117.26, Proposed Well Type:OG, Proposed Well Class:POOL
 +
|-
 +
| Correction to Well
 +
| 2012-08-24
 +
| CORRECTION TO CASING PROGRAM.
 +
|-
 +
| Reached Total Depth
 +
| 2013-01-12
 +
|
 +
|-
 +
| Completion Report Received
 +
| 2013-02-28
 +
|
 +
|-
 +
| Construction Permit Expires
 +
| 2014-08-16
 +
|
 +
|-
 +
| Record Last Modified
 +
| 2017-02-15
 +
|
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 2013-03-04
 +
| style="text-align: right;" | 3970
 +
| style="text-align: right;" | 3978
 +
| style="text-align: right;" | 25
 
|-
 
|-
| Horizontal:
+
|  
 +
| style="text-align: right;" | 3970
 +
| style="text-align: right;" | 3978
 +
| style="text-align: right;" | 25
 
|-
 
|-
| Producing: No
+
|  
 +
| style="text-align: right;" | 3970
 +
| style="text-align: right;" | 3978
 +
| style="text-align: right;" | 25
 
|-
 
|-
| Violations: 0
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 
|-
 
|-
| Latitude: 40.2400204947
+
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
| Longitude: -81.8982970632
+
|}-->
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
| 2012-10-29
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 1050 Bbl
 +
| style="text-align: right;" | 17500
 +
| [[Universal Well Services Inc.]]
 +
|
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
+
|-
!scope="col" | OIL PRODUCTION DAYS
+
| 2013
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| style="text-align: right;" | 1084.00
 +
| style="text-align: right;" | 332.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2014
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| style="text-align: right;" | 2504.00
 +
| style="text-align: right;" | 151.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2015
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| style="text-align: right;" | 2273.00
 +
| style="text-align: right;" | 67.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2016
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| style="text-align: right;" | 2634.00
 +
| style="text-align: right;" | 112.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2017
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| style="text-align: right;" | 2130.00
 +
| style="text-align: right;" | 108.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2018
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| style="text-align: right;" | 2068.00
 +
| style="text-align: right;" | 71.00
 +
| style="text-align: right;" | 365
 +
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
{| class="wikitable sortable" width="95%"
+
{| class="wikitable sortable"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | TYPE
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | QUANTITY
+
!scope="col" style="text-align: center"| Waste Type
!scope="col" | UNITS
+
!scope="col" style="text-align: center"| Quantity (bbl)
!scope="col" | DISPOSAL METHOD
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | WASTE FACILITY PERMIT ID
+
|-
!scope="col" | WASTE FACILITY NAME
+
| 2013
!scope="col" | FACILITY CITY
+
| [[JOHN  F WILLIAMS OIL FIELD SER]]
!scope="col" | FACILITY STATE
+
| Brine
 +
| style="text-align: right;" | 22
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2014
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2015
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2016
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2017
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2018
 +
| [[JOHN  F WILLIAMS OIL FIELD SER]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
 
| -108808592
 
| -108808592
| 2012-09-11
+
| 2012-9-11 0:00:
|
+
| DD
| On the day of my inspection I found that Maric Drilling  was drilling on fluid at a depth of 384'. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
+
| No Violations
|
+
|  
|
 
|
 
|-
 
 
|-
 
|-
 
| -1186098361
 
| -1186098361
| 2012-09-12
+
| 2012-9-12 0:00:
|
+
| DD
| On the day of my inspection Petroset started pumping cement down the annulus of the 8.625" casing and 11" hole. The annulus bridged off within 5 minutes of starting the job. Attempts were made to clear the bridge, but were unsuccessful. Appalachian Well Surveys ran a bond log, which showed that there was good cement bond from 672' to 98'. Petroset conducted a pressure test of the casing at 300 psi for 30 minutes. The casing passed the pressure test and Maric Drilling was cleared to continue drilling. They will attempt to cement the remaining 98' of open 8.625" casing at a later stage in well construction.
+
| No Violations
|
+
|  
|
 
|
 
|-
 
 
|-
 
|-
 
| -1717091810
 
| -1717091810
| 2012-09-11
+
| 2012-9-11 0:00:
|
+
| DD
| On the day of my inspection I found that Maric Drilling drilled an 11" surface hole on fluid to 732'. They ran 8.625" casing to 672'. The hole was circulating with the mud pump when I arrived. Petroset broke circulation, pumped 400 lbs. gel, 100 lbs cotton seed hulls and 260 sack of class A cement. Good circulation was maintained throughout the job and cement was circulated to surface. When Petroset stopped pumping the cement immediately fell down the hole. The height of the cement could not be determined from surface. A collective decision was made to let the cement set overnight and come back in 8 hours to fill from the surface.
+
| No Violations
|
+
|  
|
 
|
 
|-
 
 
|-
 
|-
 
| -1822336479
 
| -1822336479
| 2013-07-03
+
| 2013-7-3 0:00:0
|
+
| PL
| On the day of my inspection I found that the well site was graded out and 90% covered with well established grasses and field vegetation. The leases road was graveled all the way back to the well. The well head was equipped with a pumping unit and connected to a tank battery that consisted of one 210 barrel stock tank, one 100 barrel brine tank, one separator and an earthen dike. Proper identification was posted and there were no leaks or spills. This well site passes preliminary restoration.
+
| No Violations
|
+
|  
|
 
|
 
|-
 
 
|-
 
|-
 
| -2075161272
 
| -2075161272
| 2012-09-14
+
| 2012-9-14 0:00:
|
+
| DD
| On the day of my inspection I found that Maric Drilling  was drilling on fluid at a depth of 2180'. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
+
| No Violations
|
+
|  
|
 
|
 
 
|-
 
|-
 +
| -2114814888
 +
| 2016-5-23 0:00:
 +
| PW
 +
| No Violations
 +
| 0.50
 
|-
 
|-
 
| -956584276
 
| -956584276
 +
| 2012-10-16 0:00
 +
| DD
 +
| No Violations
 +
|
 +
|-
 +
| 0108808592
 +
| 2012-09-11
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| On the day of my inspection I found that Maric Drilling  was drilling on fluid at a depth of 384. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
 +
|-
 +
| 0255013535
 +
| 2012-09-18
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| On the day of my inspection Maric Drilling ran 4.5 casing to 4033 cemented with 140 sacks class A by Petroset. Good circulation was maintained throughout the job. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
 +
|-
 +
| 0956584276
 
| 2012-10-16
 
| 2012-10-16
|
+
| Drill / Deepen /  Reopen
| On the day of my inspection I found that sack cement had been mixed and poured down the annulus of the 8.625" casing and 11" hole to fill it to surface from the bridge depth of approximately 20'. The pits were still open and there were no sags or tears in the pit liners.
+
| No Violations
|
+
| On the day of my inspection I found that sack cement had been mixed and poured down the annulus of the 8.625 casing and 11 hole to fill it to surface from the bridge depth of approximately 20. The pits were still open and there were no sags or tears in the pit liners.
|
 
|
 
 
|-
 
|-
 +
| 1186098361
 +
| 2012-09-12
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| On the day of my inspection Petroset started pumping cement down the annulus of the 8.625 casing and 11 hole. The annulus bridged off within 5 minutes of starting the job. Attempts were made to clear the bridge, but were unsuccessful. Appalachian Well Surveys ran a bond log, which showed that there was good cement bond from 672 to 98. Petroset conducted a pressure test of the casing at 300 psi for 30 minutes. The casing passed the pressure test and Maric Drilling was cleared to continue drilling. They will attempt to cement the remaining 98 of open 8.625 casing at a later stage in well construction.
 
|-
 
|-
 
| 1346962127
 
| 1346962127
 
| 2012-09-06
 
| 2012-09-06
|
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| On the day of my inspection I found that the location had been excavated and the pits were dug. No drilling equipment was on location.
 
| On the day of my inspection I found that the location had been excavated and the pits were dug. No drilling equipment was on location.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1348242902
 
| 1348242902
 
| 2012-09-17
 
| 2012-09-17
|
+
| Drill / Deepen /  Reopen
| On the day of my inspection I found that Maric Drilling  was drilling on fluid at a depth of 3671'. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
+
| No Violations
|
+
| On the day of my inspection I found that Maric Drilling  was drilling on fluid at a depth of 3671. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1349106227
 
| 1349106227
 
| 2012-09-24
 
| 2012-09-24
|
+
| Drill / Deepen /  Reopen
| On the day of my inspection I found that the pit were still open. The fluid level was approximately 18" from surface and there were no sags or tears in the pit liners. The well head was shut in with a 4.5" bull plug, and there were no leaks or spills. The drilling rig was no longer on location. Some drilling equipment remained.
+
| No Violations
|
+
| On the day of my inspection I found that the pit were still open. The fluid level was approximately 18 from surface and there were no sags or tears in the pit liners. The well head was shut in with a 4.5 bull plug, and there were no leaks or spills. The drilling rig was no longer on location. Some drilling equipment remained.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1483704917
 
| 1483704917
 
| 2012-09-10
 
| 2012-09-10
|
+
| Drill / Deepen /  Reopen
| On the day of my inspection I found that Maric Drilling was rigged up, the pits and flow ditch were lined, and there was new 8.625" casing on the rack. The permit was in the doghouse and there were no leaks or spills. The well was not spudded at the time of my inspection.
+
| No Violations
|
+
| On the day of my inspection I found that Maric Drilling was rigged up, the pits and flow ditch were lined, and there was new 8.625 casing on the rack. The permit was in the doghouse and there were no leaks or spills. The well was not spudded at the time of my inspection.
|
 
|
 
 
|-
 
|-
 +
| 1717091810
 +
| 2012-09-11
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| On the day of my inspection I found that Maric Drilling drilled an 11 surface hole on fluid to 732. They ran 8.625 casing to 672. The hole was circulating with the mud pump when I arrived. Petroset broke circulation, pumped 400 lbs. gel, 100 lbs cotton seed hulls and 260 sack of class A cement. Good circulation was maintained throughout the job and cement was circulated to surface. When Petroset stopped pumping the cement immediately fell down the hole. The height of the cement could not be determined from surface. A collective decision was made to let the cement set overnight and come back in 8 hours to fill from the surface.
 +
|-
 +
| 1822336479
 +
| 2013-07-03
 +
| Preliminary Restoration
 +
| No Violations
 +
| On the day of my inspection I found that the well site was graded out and 90% covered with well established grasses and field vegetation. The leases road was graveled all the way back to the well. The well head was equipped with a pumping unit and connected to a tank battery that consisted of one 210 barrel stock tank, one 100 barrel brine tank, one separator and an earthen dike. Proper identification was posted and there were no leaks or spills. This well site passes preliminary restoration.
 +
|-
 +
| 1944010015
 +
| 2020-1-8 0:00:0
 +
| PW
 +
| No Violations
 +
| 0.40
 +
|-
 +
| 2075161272
 +
| 2012-09-14
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| On the day of my inspection I found that Maric Drilling  was drilling on fluid at a depth of 2180. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
 +
|-
 +
| 2114814888
 +
| 2016-05-23
 +
| Production Wells
 +
| No Violations
 +
| On the day of my inspection I found that the well was being produced with an electric powered pumping unit. The valves were open on the tubing and casing lines. The gauges showed 25 psi. gas pressure. The tank battery consisted of one 210 barrel steel tank, one 100 barrel steel tank, one vertical separator and meter box. An earthen dike was in place around the production equipment. Identification was posted at the tank battery. I found no leaks or spills at the wellhead or production equipment.
 
|-
 
|-
 
| 255013535
 
| 255013535
| 2012-09-18
+
| 2012-9-18 0:00:
|
+
| DD
| On the day of my inspection Maric Drilling ran 4.5" casing to 4033' cemented with 140 sacks class A by Petroset. Good circulation was maintained throughout the job. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
+
| No Violations
|
+
|  
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 06:22, 12 January 2021

Well Details

Well ID: 34-031-27203
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Country: United States
State: Ohio
County: Coshocton
Municipality: Jackson Township
Operator Name: JOHN F WILLIAMS OIL FIELD SER
Well Pad ID:
Farm/Lease Name: MAGNESS ELEANOR
License Status: Producing
License Date: 2012-08-16
Spud Date: 2012-09-11
Spud Drilling Contractor: MARIC DRILLING CO.
Final Drill Date: 2013-01-12
Well Total Depth: 4046.00 ft
Configuration: Vertical
Latitude: 40.230000
Longitude: -81.890000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2012-08-16 Proposed Formations:CLINTON, Issued Date:8/16/2012, Expired Date:8/16/2014 12:00:00 PM, Drilling unit acres:117.26, Proposed Well Type:OG, Proposed Well Class:POOL
Correction to Well 2012-08-24 CORRECTION TO CASING PROGRAM.
Reached Total Depth 2013-01-12
Completion Report Received 2013-02-28
Construction Permit Expires 2014-08-16
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2013-03-04 3970 3978 25
3970 3978 25
3970 3978 25

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2012-10-29 H2O 15 1050 Bbl 17500 Universal Well Services Inc.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 JOHN F WILLIAMS OIL FIELD SER 1084.00 332.00 365
2014 JOHN F WILLIAMS OIL FIELD SER 2504.00 151.00 365
2015 JOHN F WILLIAMS OIL FIELD SER 2273.00 67.00 365
2016 JOHN F WILLIAMS OIL FIELD SER 2634.00 112.00 365
2017 JOHN F WILLIAMS OIL FIELD SER 2130.00 108.00 365
2018 JOHN F WILLIAMS OIL FIELD SER 2068.00 71.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 JOHN F WILLIAMS OIL FIELD SER Brine 22 365
2014 JOHN F WILLIAMS OIL FIELD SER Brine 0 365
2015 JOHN F WILLIAMS OIL FIELD SER Brine 0 365
2016 JOHN F WILLIAMS OIL FIELD SER Brine 0 365
2017 JOHN F WILLIAMS OIL FIELD SER Brine 0 365
2018 JOHN F WILLIAMS OIL FIELD SER Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-108808592 2012-9-11 0:00: DD No Violations
-1186098361 2012-9-12 0:00: DD No Violations
-1717091810 2012-9-11 0:00: DD No Violations
-1822336479 2013-7-3 0:00:0 PL No Violations
-2075161272 2012-9-14 0:00: DD No Violations
-2114814888 2016-5-23 0:00: PW No Violations 0.50
-956584276 2012-10-16 0:00 DD No Violations
0108808592 2012-09-11 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Maric Drilling was drilling on fluid at a depth of 384. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
0255013535 2012-09-18 Drill / Deepen / Reopen No Violations On the day of my inspection Maric Drilling ran 4.5 casing to 4033 cemented with 140 sacks class A by Petroset. Good circulation was maintained throughout the job. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
0956584276 2012-10-16 Drill / Deepen / Reopen No Violations On the day of my inspection I found that sack cement had been mixed and poured down the annulus of the 8.625 casing and 11 hole to fill it to surface from the bridge depth of approximately 20. The pits were still open and there were no sags or tears in the pit liners.
1186098361 2012-09-12 Drill / Deepen / Reopen No Violations On the day of my inspection Petroset started pumping cement down the annulus of the 8.625 casing and 11 hole. The annulus bridged off within 5 minutes of starting the job. Attempts were made to clear the bridge, but were unsuccessful. Appalachian Well Surveys ran a bond log, which showed that there was good cement bond from 672 to 98. Petroset conducted a pressure test of the casing at 300 psi for 30 minutes. The casing passed the pressure test and Maric Drilling was cleared to continue drilling. They will attempt to cement the remaining 98 of open 8.625 casing at a later stage in well construction.
1346962127 2012-09-06 Drill / Deepen / Reopen No Violations On the day of my inspection I found that the location had been excavated and the pits were dug. No drilling equipment was on location.
1348242902 2012-09-17 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Maric Drilling was drilling on fluid at a depth of 3671. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
1349106227 2012-09-24 Drill / Deepen / Reopen No Violations On the day of my inspection I found that the pit were still open. The fluid level was approximately 18 from surface and there were no sags or tears in the pit liners. The well head was shut in with a 4.5 bull plug, and there were no leaks or spills. The drilling rig was no longer on location. Some drilling equipment remained.
1483704917 2012-09-10 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Maric Drilling was rigged up, the pits and flow ditch were lined, and there was new 8.625 casing on the rack. The permit was in the doghouse and there were no leaks or spills. The well was not spudded at the time of my inspection.
1717091810 2012-09-11 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Maric Drilling drilled an 11 surface hole on fluid to 732. They ran 8.625 casing to 672. The hole was circulating with the mud pump when I arrived. Petroset broke circulation, pumped 400 lbs. gel, 100 lbs cotton seed hulls and 260 sack of class A cement. Good circulation was maintained throughout the job and cement was circulated to surface. When Petroset stopped pumping the cement immediately fell down the hole. The height of the cement could not be determined from surface. A collective decision was made to let the cement set overnight and come back in 8 hours to fill from the surface.
1822336479 2013-07-03 Preliminary Restoration No Violations On the day of my inspection I found that the well site was graded out and 90% covered with well established grasses and field vegetation. The leases road was graveled all the way back to the well. The well head was equipped with a pumping unit and connected to a tank battery that consisted of one 210 barrel stock tank, one 100 barrel brine tank, one separator and an earthen dike. Proper identification was posted and there were no leaks or spills. This well site passes preliminary restoration.
1944010015 2020-1-8 0:00:0 PW No Violations 0.40
2075161272 2012-09-14 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Maric Drilling was drilling on fluid at a depth of 2180. The permit was on display in the doghouse, there were no sags or tears in the pit liners and there were no leaks or spills.
2114814888 2016-05-23 Production Wells No Violations On the day of my inspection I found that the well was being produced with an electric powered pumping unit. The valves were open on the tubing and casing lines. The gauges showed 25 psi. gas pressure. The tank battery consisted of one 210 barrel steel tank, one 100 barrel steel tank, one vertical separator and meter box. An earthen dike was in place around the production equipment. Identification was posted at the tank battery. I found no leaks or spills at the wellhead or production equipment.
255013535 2012-9-18 0:00: DD No Violations

For data sources see[9]

References