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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-073-20388 | | Well ID: 34-073-20388 | ||
− | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39. | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.49, -82.62 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 11: | Line 11: | ||
| County: [[Hocking_County,_Ohio|Hocking]] | | County: [[Hocking_County,_Ohio|Hocking]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Laurel_Township,_Hocking_County,_Ohio|Laurel Township]] |
|- | |- | ||
| Operator Name: [[COLUMBIA GAS TRANSMISSION LLC]] | | Operator Name: [[COLUMBIA GAS TRANSMISSION LLC]] | ||
Line 21: | Line 21: | ||
| License Status: Plugged and Abandoned | | License Status: Plugged and Abandoned | ||
|- | |- | ||
− | | License Date: | + | | License Date: 2018-08-20 |
|- | |- | ||
| Spud Date: 1953-07-29 | | Spud Date: 1953-07-29 | ||
Line 29: | Line 29: | ||
| Final Drill Date: 1953-09-29 | | Final Drill Date: 1953-09-29 | ||
|- | |- | ||
− | | Well Total Depth: 2071 ft | + | | Well Total Depth: 2071.00 ft |
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Latitude: 39. | + | | Latitude: 39.490000 |
|- | |- | ||
− | | Longitude: -82. | + | | Longitude: -82.620000 |
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Well History == | == Well History == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 85: | Line 85: | ||
| title = Risk Based Data Management System - Well and WellHistry Tables | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
<!--== Perforation Treatments == | <!--== Perforation Treatments == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 157: | Line 157: | ||
!scope="col" style="text-align: center"| Inspection Result | !scope="col" style="text-align: center"| Inspection Result | ||
!scope="col" style="text-align: center"| Inspection Comments | !scope="col" style="text-align: center"| Inspection Comments | ||
+ | |- | ||
+ | | -1264179256 | ||
+ | | 2014-12-12 0:00 | ||
+ | | SO | ||
+ | | No Violations | ||
+ | | 0.50 | ||
+ | |- | ||
+ | | -1749424166 | ||
+ | | 2018-12-3 0:00: | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 1.30 | ||
+ | |- | ||
+ | | -20620938 | ||
+ | | 2017-8-4 0:00:0 | ||
+ | | SO | ||
+ | | No Violations | ||
+ | | 0.80 | ||
+ | |- | ||
+ | | -2077984764 | ||
+ | | 2014-1-3 0:00:0 | ||
+ | | SO | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -323204915 | ||
+ | | 2016-10-4 0:00: | ||
+ | | SO | ||
+ | | No Violations | ||
+ | | 0.30 | ||
|- | |- | ||
| 0020620938 | | 0020620938 | ||
Line 205: | Line 235: | ||
| No Violations | | No Violations | ||
| During the inspection a bond log was conducted on the 5 inch casing. The bond log showed cement up to 1200 feet on the backside of the 5 inch casing. Time of inspection: 10:50 AM. | | During the inspection a bond log was conducted on the 5 inch casing. The bond log showed cement up to 1200 feet on the backside of the 5 inch casing. Time of inspection: 10:50 AM. | ||
+ | |- | ||
+ | | 1567516838 | ||
+ | | 2019-8-29 0:00: | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 0.30 | ||
|- | |- | ||
| 1749424166 | | 1749424166 | ||
Line 217: | Line 253: | ||
| No Violations | | No Violations | ||
| Storage well inspection, no violations noted. | | Storage well inspection, no violations noted. | ||
+ | |- | ||
+ | | 471956518 | ||
+ | | 2018-8-9 0:00:0 | ||
+ | | SO | ||
+ | | No Violations | ||
+ | | 0.30 | ||
+ | |- | ||
+ | | 548290580 | ||
+ | | 2018-12-5 0:00: | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 0.50 | ||
|- | |- | ||
|} | |} | ||
Line 231: | Line 279: | ||
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
==References== | ==References== | ||
<references/> | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Ohio Wells]] | [[Category:Ohio Wells]] |
Well ID: 34-073-20388 | Loading map...
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Country: United States | |
State: Ohio | |
County: Hocking | |
Municipality: Laurel Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: LILLIAM K EDWARDS #1 | |
License Status: Plugged and Abandoned | |
License Date: 2018-08-20 | |
Spud Date: 1953-07-29 | |
Spud Drilling Contractor: | |
Final Drill Date: 1953-09-29 | |
Well Total Depth: 2071.00 ft | |
Configuration: Vertical | |
Latitude: 39.490000 | |
Longitude: -82.620000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1953-07-29 | STORAGE, GL=841.2 |
Completed | 1953-09-29 | STORAGE, GL=841.2 |
Reached Total Depth | 1953-09-29 | STORAGE, GL=841.2 |
Change of Owner | 2011-08-17 | Operator changed from 9998, HISTORIC OWNER to 22, COLUMBIA GAS TRANSMISSION |
APP | 2018-08-20 | Proposed Formations:CLINTON SANDSTONE, Issued Date:8/20/2018, Expired Date:8/19/2020 12:00:00 PM, Drilling unit acres:99, Proposed Well Type:SO, Proposed Well Class: |
Plugged/Abandoned | 2018-12-10 | STORAGE, GL=841.2 |
Record Last Modified | 2019-05-10 | STORAGE, GL=841.2 |
Construction Permit Expires | 2020-08-19 | STORAGE, GL=841.2 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1264179256 | 2014-12-12 0:00 | SO | No Violations | 0.50 |
-1749424166 | 2018-12-3 0:00: | PB | No Violations | 1.30 |
-20620938 | 2017-8-4 0:00:0 | SO | No Violations | 0.80 |
-2077984764 | 2014-1-3 0:00:0 | SO | No Violations | 1.00 |
-323204915 | 2016-10-4 0:00: | SO | No Violations | 0.30 |
0020620938 | 2017-08-04 | Storage Well | No Violations | Columbia Gas storage well inspection. The well consists of a wellhead and a drip. Legible identification on wellhead, no violations noted, GPS was taken on day of inspection. |
0323204915 | 2016-10-04 | Storage Well | No Violations | Storage well inspection. The well consists of a well head and separator. There was a legible and accurate identification. No violations noted. |
0471956518 | 2018-08-09 | Storage Well | No Violations | I conducted a storage well inspection on this well today. I observed identification at the well. I did not observe any violations. Time of inspection: 1:30 PM. Weather: 75 degrees F, Sunny |
0548290580 | 2018-12-05 | Plug / Plug Back | No Violations | I witnessed plugging operations on this well. Kilbarger ran 1,400 feet of 2.38 inch drill pipe in the well. Petroset Cementing pumped 37 sacks of Class A cement through drill pipe. The 5.5 inch casing was perforated on 12/4/2018 from 1,203 feet to 1,200 feet. Kilbarger pulled 200 feet of drill pipe to the perforated zone and Petroset squeezed 2 barrels of cement on the backside of the 5.5 inch casing. Dan Talbot was on location for Columbia Gas Transmission. Refer to plug report for details. Time of inspection: 11:50 AM. |
1049944927 | 2015-08-31 | Storage Well | No Violations | Storage well inspection. Legible well identification found at well. No violations found on date of inspection. |
1122678269 | 2017-07-31 | Storage Well | No Violations | Columbia Gas storage well inspection. The well consists of a wellhead and a drip. Legible identification on wellhead, no violations noted, GPS was taken on day of inspection. |
1264179256 | 2014-12-12 | Storage Well | No Violations | This is the yearly field inspection for this storage well. There are no violations to note at this time. The well appears to be in working order. The identification is legible and is located at the well. |
1544015819 | 2018-12-04 | Plug / Plug Back | No Violations | During the inspection a bond log was conducted on the 5 inch casing. The bond log showed cement up to 1200 feet on the backside of the 5 inch casing. Time of inspection: 10:50 AM. |
1567516838 | 2019-8-29 0:00: | FR | No Violations | 0.30 |
1749424166 | 2018-12-03 | Plug / Plug Back | No Violations | I witnessed plugging operations on this well today. Kilbarger Drilling was contracted to plug the well with cement. Dan Talbot was on location for Columbia Gas Transmission. Refer to the plug report for details. Time of inspection: 12:45 PM. Weather: 38 degrees F, Overcast |
2077984764 | 2014-01-03 | Storage Well | No Violations | Storage well inspection, no violations noted. |
471956518 | 2018-8-9 0:00:0 | SO | No Violations | 0.30 |
548290580 | 2018-12-5 0:00: | PB | No Violations | 0.50 |
For data sources see[3]