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Difference between revisions of "37-131-20187"

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[[Category:Wells]]

Revision as of 18:07, 29 June 2014

Well Details

Well ID: 37-131-20187
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County: Wyoming
Municipality: Washington Township
Operator Name: CARRIZO (MARCELLUS) LLC
Well Pad ID: 145314
Farm/Lease Name: MAZZARA 5H
First Permit Date: 2011-07-12
Last Permit Date: 2011-07-12
Spud Date: 2011-08-17
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: None
Latitude: 41.621427
Longitude: -75.99468

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1990315 2011-07-26 No Violations Noted
2038879 2012-02-01 No Violations Noted
2090795 2012-08-07 No Violations Noted Nabors M 61, Conp. Man - Skip McClelland, @ 7354'

1132' Hole wet 5694' Tully 5800' Hamilton Only drilled 120' since started, having problems with curve. Discussed need to build berms.

2117809 2012-11-26 No Violations Noted
2125665 2012-12-13 Pending Checking well for gas, due to nearby water complaint. Carrizo reps on site - Gary Byron, Jesse Bonnice, & Tom Weller. Have a water truck on site to flood cellars.

20 x 13 3/8" annulus - cement return line - no bubbles. 13 3/8 x 9 5/8" annulus - open holes in landing collar - no bubbles. 9 5/8 x 5 1/2" annulus vent(cement return line) - > 10% methane and > 100% LEL combust. Eric Rooney took isotopic sample.

2137279 2013-01-24 No Violations Noted Stone rig, Comp Man - Larry Giraud not on site at present, talked to Stone tool pusher

Rig is on site cleaning out hole and perfing in prep for frac, which should start in the beginning of Feb. Rig has 2 more wells to go, should finish next week. Containment is good, frac tanks, etc not on site yet.

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-2 DRILL CUTTINGS 1004.23 Tons LANDFILL 301626 WHITE PINES LANDFILL MILLVILLE PA
2012-1 DRILL CUTTINGS 1290.0 Tons LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH

References