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Difference between revisions of "34-127-20550"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-127-20550
 
| Well ID: 34-127-20550
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.80802386, -82.19827283 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.8, -82.19 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Perry County, Ohio|Perry]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[JEANIE ENTERPISES LLC]]
+
| County: [[Perry_County,_Ohio|Perry]]
 +
|-
 +
| Municipality: [[Clayton_Township,_Perry_County,_Ohio|Clayton Township]]
 +
|-
 +
| Operator Name: [[JEANIE ENTERPRISES LLC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: KEFFER-HUMPHREY
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date:  
 
|-
 
|-
 
| Spud Date: 1944-01-10
 
| Spud Date: 1944-01-10
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1944-02-15
 +
|-
 +
| Well Total Depth: 3369.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 39.800000
 
|-
 
|-
| Violations: 0
+
| Longitude: -82.190000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Latitude: 39.80802386
+
| Original Spud
 +
| 1944-01-10
 +
| GL=992.9
 
|-
 
|-
| Longitude: -82.19827283
+
| Completed
 +
| 1944-02-15
 +
| GL=992.9
 +
|-
 +
| Reached Total Depth
 +
| 1944-02-15
 +
| GL=992.9
 +
|-
 +
| Change of Owner
 +
| 2007-08-30
 +
| Operator changed from 456, SCHMELZER MARK to 8268, JEANIE ENTERPISES LLC
 +
|-
 +
| Record Last Modified
 +
| 2013-10-03
 +
| GL=992.9
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 1995-0
+
| 1995
| style="text-align:right;" | 0.0
+
| [[SCHMELZER MARK]]
|  
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 316.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 316.0
+
|-
|  
+
| 1996
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 551.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1997
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 563.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1998
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 406.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 239.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 307.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 385.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2002
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 235.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2003
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 158.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2004
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 240.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2005
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 159.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 2006
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 489.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1996-0
+
| 2007
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 329.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 551.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 313.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1997-0
+
| 2009
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 247.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 563.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 150.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 2011
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 169.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 406.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 73.00
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 1999-0
+
| 2013
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 150.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 239.0
 
|
 
 
|-
 
|-
 +
| 2014
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 205.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 2015
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 77.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 307.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 174.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 2017
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|  
+
| style="text-align: right;" | 15.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 385.0
 
|
 
 
|-
 
|-
 +
| 2018
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 14.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
|}
| style="text-align:right;" | 0.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2020-11-16
| style="text-align:right;" | 235.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1995
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 1996
| style="text-align:right;" | 0.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 158.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2004-0
+
| 1998
| style="text-align:right;" | 0.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 240.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 2000
| style="text-align:right;" | 0.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 159.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2006-0
+
| 2002
| style="text-align:right;" | 0.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 489.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2007-0
+
| 2004
| style="text-align:right;" | 0.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 329.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2006
| style="text-align:right;" | 0.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 313.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 2008
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 247.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" |
 
|-
 
|-
| 2010-0
+
| 2010
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 150.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2011-0
+
| 2012
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 366
| style="text-align:right;" | 169.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| Brine
 +
| style="text-align: right;" | 115
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2012-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 73.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2013-0
+
| 2016
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 150.0
 
|
 
 
|-
 
|-
 +
| 2017
 +
| [[JEANIE ENTERPRISES LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2014-0
+
| 2018
| style="text-align:right;" | 0.0
+
| [[JEANIE ENTERPRISES LLC]]
| style="text-align:right;" | 365.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 205.0
 
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| -13564100
 +
| 2013-3-26 0:00:
 +
| PW
 +
| No Violations
 +
| 1.00
 +
|-
 +
| -1454401861
 +
| 2013-6-14 0:00:
 +
| PW
 +
| No Violations
 +
| 1.00
 
|-
 
|-
| 1210526727
+
| -1514553077
| 2013-03-26
+
| 2013-4-2 0:00:0
|
+
| PW
| During the inspection of this well I found oil around the unit. The plastic flow line was disconnected and the oil pumped on the ground. All the oil will need removed along with the contaminated soil. This well also needs to have identification on it.
+
| No Violations
|  
+
| 1.00
|  
 
|  
 
 
|-
 
|-
 +
| -2014600014
 +
| 2013-4-11 0:00:
 +
| PW
 +
| No Violations
 +
| 2.00
 
|-
 
|-
| -13564100
+
| 0013564100
 
| 2013-03-26
 
| 2013-03-26
|  
+
| Production Wells
 +
| No Violations
 
| This well is capable of production. It has a pumping unit on it with rods and tubing. There is no identification at the well or the tank. Oil was all over the ground around the unit. I talked with a Jennifer from Jeanie Enterprises and they are going to get somebody over there right away. I will do a follow up first thing in the morning.
 
| This well is capable of production. It has a pumping unit on it with rods and tubing. There is no identification at the well or the tank. Oil was all over the ground around the unit. I talked with a Jennifer from Jeanie Enterprises and they are going to get somebody over there right away. I will do a follow up first thing in the morning.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1210526727
 +
| 2013-03-26
 +
| Production Wells
 +
| Violations Noted
 +
| During the inspection of this well I found oil around the unit. The plastic flow line was disconnected and the oil pumped on the ground. All the oil will need removed along with the contaminated soil. This well also needs to have identification on it.
 
|-
 
|-
 
| 1364466253
 
| 1364466253
 
| 2013-03-27
 
| 2013-03-27
|  
+
| Production Wells
 +
| No Violations
 
| I did a follow up on this well to make sure they started the clean-up. I tried to call them and got no answer. I showed up at the well and there was no one there. It was around 8:30 in the morning. They started the clean-up the day before. They put down straw and peat moss to soak up the oil. They had a water pump to pump oil to the tank. I took pics of the location. I will go back tomorrow to check on progress.
 
| I did a follow up on this well to make sure they started the clean-up. I tried to call them and got no answer. I showed up at the well and there was no one there. It was around 8:30 in the morning. They started the clean-up the day before. They put down straw and peat moss to soak up the oil. They had a water pump to pump oil to the tank. I took pics of the location. I will go back tomorrow to check on progress.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1454401861
| -1454401861
 
 
| 2013-06-14
 
| 2013-06-14
|  
+
| Production Wells
 +
| No Violations
 
| I inspected this location to see if everything had been done. The location had been reclaimed, the dike has been put around the tanks and the identification is located on the tank and the well. This well is now in-compliance.
 
| I inspected this location to see if everything had been done. The location had been reclaimed, the dike has been put around the tanks and the identification is located on the tank and the well. This well is now in-compliance.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1514553077
| -1514553077
 
 
| 2013-04-02
 
| 2013-04-02
|  
+
| Production Wells
 +
| No Violations
 
| I did a follow up on this well. All of the heavy oil and contaminated soil have been removed. There are still pads on location to clean up small spots. There was no one on location during time of inspection.
 
| I did a follow up on this well. All of the heavy oil and contaminated soil have been removed. There are still pads on location to clean up small spots. There was no one on location during time of inspection.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1905872786
 
| 1905872786
 
| 2013-03-28
 
| 2013-03-28
|  
+
| Production Wells
 +
| No Violations
 
| I went to see how the clean-up of the oil was going. They put down gravel back the lane to the well. They have a track-o there to remove contaminated soil with a dump truck. They have been putting down diapers to soak up oil. I will check back in a couple days. Everything looks to be going good as of now.
 
| I went to see how the clean-up of the oil was going. They put down gravel back the lane to the well. They have a track-o there to remove contaminated soil with a dump truck. They have been putting down diapers to soak up oil. I will check back in a couple days. Everything looks to be going good as of now.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 2014600014
| -2014600014
 
 
| 2013-04-11
 
| 2013-04-11
|  
+
| Production Wells
 +
| No Violations
 
| I went and checked on how the clean-up has come along. The contaminated soil has all been removed. It just needs to be straightened back up now. I stopped over at Jeanie Enterprises office and let them no.
 
| I went and checked on how the clean-up has come along. The contaminated soil has all been removed. It just needs to be straightened back up now. I stopped over at Jeanie Enterprises office and let them no.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 1210526727
 +
| US-OH-105487
 +
| 2014-04-23
 
|  
 
|  
 +
| Well operation causing pollution and contamination
 +
|-
 +
| 1210526727
 +
| US-OH-105488
 +
| 2014-04-23
 
|  
 
|  
 +
| Well insufficiently equipped to prevent escape of oil and gas
 +
|-
 +
| 1210526727
 +
| US-OH-105489
 +
| 2014-04-23
 
|  
 
|  
 +
| Failure to legibly identify well
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 09:33, 12 January 2021

Well Details

Well ID: 34-127-20550
Loading map...
Country: United States
State: Ohio
County: Perry
Municipality: Clayton Township
Operator Name: JEANIE ENTERPRISES LLC
Well Pad ID:
Farm/Lease Name: KEFFER-HUMPHREY
License Status: Producing
License Date:
Spud Date: 1944-01-10
Spud Drilling Contractor:
Final Drill Date: 1944-02-15
Well Total Depth: 3369.00 ft
Configuration: Vertical
Latitude: 39.800000
Longitude: -82.190000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1944-01-10 GL=992.9
Completed 1944-02-15 GL=992.9
Reached Total Depth 1944-02-15 GL=992.9
Change of Owner 2007-08-30 Operator changed from 456, SCHMELZER MARK to 8268, JEANIE ENTERPISES LLC
Record Last Modified 2013-10-03 GL=992.9

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1995 SCHMELZER MARK 0.00 316.00 365
1996 SCHMELZER MARK 0.00 551.00 365
1997 SCHMELZER MARK 0.00 563.00 365
1998 SCHMELZER MARK 0.00 406.00 365
1999 SCHMELZER MARK 0.00 239.00 365
2000 SCHMELZER MARK 0.00 307.00 365
2001 SCHMELZER MARK 0.00 385.00 365
2002 SCHMELZER MARK 0.00 235.00 365
2003 SCHMELZER MARK 0.00 158.00 365
2004 SCHMELZER MARK 0.00 240.00 365
2005 SCHMELZER MARK 0.00 159.00 365
2006 SCHMELZER MARK 0.00 489.00 365
2007 JEANIE ENTERPRISES LLC 0.00 329.00 365
2008 JEANIE ENTERPRISES LLC 0.00 313.00 365
2009 JEANIE ENTERPRISES LLC 0.00 247.00 0
2010 JEANIE ENTERPRISES LLC 0.00 150.00 365
2011 JEANIE ENTERPRISES LLC 0.00 169.00 365
2012 JEANIE ENTERPRISES LLC 0.00 73.00 366
2013 JEANIE ENTERPRISES LLC 0.00 150.00 365
2014 JEANIE ENTERPRISES LLC 0.00 205.00 365
2015 JEANIE ENTERPRISES LLC 0.00 77.00 365
2016 JEANIE ENTERPRISES LLC 0.00 174.00 365
2017 JEANIE ENTERPRISES LLC 15.00 0.00 365
2018 JEANIE ENTERPRISES LLC 0.00 14.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1995 SCHMELZER MARK Brine 0 365
1996 SCHMELZER MARK Brine 0 365
1997 SCHMELZER MARK Brine 0 365
1998 SCHMELZER MARK Brine 0 365
1999 SCHMELZER MARK Brine 0 365
2000 SCHMELZER MARK Brine 0 365
2001 SCHMELZER MARK Brine 0 365
2002 SCHMELZER MARK Brine 0 365
2003 SCHMELZER MARK Brine 0 365
2004 SCHMELZER MARK Brine 0 365
2005 SCHMELZER MARK Brine 0 365
2006 SCHMELZER MARK Brine 0 365
2007 JEANIE ENTERPRISES LLC Brine 0 365
2008 JEANIE ENTERPRISES LLC Brine 0 365
2009 JEANIE ENTERPRISES LLC Brine 0
2010 JEANIE ENTERPRISES LLC Brine 0 365
2011 JEANIE ENTERPRISES LLC Brine 0 365
2012 JEANIE ENTERPRISES LLC Brine 0 366
2013 JEANIE ENTERPRISES LLC Brine 115 365
2014 JEANIE ENTERPRISES LLC Brine 0 365
2015 JEANIE ENTERPRISES LLC Brine 0 365
2016 JEANIE ENTERPRISES LLC Brine 0 365
2017 JEANIE ENTERPRISES LLC Brine 0 365
2018 JEANIE ENTERPRISES LLC Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-13564100 2013-3-26 0:00: PW No Violations 1.00
-1454401861 2013-6-14 0:00: PW No Violations 1.00
-1514553077 2013-4-2 0:00:0 PW No Violations 1.00
-2014600014 2013-4-11 0:00: PW No Violations 2.00
0013564100 2013-03-26 Production Wells No Violations This well is capable of production. It has a pumping unit on it with rods and tubing. There is no identification at the well or the tank. Oil was all over the ground around the unit. I talked with a Jennifer from Jeanie Enterprises and they are going to get somebody over there right away. I will do a follow up first thing in the morning.
1210526727 2013-03-26 Production Wells Violations Noted During the inspection of this well I found oil around the unit. The plastic flow line was disconnected and the oil pumped on the ground. All the oil will need removed along with the contaminated soil. This well also needs to have identification on it.
1364466253 2013-03-27 Production Wells No Violations I did a follow up on this well to make sure they started the clean-up. I tried to call them and got no answer. I showed up at the well and there was no one there. It was around 8:30 in the morning. They started the clean-up the day before. They put down straw and peat moss to soak up the oil. They had a water pump to pump oil to the tank. I took pics of the location. I will go back tomorrow to check on progress.
1454401861 2013-06-14 Production Wells No Violations I inspected this location to see if everything had been done. The location had been reclaimed, the dike has been put around the tanks and the identification is located on the tank and the well. This well is now in-compliance.
1514553077 2013-04-02 Production Wells No Violations I did a follow up on this well. All of the heavy oil and contaminated soil have been removed. There are still pads on location to clean up small spots. There was no one on location during time of inspection.
1905872786 2013-03-28 Production Wells No Violations I went to see how the clean-up of the oil was going. They put down gravel back the lane to the well. They have a track-o there to remove contaminated soil with a dump truck. They have been putting down diapers to soak up oil. I will check back in a couple days. Everything looks to be going good as of now.
2014600014 2013-04-11 Production Wells No Violations I went and checked on how the clean-up has come along. The contaminated soil has all been removed. It just needs to be straightened back up now. I stopped over at Jeanie Enterprises office and let them no.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1210526727 US-OH-105487 2014-04-23 Well operation causing pollution and contamination
1210526727 US-OH-105488 2014-04-23 Well insufficiently equipped to prevent escape of oil and gas
1210526727 US-OH-105489 2014-04-23 Failure to legibly identify well

For data sources see[7]

References