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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-127-21530 | | Well ID: 34-127-21530 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.59, -82.21 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | Municipality: | + | | State: Ohio |
+ | |- | ||
+ | | County: [[Perry_County,_Ohio|Perry]] | ||
+ | |- | ||
+ | | Municipality: [[Salt Lick_Township,_Perry_County,_Ohio|Salt Lick Township]] | ||
|- | |- | ||
| Operator Name: [[ORPHAN WELL PROGRAM]] | | Operator Name: [[ORPHAN WELL PROGRAM]] | ||
Line 13: | Line 17: | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: WNF (NEW YORK COAL CO) |
|- | |- | ||
− | | | + | | License Status: Final Restoration |
|- | |- | ||
− | | | + | | License Date: 2010-04-05 |
|- | |- | ||
| Spud Date: 1951-05-26 | | Spud Date: 1951-05-26 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: |
+ | |- | ||
+ | | Final Drill Date: 1951-07-06 | ||
+ | |- | ||
+ | | Well Total Depth: 3675.00 ft | ||
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Well Status: | + | | Latitude: 39.590000 |
+ | |- | ||
+ | | Longitude: -82.210000 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
|- | |- | ||
− | | | + | | Original Spud |
+ | | 1951-05-26 | ||
+ | | I/O CASE NO. 2008 05 007 | ||
|- | |- | ||
− | | | + | | Completed |
+ | | 1951-07-06 | ||
+ | | I/O CASE NO. 2008 05 007 | ||
|- | |- | ||
− | | | + | | Reached Total Depth |
+ | | 1951-07-06 | ||
+ | | I/O CASE NO. 2008 05 007 | ||
+ | |- | ||
+ | | APP | ||
+ | | 2010-04-05 | ||
+ | | Proposed Formations:CLINTON, Issued Date:4/5/2010, Expired Date:4/5/2011 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2010-04-05 | ||
+ | | Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM | ||
+ | |- | ||
+ | | Plugged by Orphan Well Program | ||
+ | | 2010-04-27 | ||
+ | | Plugged by Orphan Well Program | ||
+ | |- | ||
+ | | Plugged/Abandoned | ||
+ | | 2010-04-27 | ||
+ | | I/O CASE NO. 2008 05 007 | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 2011-04-05 | ||
+ | | I/O CASE NO. 2008 05 007 | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2015-02-09 | ||
+ | | I/O CASE NO. 2008 05 007 | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | -1227159543 | |
+ | | 2011-6-2 0:00:0 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -1941600534 | ||
+ | | 2011-6-2 0:00:0 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 0.50 | ||
+ | |- | ||
+ | | -2132501503 | ||
+ | | 2010-4-20 0:00: | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 10.00 | ||
+ | |- | ||
+ | | -643910373 | ||
+ | | 2010-1-6 0:00:0 | ||
+ | | OR | ||
+ | | No Violations | ||
+ | | | ||
+ | |- | ||
+ | | -937858483 | ||
+ | | 2010-4-7 0:00:0 | ||
+ | | OR | ||
+ | | No Violations | ||
+ | | 0.50 | ||
+ | |- | ||
+ | | -946318802 | ||
+ | | 2010-4-21 0:00: | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 10.00 | ||
+ | |- | ||
+ | | 0643910373 | ||
+ | | 2010-01-06 | ||
+ | | Orphan | ||
+ | | No Violations | ||
+ | | Pre-bid meeting at well site, met with Rob Stonerock, Mike McCormac, Ken Wright and Ben Lehner, no change in well since last inspection. | ||
+ | |- | ||
+ | | 0870726645 | ||
+ | | 2007-04-18 | ||
+ | | Orphan | ||
+ | | No Violations | ||
+ | | Met with Mike McCormac and Max Norris(WNF) to inspect orphan well, no casing visible in well, open well bore, approx 16 across. Fluid level approx 50ft down. No contamination noted at this time. With an open hole like this in public area this well may cause harm to the public. | ||
+ | |- | ||
+ | | 0937858483 | ||
+ | | 2010-04-07 | ||
+ | | Orphan | ||
+ | | No Violations | ||
+ | | Plugging rig will be moving in next week. | ||
+ | |- | ||
+ | | 0946318802 | ||
+ | | 2010-04-21 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | At start up pumped over 300 bbls of water in well bore, no circulation. Built another pit and started mixing gel, and lost circulation materials for LCM pill. Pumped LCM pill down well bore and started cleaning out well bore, still no circulation. Mixed up another LCM pill and pumped down well bore, left set over night. | ||
+ | |- | ||
+ | | 0956882573 | ||
+ | | 2008-02-26 | ||
+ | | Orphan | ||
+ | | No Violations | ||
+ | | Follow-up inspection, took photos and sketch for I&O case. | ||
|- | |- | ||
| 1074707834 | | 1074707834 | ||
| 2010-04-22 | | 2010-04-22 | ||
− | | | + | | Plug / Plug Back |
− | | Started cleaning down well bore, after pumping approx. 20 bbls of fluid in well bore circulation was losted. Tripped out of well and reduced bit size to a 6 1/4, tripped back in continued cleaning down well bore with no circulation. Pumped approx 200 bbls of water with no circulation. Cleaned down to approx. | + | | No Violations |
− | + | | Started cleaning down well bore, after pumping approx. 20 bbls of fluid in well bore circulation was losted. Tripped out of well and reduced bit size to a 6 1/4, tripped back in continued cleaning down well bore with no circulation. Pumped approx 200 bbls of water with no circulation. Cleaned down to approx. 1135ft., with no circulation. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1137272568 | | 1137272568 | ||
| 2009-08-24 | | 2009-08-24 | ||
− | | | + | | Orphan |
+ | | No Violations | ||
| Marked well location and lease road for pre-bid meeting. | | Marked well location and lease road for pre-bid meeting. | ||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 1227159543 |
− | |||
| 2011-06-02 | | 2011-06-02 | ||
− | | | + | | Final Restoration |
+ | | No Violations | ||
| Accompanied D. Goins on restoration follow-up. | | Accompanied D. Goins on restoration follow-up. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1273750107 | | 1273750107 | ||
| 2010-04-16 | | 2010-04-16 | ||
− | | | + | | Plug / Plug Back |
− | | Cleaning out well bore with a 8 3/4 button bit. Drilling out wood and plug materials. At the end of the day approx. | + | | No Violations |
− | + | | Cleaning out well bore with a 8 3/4 button bit. Drilling out wood and plug materials. At the end of the day approx. 80ft deep. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1273841312 | | 1273841312 | ||
| 2010-04-23 | | 2010-04-23 | ||
− | | | + | | Plug / Plug Back |
− | | Spoke with Mike McCormac about plugging well at | + | | No Violations |
− | + | | Spoke with Mike McCormac about plugging well at 1135ft, company has fears that if they continue down well bore without circulation that materials may stick bit anad drill pipe. No shows of gas since first drilling through rock bidge plug. Pulled drill pipe and bit, ran in 1 1/2 tubing in well bore. Cemented well bore soild from 1135ft to 170ft. Will leave set over weekend will tap plug next week. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1273842282 | | 1273842282 | ||
| 2010-04-27 | | 2010-04-27 | ||
− | | | + | | Plug / Plug Back |
− | | Tagged plug, plug set at | + | | No Violations |
− | + | | Tagged plug, plug set at 210ft. Set Brush and stone bridge plug at 210ft over coal seam. Topped off well with approx. 6 yards of 9 bag grout mix. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1435798528 | | 1435798528 | ||
| 2010-04-19 | | 2010-04-19 | ||
− | | | + | | Plug / Plug Back |
− | | Started cleaning out well bore, at approx. | + | | No Violations |
− | + | | Started cleaning out well bore, at approx. 170ft lost circulation, recovered after pumping approx. 100bbl of brine. At approx. 223ft drilling hard material, at 225ft lost circulation, unable to recover. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1722440352 | | 1722440352 | ||
| 2010-04-01 | | 2010-04-01 | ||
− | | | + | | Orphan |
+ | | No Violations | ||
| Started to remove trees and brush and prepare well site for plugging rig. | | Started to remove trees and brush and prepare well site for plugging rig. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 1941600534 |
| 2011-06-02 | | 2011-06-02 | ||
− | | | + | | Final Restoration |
+ | | No Violations | ||
| Restoration meets 1509.072(B) requirements. | | Restoration meets 1509.072(B) requirements. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1966972584 | | 1966972584 | ||
| 2010-04-29 | | 2010-04-29 | ||
− | | | + | | Plug / Plug Back |
+ | | No Violations | ||
| Witnessed cutting off conductor casing and placing ID plate on well bore. | | Witnessed cutting off conductor casing and placing ID plate on well bore. | ||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 2132501503 |
− | |||
| 2010-04-20 | | 2010-04-20 | ||
− | | | + | | Plug / Plug Back |
− | | No circulation at start up, pumped approx. 200bbls of water. Able to get circulation back on well bore, started cleaning out well bore. Approx. | + | | No Violations |
− | + | | No circulation at start up, pumped approx. 200bbls of water. Able to get circulation back on well bore, started cleaning out well bore. Approx.275ft hit rock bridge plug, after drilling out bridge plug encountered small amount of gas and water. Continued cleaning out well bore at approx. 400ft lost circulation. Pumped approx.125 bbls of water down well bore and shut in for the night. | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 870726645 | | 870726645 | ||
− | | 2007- | + | | 2007-4-18 0:00: |
− | | | + | | OR |
− | | | + | | No Violations |
− | |||
− | |||
| | | | ||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 956882573 | | 956882573 | ||
− | | 2008- | + | | 2008-2-26 0:00: |
− | | | + | | OR |
− | | | + | | No Violations |
− | |||
− | |||
| | | | ||
|- | |- | ||
|} | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-127-21530 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Salt Lick Township | |
Operator Name: ORPHAN WELL PROGRAM | |
Well Pad ID: | |
Farm/Lease Name: WNF (NEW YORK COAL CO) | |
License Status: Final Restoration | |
License Date: 2010-04-05 | |
Spud Date: 1951-05-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1951-07-06 | |
Well Total Depth: 3675.00 ft | |
Configuration: Vertical | |
Latitude: 39.590000 | |
Longitude: -82.210000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1951-05-26 | I/O CASE NO. 2008 05 007 |
Completed | 1951-07-06 | I/O CASE NO. 2008 05 007 |
Reached Total Depth | 1951-07-06 | I/O CASE NO. 2008 05 007 |
APP | 2010-04-05 | Proposed Formations:CLINTON, Issued Date:4/5/2010, Expired Date:4/5/2011 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2010-04-05 | Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM |
Plugged by Orphan Well Program | 2010-04-27 | Plugged by Orphan Well Program |
Plugged/Abandoned | 2010-04-27 | I/O CASE NO. 2008 05 007 |
Construction Permit Expires | 2011-04-05 | I/O CASE NO. 2008 05 007 |
Record Last Modified | 2015-02-09 | I/O CASE NO. 2008 05 007 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1227159543 | 2011-6-2 0:00:0 | FR | No Violations | 1.00 |
-1941600534 | 2011-6-2 0:00:0 | FR | No Violations | 0.50 |
-2132501503 | 2010-4-20 0:00: | PB | No Violations | 10.00 |
-643910373 | 2010-1-6 0:00:0 | OR | No Violations | |
-937858483 | 2010-4-7 0:00:0 | OR | No Violations | 0.50 |
-946318802 | 2010-4-21 0:00: | PB | No Violations | 10.00 |
0643910373 | 2010-01-06 | Orphan | No Violations | Pre-bid meeting at well site, met with Rob Stonerock, Mike McCormac, Ken Wright and Ben Lehner, no change in well since last inspection. |
0870726645 | 2007-04-18 | Orphan | No Violations | Met with Mike McCormac and Max Norris(WNF) to inspect orphan well, no casing visible in well, open well bore, approx 16 across. Fluid level approx 50ft down. No contamination noted at this time. With an open hole like this in public area this well may cause harm to the public. |
0937858483 | 2010-04-07 | Orphan | No Violations | Plugging rig will be moving in next week. |
0946318802 | 2010-04-21 | Plug / Plug Back | No Violations | At start up pumped over 300 bbls of water in well bore, no circulation. Built another pit and started mixing gel, and lost circulation materials for LCM pill. Pumped LCM pill down well bore and started cleaning out well bore, still no circulation. Mixed up another LCM pill and pumped down well bore, left set over night. |
0956882573 | 2008-02-26 | Orphan | No Violations | Follow-up inspection, took photos and sketch for I&O case. |
1074707834 | 2010-04-22 | Plug / Plug Back | No Violations | Started cleaning down well bore, after pumping approx. 20 bbls of fluid in well bore circulation was losted. Tripped out of well and reduced bit size to a 6 1/4, tripped back in continued cleaning down well bore with no circulation. Pumped approx 200 bbls of water with no circulation. Cleaned down to approx. 1135ft., with no circulation. |
1137272568 | 2009-08-24 | Orphan | No Violations | Marked well location and lease road for pre-bid meeting. |
1227159543 | 2011-06-02 | Final Restoration | No Violations | Accompanied D. Goins on restoration follow-up. |
1273750107 | 2010-04-16 | Plug / Plug Back | No Violations | Cleaning out well bore with a 8 3/4 button bit. Drilling out wood and plug materials. At the end of the day approx. 80ft deep. |
1273841312 | 2010-04-23 | Plug / Plug Back | No Violations | Spoke with Mike McCormac about plugging well at 1135ft, company has fears that if they continue down well bore without circulation that materials may stick bit anad drill pipe. No shows of gas since first drilling through rock bidge plug. Pulled drill pipe and bit, ran in 1 1/2 tubing in well bore. Cemented well bore soild from 1135ft to 170ft. Will leave set over weekend will tap plug next week. |
1273842282 | 2010-04-27 | Plug / Plug Back | No Violations | Tagged plug, plug set at 210ft. Set Brush and stone bridge plug at 210ft over coal seam. Topped off well with approx. 6 yards of 9 bag grout mix. |
1435798528 | 2010-04-19 | Plug / Plug Back | No Violations | Started cleaning out well bore, at approx. 170ft lost circulation, recovered after pumping approx. 100bbl of brine. At approx. 223ft drilling hard material, at 225ft lost circulation, unable to recover. |
1722440352 | 2010-04-01 | Orphan | No Violations | Started to remove trees and brush and prepare well site for plugging rig. |
1941600534 | 2011-06-02 | Final Restoration | No Violations | Restoration meets 1509.072(B) requirements. |
1966972584 | 2010-04-29 | Plug / Plug Back | No Violations | Witnessed cutting off conductor casing and placing ID plate on well bore. |
2132501503 | 2010-04-20 | Plug / Plug Back | No Violations | No circulation at start up, pumped approx. 200bbls of water. Able to get circulation back on well bore, started cleaning out well bore. Approx.275ft hit rock bridge plug, after drilling out bridge plug encountered small amount of gas and water. Continued cleaning out well bore at approx. 400ft lost circulation. Pumped approx.125 bbls of water down well bore and shut in for the night. |
870726645 | 2007-4-18 0:00: | OR | No Violations | |
956882573 | 2008-2-26 0:00: | OR | No Violations |
For data sources see[3]