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Difference between revisions of "34-093-21240"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-093-21240
 
| Well ID: 34-093-21240
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.2784156208, -82.2153712087 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.27, -82.21 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| Country: United States
 
|-
 
|-
| Municipality:
+
| State: Ohio
 
|-
 
|-
| Operator Name:
+
| County: [[Lorain_County,_Ohio|Lorain]]
 
|-
 
|-
| Well Pad ID:
+
| Municipality: [[Pittsfield_Township,_Lorain_County,_Ohio|Pittsfield Township]]
 
|-
 
|-
| Farm/Lease Name:
+
| Operator Name: [[BECKMAN ANNIE]]
 
|-
 
|-
| First Permit Date:
+
| Well Pad ID:  
 
|-
 
|-
| Last Permit Date:
+
| Farm/Lease Name: BECKMAN FRANK
 
|-
 
|-
| Spud Date:
+
| License Status: Domestic Well
 
|-
 
|-
| Unconventional:
+
| License Date: 1983-11-16
 
|-
 
|-
| Horizontal:
+
| Spud Date: 1900-01-01
 
|-
 
|-
| Producing: No
+
| Spud Drilling Contractor:  
 
|-
 
|-
| Violations: 2
+
| Final Drill Date:  
 
|-
 
|-
| Latitude: 41.2784156208
+
| Well Total Depth: 0.00 ft
 
|-
 
|-
| Longitude: -82.2153712087
+
| Configuration: Vertical
 
|-
 
|-
 +
| Latitude: 41.270000
 +
|-
 +
| Longitude: -82.210000
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | GAS QUANTITY
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comment
!scope="col" | CONDENSATE QUANTITY
+
|-
!scope="col" | CONDENSATE PRODUCTION DAYS
+
| CO
!scope="col" | OIL QUANTITY
+
| 1983-11-16
!scope="col" | OIL PRODUCTION DAYS
+
| 1647  BECKMAN ANNIE  GeoDate  11/16/83
 +
|-
 +
| Oil and Gas
 +
| 1983-11-16
 +
| Issued Date 11/16/83 Expired Date 5/14/84 Acres 0006780 Tool Type CT Proposed Formation OHIO SHALE Proposed Depth 00000 Proposed Drill Depth 00000
 +
|-
 +
| Construction Permit Expires
 +
| 1984-05-14
 +
| PERMIT EXPIRED.
 +
|-
 +
| Record Last Modified
 +
| 2015-09-24
 +
| PERMIT EXPIRED.
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | TYPE
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | QUANTITY
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | UNITS
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | DISPOSAL METHOD
+
|-
!scope="col" | WASTE FACILITY PERMIT ID
+
|}-->
!scope="col" | WASTE FACILITY NAME
+
<!--== Fracking Activities ==
!scope="col" | FACILITY CITY
+
==== Fracking Jobs ====
!scope="col" | FACILITY STATE
+
{| class="wikitable sortable" width="95%"
|}
+
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
 
| 1144703944
 
| 1144703944
 
| 2006-04-10
 
| 2006-04-10
|
+
| Production Wells
 +
| Violations Noted
 
| Domestic gas well. Leak has been repaired by Hottel Oil and Gas for Mrs. Beckman. 32 psi on well gauge. Home is using gas from well. Mrs. Beckman has not replaced gas line from Columbia Gas to her home. Sun, 60 degrees.
 
| Domestic gas well. Leak has been repaired by Hottel Oil and Gas for Mrs. Beckman. 32 psi on well gauge. Home is using gas from well. Mrs. Beckman has not replaced gas line from Columbia Gas to her home. Sun, 60 degrees.
|
 
| 9-9-05(A)1
 
|
 
 
|-
 
|-
 +
| 1542734855
 +
| 2018-10-30
 +
| Exempt Well Pre Transfer
 +
| No Violations
 +
| Conducted this compliance inspection at the request of Kathryn Smith of DOGRM Surety & Bonding section to perform Pre-Exempt Transfer inspection. I met the tenant he proceeded to show me where the well is located due to the ODNRs well locator which shows this well on the property to the west. The actual location of the well is (Lat/Long 41.27877, -82.213823)  which is to the east of the barn. This well didnt have a well head it had the 4.5 diameter casing with a swedge and a valve then to a flow lines, which to a regulator; all of which is located at the northeast corner of the house no within tank battery.
 +
1. No compliance issues found at time of inspection.
 +
2. No inhabited structure within 200 feet.
 +
3. Well is used to provide domestic gas to the house located at 102 E. Hamilton street.
 +
4. Well is located on property own by Annie Ruth Beckman Trust Bonnie Rm Venable Trustee.
 +
|-
 +
| 1593131580
 +
| 2006-03-24
 +
| Production Wells
 +
| Violations Noted
 +
| Called by David Hodges to check gas complaint from Oberlin Fire Department. Columbia Gas shut off Mrs. Beckmans gas to her home due to leaks in line from Columbias service and her domestic gas well. Valve is closed on top of well head. 9% lel is leaking from 6 casing at well. Advised Mrs. Beckman to have leak repaired before Columbia will turn on her gas. They pulled her meter. Called Doug Hottel to repair well and run new gas line to her home. Cloudy, 35 degrees.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 1144703944
 +
| US-OH-103715
 +
| 2006-03-24
 +
|
 +
| Well insufficiently equipped to prevent escape of oil and gas
 
|-
 
|-
 
| 1593131580
 
| 1593131580
 +
| US-OH-115580
 
| 2006-03-24
 
| 2006-03-24
|
+
|  
| Called by David Hodges to check gas complaint from Oberlin Fire Department. Columbia Gas shut off Mrs. Beckman's gas to her home due to leaks in line from Columbia's service and her domestic gas well. Valve is closed on top of well head. 9% lel is leaking from 6'' casing at well. Advised Mrs. Beckman to have leak repaired before Columbia will turn on her gas. They pulled her meter. Called Doug Hottel to repair well and run new gas line to her home. Cloudy, 35 degrees.
+
| Well insufficiently equipped to prevent escape of oil and gas
|
 
| 9-9-05(A)1
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 09:58, 12 January 2021

Well Details

Well ID: 34-093-21240
Loading map...
Country: United States
State: Ohio
County: Lorain
Municipality: Pittsfield Township
Operator Name: BECKMAN ANNIE
Well Pad ID:
Farm/Lease Name: BECKMAN FRANK
License Status: Domestic Well
License Date: 1983-11-16
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 41.270000
Longitude: -82.210000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1983-11-16 1647 BECKMAN ANNIE GeoDate 11/16/83
Oil and Gas 1983-11-16 Issued Date 11/16/83 Expired Date 5/14/84 Acres 0006780 Tool Type CT Proposed Formation OHIO SHALE Proposed Depth 00000 Proposed Drill Depth 00000
Construction Permit Expires 1984-05-14 PERMIT EXPIRED.
Record Last Modified 2015-09-24 PERMIT EXPIRED.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1144703944 2006-04-10 Production Wells Violations Noted Domestic gas well. Leak has been repaired by Hottel Oil and Gas for Mrs. Beckman. 32 psi on well gauge. Home is using gas from well. Mrs. Beckman has not replaced gas line from Columbia Gas to her home. Sun, 60 degrees.
1542734855 2018-10-30 Exempt Well Pre Transfer No Violations Conducted this compliance inspection at the request of Kathryn Smith of DOGRM Surety & Bonding section to perform Pre-Exempt Transfer inspection. I met the tenant he proceeded to show me where the well is located due to the ODNRs well locator which shows this well on the property to the west. The actual location of the well is (Lat/Long 41.27877, -82.213823) which is to the east of the barn. This well didnt have a well head it had the 4.5 diameter casing with a swedge and a valve then to a flow lines, which to a regulator; all of which is located at the northeast corner of the house no within tank battery.

1. No compliance issues found at time of inspection. 2. No inhabited structure within 200 feet. 3. Well is used to provide domestic gas to the house located at 102 E. Hamilton street. 4. Well is located on property own by Annie Ruth Beckman Trust Bonnie Rm Venable Trustee.

1593131580 2006-03-24 Production Wells Violations Noted Called by David Hodges to check gas complaint from Oberlin Fire Department. Columbia Gas shut off Mrs. Beckmans gas to her home due to leaks in line from Columbias service and her domestic gas well. Valve is closed on top of well head. 9% lel is leaking from 6 casing at well. Advised Mrs. Beckman to have leak repaired before Columbia will turn on her gas. They pulled her meter. Called Doug Hottel to repair well and run new gas line to her home. Cloudy, 35 degrees.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1144703944 US-OH-103715 2006-03-24 Well insufficiently equipped to prevent escape of oil and gas
1593131580 US-OH-115580 2006-03-24 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[3]

References