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Difference between revisions of "34-155-22187"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-155-22187
 
| Well ID: 34-155-22187
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.29670909, -80.58687528 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.29, -80.58 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Trumbull County, Ohio|Trumbull]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Trumbull_County,_Ohio|Trumbull]]
 +
|-
 +
| Municipality: [[Hartford_Township,_Trumbull_County,_Ohio|Hartford Township]]
 
|-
 
|-
 
| Operator Name: [[BIG SKY ENERGY INC]]
 
| Operator Name: [[BIG SKY ENERGY INC]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: JONES K
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1984-07-11
 
|-
 
|-
 
| Spud Date: 1985-01-05
 
| Spud Date: 1985-01-05
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[ARMSTRONG DRLG]]
 +
|-
 +
| Final Drill Date: 1985-01-10
 +
|-
 +
| Well Total Depth: 5036.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 41.290000
 
|-
 
|-
| Violations: 0
+
| Longitude: -80.580000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Latitude: 41.29670909
+
| Oil and Gas
 +
| 1982-04-15
 +
| Issued Date 4/15/82 Expired Date 10/12/82 Acres 0051110 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
 
|-
 
|-
| Longitude: -80.58687528
+
| CO
 +
| 1984-07-11
 +
| 54  TITAN ENERGY CORP  GeoDate  7/11/84
 +
|-
 +
| Oil and Gas
 +
| 1984-07-11
 +
| Issued Date 7/11/84 Expired Date 1/7/85 Acres 0051110 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05036 Proposed Drill Depth 05036
 +
|-
 +
| Original Spud
 +
| 1985-01-05
 +
| WELL CARD DATA
 +
PI 4/15/82
 +
S/OIL; TOOL RF
 +
ORIG OWNER AKA TITAN ENERGY GROUP
 +
|-
 +
| Construction Permit Expires
 +
| 1985-01-07
 +
| WELL CARD DATA
 +
PI 4/15/82
 +
S/OIL; TOOL RF
 +
ORIG OWNER AKA TITAN ENERGY GROUP
 +
|-
 +
| Completed
 +
| 1985-01-10
 +
| WELL CARD DATA
 +
PI 4/15/82
 +
S/OIL; TOOL RF
 +
ORIG OWNER AKA TITAN ENERGY GROUP
 +
|-
 +
| Reached Total Depth
 +
| 1985-01-10
 +
| WELL CARD DATA
 +
PI 4/15/82
 +
S/OIL; TOOL RF
 +
ORIG OWNER AKA TITAN ENERGY GROUP
 +
|-
 +
| CO
 +
| 1985-02-12
 +
| 224  ATLAS ENERGY GROUP INC  GeoDate  4/15/82
 +
|-
 +
| Completion Report Received
 +
| 1985-02-26
 +
| WELL CARD DATA
 +
PI 4/15/82
 +
S/OIL; TOOL RF
 +
ORIG OWNER AKA TITAN ENERGY GROUP
 +
|-
 +
| Change of Owner
 +
| 1998-01-26
 +
| Operator changed from 54, TITAN ENERGY CORP to 1333, BARR ROBT/dba BIG SKY PET
 +
|-
 +
| Plugging Plan Approved
 +
| 1998-01-27
 +
| WELL CARD DATA
 +
PI 4/15/82
 +
S/OIL; TOOL RF
 +
ORIG OWNER AKA TITAN ENERGY GROUP
 +
|-
 +
| Record Last Modified
 +
| 2017-02-15
 +
| WELL CARD DATA
 +
PI 4/15/82
 +
S/OIL; TOOL RF
 +
ORIG OWNER AKA TITAN ENERGY GROUP
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | CONDENSATE PRODUCTION DAYS
+
|-
!scope="col" | OIL QUANTITY
+
| 1998-01-27
!scope="col" | OIL PRODUCTION DAYS
+
| style="text-align: right;" | 4833
 +
| style="text-align: right;" | 4881
 +
| style="text-align: right;" | 23
 
|-
 
|-
| 1985-0
 
| style="text-align:right;" | 4590.0
 
 
|  
 
|  
 +
| style="text-align: right;" | 4833
 +
| style="text-align: right;" | 4881
 +
| style="text-align: right;" | 23
 +
|-
 
|  
 
|  
|  
+
| style="text-align: right;" | 4833
| style="text-align:right;" | 46.0
+
| style="text-align: right;" | 4881
|  
+
| style="text-align: right;" | 23
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
 +
|}-->
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1986-0
 
| style="text-align:right;" | 2890.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 74886 Gal
 +
| style="text-align: right;" | 70000
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 79.0
+
|-
 +
|
 +
| ACID
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 500 Gal
 +
| style="text-align: right;" | 0
 
|  
 
|  
 +
| F/W 500 GAL ACID; 74886 GAL H2O, 70M# SAND, 180 MSCF N2
 
|-
 
|-
|-
 
| 1987-0
 
| style="text-align:right;" | 684.0
 
 
|  
 
|  
 +
| N2
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 180 Mscf
 +
| style="text-align: right;" | 0
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1985
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 4590.00
 +
| style="text-align: right;" | 46.00
 +
| style="text-align: right;" | 283
 +
|-
 +
| 1986
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 2890.00
 +
| style="text-align: right;" | 79.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1987
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 684.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1988
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 2293.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1989
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 2399.00
 +
| style="text-align: right;" | 70.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1990
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 1734.00
 +
| style="text-align: right;" | 52.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1991
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 684.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1992
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 479.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1994
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1997
 +
| [[TITAN ENERGY CORP]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 245
 +
|-
 +
| 2000
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 1707.00
 +
| style="text-align: right;" | 78.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 720.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2002
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 1366.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2003
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 1911.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2004
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 927.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1988-0
+
| 2005
| style="text-align:right;" | 2293.0
+
| [[BIG SKY ENERGY INC]]
|  
+
| style="text-align: right;" | 511.00
|
+
| style="text-align: right;" | 48.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 1002.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1989-0
+
| 2007
| style="text-align:right;" | 2399.0
+
| [[BIG SKY ENERGY INC]]
|  
+
| style="text-align: right;" | 833.00
|
+
| style="text-align: right;" | 31.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 70.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 790.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1990-0
+
| 2009
| style="text-align:right;" | 1734.0
+
| [[BIG SKY ENERGY INC]]
|  
+
| style="text-align: right;" | 2146.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 52.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 1266.00
 +
| style="text-align: right;" | 31.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1991-0
+
| 2011
| style="text-align:right;" | 684.0
+
| [[BIG SKY ENERGY INC]]
|
+
| style="text-align: right;" | 722.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 2012
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 1821.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 1992-0
+
| 2013
| style="text-align:right;" | 479.0
+
| [[BIG SKY ENERGY INC]]
|
+
| style="text-align: right;" | 473.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 2014
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 619.00
 +
| style="text-align: right;" | 11.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1993-0
+
| 2016
| style="text-align:right;" | 0.0
+
| [[BIG SKY ENERGY INC]]
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 98
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 2017
 +
| [[BIG SKY ENERGY INC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1994-0
+
|}
| style="text-align:right;" | 0.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2020-11-16
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1985
 +
| [[TITAN ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 283
 
|-
 
|-
| 1997-0
+
| 1986
| style="text-align:right;" | 0.0
+
| [[TITAN ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1987
 +
| [[TITAN ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 1988
| style="text-align:right;" | 1707.0
+
| [[TITAN ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 78.0
 
|
 
 
|-
 
|-
 +
| 1989
 +
| [[TITAN ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 1990
| style="text-align:right;" | 720.0
+
| [[TITAN ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[TITAN ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 1992
| style="text-align:right;" | 1366.0
+
| [[TITAN ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[TITAN ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 1994
| style="text-align:right;" | 1911.0
+
| [[TITAN ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[TITAN ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 245
 
|-
 
|-
| 2004-0
+
| 2000
| style="text-align:right;" | 927.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 2002
| style="text-align:right;" | 511.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 48.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2006-0
+
| 2004
| style="text-align:right;" | 1002.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2007-0
+
| 2006
| style="text-align:right;" | 833.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 31.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2008
| style="text-align:right;" | 790.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 2010
| style="text-align:right;" | 2146.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2010-0
+
| 2012
| style="text-align:right;" | 1266.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 366
| style="text-align:right;" | 31.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2011-0
+
| 2014
| style="text-align:right;" | 722.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 45
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[BIG SKY ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 98
 
|-
 
|-
| 2012-0
+
| 2017
| style="text-align:right;" | 1821.0
+
| [[BIG SKY ENERGY INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| -1048590846
 +
| 2016-6-10 0:00:
 +
| PW
 +
| No Violations
 +
| 0.70
 
|-
 
|-
 
| -1055987089
 
| -1055987089
 +
| 2014-10-14 0:00
 +
| PW
 +
| No Violations
 +
| 0.50
 +
|-
 +
| 0000PL4007
 +
|
 +
| Preliminary Restoration
 +
| No Violations
 +
| Preliminary Restoration  done information from Data Point
 +
|-
 +
| 0002609818
 +
| 2017-12-12
 +
| Production Wells
 +
| No Violations
 +
-up line has a plug.  The access road in the good repair.  Photos were taken and are available upon request.
 +
|-
 +
| 0070987720
 +
| 2017-01-18
 +
| Production Wells
 +
| No Violations
 +
 +
 +
Big Sky still needs to:
 +
Scrap up soil next to the wellhead and dispose of at an approved landfill.
 +
 +
Photos were taken and are available upon request.
 +
|-
 +
| 0759656778
 +
| 2018-03-19
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-up for compliance notice 1106553772.  The well was equipped with a Concoyle plunger lift assembly and the annulus and flow line valves were open.  There was oil stained soil still located at the base of the well and still needs cleaned up.  The tank battery consisted of one 100 BBL production tank, one 50 BBL tank and a mechanical separator.  Valves on the separator were open.  The tank battery was diked.  There was a Big Sky Energy stenciled identification sign on a storage tank and an identification sign on the separator, which was legible.  The access was stable.
 +
|-
 +
| 1048590846
 +
| 2016-06-10
 +
| Production Wells
 +
| No Violations
 +
 +
|-
 +
| 1055987089
 
| 2014-10-14
 
| 2014-10-14
|  
+
| Production Wells
 +
| No Violations
 
| I was on location for a status check.  During my inspection, I found the well in production.  The well was equipped with a 4 Concoyl assembly.  The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank, and a separator.  A dike surrounded the production equipment.  An identification sign was stenciled on the production tank.  There was a bull plug on the load line.  There was a 7 day production chart in the separator.  The lease road was in stable condition.
 
| I was on location for a status check.  During my inspection, I found the well in production.  The well was equipped with a 4 Concoyl assembly.  The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank, and a separator.  A dike surrounded the production equipment.  An identification sign was stenciled on the production tank.  There was a bull plug on the load line.  There was a 7 day production chart in the separator.  The lease road was in stable condition.
 +
|-
 +
| 1106553772
 +
| 2016-04-28
 +
| Production Wells
 +
| Violations Noted
 +
| I was on location in reference to compliance to Chiefs Order 2016-
 +
 +
Big Sky needs to:
 +
Shut in the well immediately per the temporary restraining order issued by the Trumbull County Court of Common Pleas dated 4-11-2016
 +
Remove and properly dispose of all oil stained soil and vegetation at the well and separator.
 +
Repair the surface area affected by the oil releases at the well and separator.
 +
 +
The equipment on the site consists of the following:
 +
 +
 +
1 Mechanical separator
 +
|-
 +
| 2609818
 +
| 2017-12-12 0:00
 +
| PW
 +
| No Violations
 +
| 0.50
 +
|-
 +
| 70987720
 +
| 2017-1-18 0:00:
 +
| PW
 +
| No Violations
 +
| 0.60
 +
|-
 +
| 759656778
 +
| 2018-3-19 0:00:
 +
| PW
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| PL4007
 
|  
 
|  
 +
| PL
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| PL4007
+
| 1106553772
|
+
| US-OH-102631
|
+
| 2016-05-27
| Preliminary Restoration  done information from Data Point
 
|  
 
|  
 
 
|  
 
|  
 +
| Well operation causing pollution and contamination
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 10:05, 12 January 2021

Well Details

Well ID: 34-155-22187
Loading map...
Country: United States
State: Ohio
County: Trumbull
Municipality: Hartford Township
Operator Name: BIG SKY ENERGY INC
Well Pad ID:
Farm/Lease Name: JONES K
License Status: Producing
License Date: 1984-07-11
Spud Date: 1985-01-05
Spud Drilling Contractor: ARMSTRONG DRLG
Final Drill Date: 1985-01-10
Well Total Depth: 5036.00 ft
Configuration: Vertical
Latitude: 41.290000
Longitude: -80.580000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-04-15 Issued Date 4/15/82 Expired Date 10/12/82 Acres 0051110 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-07-11 54 TITAN ENERGY CORP GeoDate 7/11/84
Oil and Gas 1984-07-11 Issued Date 7/11/84 Expired Date 1/7/85 Acres 0051110 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05036 Proposed Drill Depth 05036
Original Spud 1985-01-05 WELL CARD DATA

PI 4/15/82 S/OIL; TOOL RF ORIG OWNER AKA TITAN ENERGY GROUP

Construction Permit Expires 1985-01-07 WELL CARD DATA

PI 4/15/82 S/OIL; TOOL RF ORIG OWNER AKA TITAN ENERGY GROUP

Completed 1985-01-10 WELL CARD DATA

PI 4/15/82 S/OIL; TOOL RF ORIG OWNER AKA TITAN ENERGY GROUP

Reached Total Depth 1985-01-10 WELL CARD DATA

PI 4/15/82 S/OIL; TOOL RF ORIG OWNER AKA TITAN ENERGY GROUP

CO 1985-02-12 224 ATLAS ENERGY GROUP INC GeoDate 4/15/82
Completion Report Received 1985-02-26 WELL CARD DATA

PI 4/15/82 S/OIL; TOOL RF ORIG OWNER AKA TITAN ENERGY GROUP

Change of Owner 1998-01-26 Operator changed from 54, TITAN ENERGY CORP to 1333, BARR ROBT/dba BIG SKY PET
Plugging Plan Approved 1998-01-27 WELL CARD DATA

PI 4/15/82 S/OIL; TOOL RF ORIG OWNER AKA TITAN ENERGY GROUP

Record Last Modified 2017-02-15 WELL CARD DATA

PI 4/15/82 S/OIL; TOOL RF ORIG OWNER AKA TITAN ENERGY GROUP

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1998-01-27 4833 4881 23
4833 4881 23
4833 4881 23

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 74886 Gal 70000
ACID 0 500 Gal 0 F/W 500 GAL ACID; 74886 GAL H2O, 70M# SAND, 180 MSCF N2
N2 0 180 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 TITAN ENERGY CORP 4590.00 46.00 283
1986 TITAN ENERGY CORP 2890.00 79.00 365
1987 TITAN ENERGY CORP 684.00 0.00 365
1988 TITAN ENERGY CORP 2293.00 0.00 365
1989 TITAN ENERGY CORP 2399.00 70.00 365
1990 TITAN ENERGY CORP 1734.00 52.00 365
1991 TITAN ENERGY CORP 684.00 0.00 365
1992 TITAN ENERGY CORP 479.00 0.00 365
1993 TITAN ENERGY CORP 0.00 0.00 365
1994 TITAN ENERGY CORP 0.00 0.00 365
1997 TITAN ENERGY CORP 0.00 0.00 245
2000 BIG SKY ENERGY INC 1707.00 78.00 365
2001 BIG SKY ENERGY INC 720.00 0.00 365
2002 BIG SKY ENERGY INC 1366.00 0.00 365
2003 BIG SKY ENERGY INC 1911.00 0.00 365
2004 BIG SKY ENERGY INC 927.00 0.00 365
2005 BIG SKY ENERGY INC 511.00 48.00 365
2006 BIG SKY ENERGY INC 1002.00 0.00 365
2007 BIG SKY ENERGY INC 833.00 31.00 365
2008 BIG SKY ENERGY INC 790.00 0.00 365
2009 BIG SKY ENERGY INC 2146.00 0.00 365
2010 BIG SKY ENERGY INC 1266.00 31.00 365
2011 BIG SKY ENERGY INC 722.00 0.00 365
2012 BIG SKY ENERGY INC 1821.00 0.00 366
2013 BIG SKY ENERGY INC 473.00 0.00 365
2014 BIG SKY ENERGY INC 619.00 11.00 365
2016 BIG SKY ENERGY INC 0.00 0.00 98
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 TITAN ENERGY CORP Brine 0 283
1986 TITAN ENERGY CORP Brine 0 365
1987 TITAN ENERGY CORP Brine 0 365
1988 TITAN ENERGY CORP Brine 0 365
1989 TITAN ENERGY CORP Brine 0 365
1990 TITAN ENERGY CORP Brine 0 365
1991 TITAN ENERGY CORP Brine 0 365
1992 TITAN ENERGY CORP Brine 0 365
1993 TITAN ENERGY CORP Brine 0 365
1994 TITAN ENERGY CORP Brine 0 365
1997 TITAN ENERGY CORP Brine 245
2000 BIG SKY ENERGY INC Brine 0 365
2001 BIG SKY ENERGY INC Brine 0 365
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 365
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 365
2008 BIG SKY ENERGY INC Brine 0 365
2009 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 0 365
2014 BIG SKY ENERGY INC Brine 45 365
2016 BIG SKY ENERGY INC Brine 0 98
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1048590846 2016-6-10 0:00: PW No Violations 0.70
-1055987089 2014-10-14 0:00 PW No Violations 0.50
0000PL4007 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0002609818 2017-12-12 Production Wells No Violations

-up line has a plug. The access road in the good repair. Photos were taken and are available upon request.

0070987720 2017-01-18 Production Wells No Violations


Big Sky still needs to: Scrap up soil next to the wellhead and dispose of at an approved landfill.

Photos were taken and are available upon request.

0759656778 2018-03-19 Production Wells No Violations I conducted a compliance notice follow-up for compliance notice 1106553772. The well was equipped with a Concoyle plunger lift assembly and the annulus and flow line valves were open. There was oil stained soil still located at the base of the well and still needs cleaned up. The tank battery consisted of one 100 BBL production tank, one 50 BBL tank and a mechanical separator. Valves on the separator were open. The tank battery was diked. There was a Big Sky Energy stenciled identification sign on a storage tank and an identification sign on the separator, which was legible. The access was stable.
1048590846 2016-06-10 Production Wells No Violations
1055987089 2014-10-14 Production Wells No Violations I was on location for a status check. During my inspection, I found the well in production. The well was equipped with a 4 Concoyl assembly. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank, and a separator. A dike surrounded the production equipment. An identification sign was stenciled on the production tank. There was a bull plug on the load line. There was a 7 day production chart in the separator. The lease road was in stable condition.
1106553772 2016-04-28 Production Wells Violations Noted I was on location in reference to compliance to Chiefs Order 2016-

Big Sky needs to: Shut in the well immediately per the temporary restraining order issued by the Trumbull County Court of Common Pleas dated 4-11-2016 Remove and properly dispose of all oil stained soil and vegetation at the well and separator. Repair the surface area affected by the oil releases at the well and separator.

The equipment on the site consists of the following:


1 Mechanical separator

2609818 2017-12-12 0:00 PW No Violations 0.50
70987720 2017-1-18 0:00: PW No Violations 0.60
759656778 2018-3-19 0:00: PW No Violations
PL4007 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1106553772 US-OH-102631 2016-05-27 Well operation causing pollution and contamination

For data sources see[9]

References