X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-173-61183"

m
m
 
(4 intermediate revisions by the same user not shown)
Line 1: Line 1:
__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-173-61183
 
| Well ID: 34-173-61183
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.28366759, -83.55204976 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.28, -83.55 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Wood County, Ohio|Wood]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Wood_County,_Ohio|Wood]]
 +
|-
 +
| Municipality: [[Portage_Township,_Wood_County,_Ohio|Portage Township]]
 
|-
 
|-
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2011]]
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2011]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: CARPENTER ROBERT (BATESON RICHARD)
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2011-08-03
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.280000
 +
|-
 +
| Longitude: -83.550000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Oil and Gas
 +
| 2007-12-02
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
 +
|-
 +
| APP
 +
| 2011-08-03
 +
| Proposed Formations:, Issued Date:8/3/2011, Expired Date:8/2/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Change of Owner
 +
| 2011-08-03
 +
| Operator changed from 9999, UNKNOWN OWNER to 8825, LANDOWNER GRANT PROGRAM 2011
 +
|-
 +
| Plugged by Orphan Well Program
 +
| 2012-05-16
 +
| Plugged by Orphan Well Program
 
|-
 
|-
| Violations: 0
+
| Plugged/Abandoned
 +
| 2012-05-16
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
 
|-
 
|-
| Latitude: 41.28366759
+
| Construction Permit Expires
 +
| 2013-08-02
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
 
|-
 
|-
| Longitude: -83.55204976
+
| Record Last Modified
 +
| 2019-06-14
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
 
|-
 
|-
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Job Number
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Job Start Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Job End Date
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| True Vertical Depth (ft)
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Total Water Volume (gal)
!scope="col" | VIOLATION CODE
+
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
!scope="col" | VIOLATION COMMENT
+
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
| 1337181753
+
|}-->
| 2012-05-04
+
<!--== Stimulations Data ==
|  
+
{| class="wikitable sortable" width="95%"
| Plugging Contractor is Black Swamp Oilfield Services, Mike Coyer. Plug set at TD of 744 due to the collapsing shale formation and a crooked hole. The drill pipe is catching on pieces of the surface casing still left in the hole from when it was removed. See Plug Report for details.
+
!scope="col" style="text-align: center"| Stimulation Date
|  
+
!scope="col" style="text-align: center"| Chemical Agent
|  
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
|  
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1337184796
+
|}-->
| 2012-05-15
+
<!--== Waste Data ==
|  
+
{| class="wikitable sortable"
| On site for setting of plug 2 from 342' to 48'. Cement pumped through 2 tubing with circulation of cement to surface. Fresh water formation is taking some cement so level is dropping. See Plug Report for details.
+
!scope="col" style="text-align: center"| Period
|  
+
!scope="col" style="text-align: center"| Operator Name
|  
+
!scope="col" style="text-align: center"| Waste Type
|  
+
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
|}-->
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
 
| -136721053
 
| -136721053
| 2012-04-30
+
| 2012-4-30 0:00:
|  
+
| OR
| At the time of my inspection the cable tool rig was set up on the well and 5.5 bit was ran to about 400' until an unknown obstruction was encountered. The crew is now setting up to run tubing in and circulate hole.
+
| No Violations
|
 
|
 
 
|  
 
|  
|-
 
 
|-
 
|-
 
| -1939794195
 
| -1939794195
| 2012-05-16
+
| 2012-5-16 0:00:
|  
+
| PB
| At the time of my inspection the well was topped off from 48' to the surface with 28 sacks of Sackrete.
+
| No Violations
|
 
|
 
 
|  
 
|  
|-
 
 
|-
 
|-
 
| -1955094967
 
| -1955094967
| 2012-05-02
+
| 2012-5-2 0:00:0
|  
+
| OR
| Rain in the area delayed continuatiun of claenout till mid afternnoon. At the time of my inspection the  2 tubing was at 452' and continued to 545'. The tubing was to hang up and is getting worse as they go deeper.
+
| No Violations
 
|  
 
|  
 +
|-
 +
| -376435608
 +
| 2012-5-1 0:00:0
 +
| OR
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -511940394
 +
| 2012-5-3 0:00:0
 +
| OR
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
|-
+
| -587709463
| 2012623642
+
| 2012-5-17 0:00:
| 2012-12-04
+
| OR
|
+
| No Violations
| At the time of my inspection the area was cleared of all equipment and all pits were closed. The area was then roughly graded for farm use next year. Final Restoration Passed.
 
|  
 
|  
 
 
|  
 
|  
 
|-
 
|-
 +
| 0136721053
 +
| 2012-04-30
 +
| Orphan
 +
| No Violations
 +
| At the time of my inspection the cable tool rig was set up on the well and 5.5 bit was ran to about 400 until an unknown obstruction was encountered. The crew is now setting up to run tubing in and circulate hole.
 
|-
 
|-
| -376435608
+
| 0376435608
 
| 2012-05-01
 
| 2012-05-01
|  
+
| Orphan
| At the time of my inspection a new piece oc casing had to be welded on existing 8 to attach a wellhead. 2 tubing was then ran to 400' to circulate oil out of the wellbore. The tubing is starting to hang up on what we believe is a few remaining pieces of 6 surface casing  around 270' (bottom of the Big Lime).
+
| No Violations
|
+
| At the time of my inspection a new piece oc casing had to be welded on existing 8 to attach a wellhead. 2 tubing was then ran to 400 to circulate oil out of the wellbore. The tubing is starting to hang up on what we believe is a few remaining pieces of 6 surface casing  around 270 (bottom of the Big Lime).
|
 
|
 
|-
 
 
|-
 
|-
| -511940394
+
| 0511940394
 
| 2012-05-03
 
| 2012-05-03
|  
+
| Orphan
| At the time of my inspection another obstruction was hit at 745' and tubing continues to hang up not only on the way down but on the way out as well. Continued circulation has produced no more oil from wellbore.
+
| No Violations
|
+
| At the time of my inspection another obstruction was hit at 745 and tubing continues to hang up not only on the way down but on the way out as well. Continued circulation has produced no more oil from wellbore.
|
 
|
 
 
|-
 
|-
|-
+
| 0587709463
| -587709463
 
 
| 2012-05-17
 
| 2012-05-17
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection the plate has been welded on the top of casing and buried four feet below grade. The pit is also being closed and field tile is being replaced.
 
| At the time of my inspection the plate has been welded on the top of casing and buried four feet below grade. The pit is also being closed and field tile is being replaced.
|  
+
|-
|  
+
| 1337181753
|  
+
| 2012-05-04
 +
| Plug / Plug Back
 +
| No Violations
 +
| Plugging Contractor is Black Swamp Oilfield Services, Mike Coyer. Plug set at TD of 744 due to the collapsing shale formation and a crooked hole. The drill pipe is catching on pieces of the surface casing still left in the hole from when it was removed. See Plug Report for details.
 +
|-
 +
| 1337184796
 +
| 2012-05-15
 +
| Plug / Plug Back
 +
| No Violations
 +
| On site for setting of plug 2 from 342 to 48. Cement pumped through 2 tubing with circulation of cement to surface. Fresh water formation is taking some cement so level is dropping. See Plug Report for details.
 +
|-
 +
| 1939794195
 +
| 2012-05-16
 +
| Plug / Plug Back
 +
| No Violations
 +
| At the time of my inspection the well was topped off from 48 to the surface with 28 sacks of Sackrete.
 +
|-
 +
| 1955094967
 +
| 2012-05-02
 +
| Orphan
 +
| No Violations
 +
| Rain in the area delayed continuatiun of claenout till mid afternnoon. At the time of my inspection the  2 tubing was at 452 and continued to 545. The tubing was to hang up and is getting worse as they go deeper.
 +
|-
 +
| 2012623642
 +
| 2012-12-04
 +
| Final Restoration
 +
| No Violations
 +
| At the time of my inspection the area was cleared of all equipment and all pits were closed. The area was then roughly graded for farm use next year. Final Restoration Passed.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 11:39, 12 January 2021

Well Details

Well ID: 34-173-61183
Loading map...
Country: United States
State: Ohio
County: Wood
Municipality: Portage Township
Operator Name: LANDOWNER GRANT PROGRAM 2011
Well Pad ID:
Farm/Lease Name: CARPENTER ROBERT (BATESON RICHARD)
License Status: Final Restoration
License Date: 2011-08-03
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.280000
Longitude: -83.550000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 2007-12-02 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
APP 2011-08-03 Proposed Formations:, Issued Date:8/3/2011, Expired Date:8/2/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2011-08-03 Operator changed from 9999, UNKNOWN OWNER to 8825, LANDOWNER GRANT PROGRAM 2011
Plugged by Orphan Well Program 2012-05-16 Plugged by Orphan Well Program
Plugged/Abandoned 2012-05-16 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
Construction Permit Expires 2013-08-02 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
Record Last Modified 2019-06-14 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-136721053 2012-4-30 0:00: OR No Violations
-1939794195 2012-5-16 0:00: PB No Violations
-1955094967 2012-5-2 0:00:0 OR No Violations
-376435608 2012-5-1 0:00:0 OR No Violations
-511940394 2012-5-3 0:00:0 OR No Violations
-587709463 2012-5-17 0:00: OR No Violations
0136721053 2012-04-30 Orphan No Violations At the time of my inspection the cable tool rig was set up on the well and 5.5 bit was ran to about 400 until an unknown obstruction was encountered. The crew is now setting up to run tubing in and circulate hole.
0376435608 2012-05-01 Orphan No Violations At the time of my inspection a new piece oc casing had to be welded on existing 8 to attach a wellhead. 2 tubing was then ran to 400 to circulate oil out of the wellbore. The tubing is starting to hang up on what we believe is a few remaining pieces of 6 surface casing around 270 (bottom of the Big Lime).
0511940394 2012-05-03 Orphan No Violations At the time of my inspection another obstruction was hit at 745 and tubing continues to hang up not only on the way down but on the way out as well. Continued circulation has produced no more oil from wellbore.
0587709463 2012-05-17 Orphan No Violations At the time of my inspection the plate has been welded on the top of casing and buried four feet below grade. The pit is also being closed and field tile is being replaced.
1337181753 2012-05-04 Plug / Plug Back No Violations Plugging Contractor is Black Swamp Oilfield Services, Mike Coyer. Plug set at TD of 744 due to the collapsing shale formation and a crooked hole. The drill pipe is catching on pieces of the surface casing still left in the hole from when it was removed. See Plug Report for details.
1337184796 2012-05-15 Plug / Plug Back No Violations On site for setting of plug 2 from 342 to 48. Cement pumped through 2 tubing with circulation of cement to surface. Fresh water formation is taking some cement so level is dropping. See Plug Report for details.
1939794195 2012-05-16 Plug / Plug Back No Violations At the time of my inspection the well was topped off from 48 to the surface with 28 sacks of Sackrete.
1955094967 2012-05-02 Orphan No Violations Rain in the area delayed continuatiun of claenout till mid afternnoon. At the time of my inspection the 2 tubing was at 452 and continued to 545. The tubing was to hang up and is getting worse as they go deeper.
2012623642 2012-12-04 Final Restoration No Violations At the time of my inspection the area was cleared of all equipment and all pits were closed. The area was then roughly graded for farm use next year. Final Restoration Passed.

For data sources see[3]

References