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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-173-61207 | | Well ID: 34-173-61207 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 41.2, -83.64 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | | + | | County: [[Wood_County,_Ohio|Wood]] |
|- | |- | ||
− | | | + | | Municipality: [[Bloom_Township,_Wood_County,_Ohio|Bloom Township]] |
|- | |- | ||
− | | | + | | Operator Name: [[HISTORIC OWNER]] |
|- | |- | ||
− | | | + | | Well Pad ID: |
|- | |- | ||
− | | | + | | Farm/Lease Name: KELLEY |
|- | |- | ||
− | | | + | | License Status: Plugged and Abandoned |
|- | |- | ||
− | | | + | | License Date: |
|- | |- | ||
− | | | + | | Spud Date: |
|- | |- | ||
− | | | + | | Spud Drilling Contractor: |
|- | |- | ||
− | | | + | | Final Drill Date: |
|- | |- | ||
− | | | + | | Well Total Depth: |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
+ | | Latitude: 41.200000 | ||
+ | |- | ||
+ | | Longitude: -83.640000 | ||
|} | |} | ||
− | == | + | For data sources see<ref>{{cite web |
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | + | !scope="col" style="text-align: center"| Well Status |
− | + | !scope="col" style="width: 15%;text-align: center"| Well Status Date | |
− | !scope="col" | + | !scope="col" style="text-align: center"| Comment |
− | + | |- | |
− | !scope="col" | + | | Oil and Gas |
− | + | | 2008-06-10 | |
− | + | | WELL INSPECTED BY KEN PIISPANEN ON 2/13/2008 TO SUBMIT TO THE I&O PROGRAM. | |
+ | |- | ||
+ | | Changed to Orphan Well Ready | ||
+ | | 2008-09-01 | ||
+ | | Changed Well To Orphan Ready | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2019-03-25 | ||
+ | | WELL INSPECTED BY KEN PIISPANEN ON 2/13/2008 TO SUBMIT TO THE I&O PROGRAM. | ||
+ | Case # 2008 09 031 UPDATED LOCATION PER DOGRM SURVEYOR 11/27/18-ALE | ||
+ | |- | ||
|} | |} | ||
− | == | + | For data sources see<ref>{{cite web |
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Perforation Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Interval Top (ft) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Interval Base (ft) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Number of Shots |
− | !scope="col" | | + | |- |
− | !scope="col" | | + | |}--> |
− | !scope="col" | | + | <!--== Fracking Activities == |
− | !scope="col" | | + | ==== Fracking Jobs ==== |
− | !scope="col" | | + | {| class="wikitable sortable" width="95%" |
− | |} | + | !scope="col" style="text-align: center"| Job Number |
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | 0692916645 | |
+ | | 2019-01-17 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | A second bottom plug was installed to this well because of the lack of fill up from the first bottom plug installed to this well on 1/15/2019. Installed 50 sacks of Class A Cement through 1.5 inch tubing. No circulation was observed during the plugging process. | ||
+ | |- | ||
+ | | 1552310964 | ||
+ | | 2019-01-15 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | Installed 40 sacks of Class A Cement through 1.5 inch tubing for the purpose of installing a bottom plug on this orphan well. No circulation was observed during the plugging process. | ||
|- | |- | ||
| 1719951254 | | 1719951254 | ||
| 2008-01-23 | | 2008-01-23 | ||
− | | | + | | Orphan |
+ | | No Violations | ||
| Well located in farm field has open 6 inch casing filled with dirt and odor of gas will be submitted to the I&O program. | | Well located in farm field has open 6 inch casing filled with dirt and odor of gas will be submitted to the I&O program. | ||
− | | | + | |- |
− | | | + | | 1889949698 |
− | | | + | | 2019-01-28 |
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | A adequate bottom plug was measured at a depth of 454 feet and it was determined to place the surface casing plug on top of the bottom plug without any spacing. Eighty sacks of Class A Cement was installed through 1.5 inch tubing and cement was briefly witnessed at the surface. After the tubing was removed this plug was measured at a depth of 30 feet . | ||
+ | |- | ||
+ | | 692916645 | ||
+ | | 2019-1-17 0:00: | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | ==References== | ||
+ | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-173-61207 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wood | |
Municipality: Bloom Township | |
Operator Name: HISTORIC OWNER | |
Well Pad ID: | |
Farm/Lease Name: KELLEY | |
License Status: Plugged and Abandoned | |
License Date: | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 41.200000 | |
Longitude: -83.640000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 2008-06-10 | WELL INSPECTED BY KEN PIISPANEN ON 2/13/2008 TO SUBMIT TO THE I&O PROGRAM. |
Changed to Orphan Well Ready | 2008-09-01 | Changed Well To Orphan Ready |
Record Last Modified | 2019-03-25 | WELL INSPECTED BY KEN PIISPANEN ON 2/13/2008 TO SUBMIT TO THE I&O PROGRAM.
Case # 2008 09 031 UPDATED LOCATION PER DOGRM SURVEYOR 11/27/18-ALE |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0692916645 | 2019-01-17 | Plug / Plug Back | No Violations | A second bottom plug was installed to this well because of the lack of fill up from the first bottom plug installed to this well on 1/15/2019. Installed 50 sacks of Class A Cement through 1.5 inch tubing. No circulation was observed during the plugging process. |
1552310964 | 2019-01-15 | Plug / Plug Back | No Violations | Installed 40 sacks of Class A Cement through 1.5 inch tubing for the purpose of installing a bottom plug on this orphan well. No circulation was observed during the plugging process. |
1719951254 | 2008-01-23 | Orphan | No Violations | Well located in farm field has open 6 inch casing filled with dirt and odor of gas will be submitted to the I&O program. |
1889949698 | 2019-01-28 | Plug / Plug Back | No Violations | A adequate bottom plug was measured at a depth of 454 feet and it was determined to place the surface casing plug on top of the bottom plug without any spacing. Eighty sacks of Class A Cement was installed through 1.5 inch tubing and cement was briefly witnessed at the surface. After the tubing was removed this plug was measured at a depth of 30 feet . |
692916645 | 2019-1-17 0:00: | PB | No Violations |
For data sources see[3]