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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-127-23757 | | Well ID: 34-127-23757 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.79, -82.08 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | Municipality: | + | | State: Ohio |
+ | |- | ||
+ | | County: [[Perry_County,_Ohio|Perry]] | ||
+ | |- | ||
+ | | Municipality: [[Harrison_Township,_Perry_County,_Ohio|Harrison Township]] | ||
|- | |- | ||
| Operator Name: [[MIDWEST OIL & GAS]] | | Operator Name: [[MIDWEST OIL & GAS]] | ||
Line 13: | Line 17: | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: CANNON ROBERT E |
|- | |- | ||
− | | | + | | License Status: Producing |
|- | |- | ||
− | | | + | | License Date: 1976-03-12 |
|- | |- | ||
| Spud Date: 1976-07-06 | | Spud Date: 1976-07-06 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: |
+ | |- | ||
+ | | Final Drill Date: 1976-08-05 | ||
+ | |- | ||
+ | | Well Total Depth: 3592.00 ft | ||
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Well Status: | + | | Latitude: 39.790000 |
+ | |- | ||
+ | | Longitude: -82.080000 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | CO | ||
+ | | 1976-03-12 | ||
+ | | 573 MIDWEST OIL & GAS GeoDate 3/12/76 | ||
+ | |- | ||
+ | | Original Spud | ||
+ | | 1976-07-06 | ||
+ | | I.P.NONE RPT. FDT/RED ROCK | ||
|- | |- | ||
− | | | + | | Completed |
+ | | 1976-08-05 | ||
+ | | I.P.NONE RPT. FDT/RED ROCK | ||
|- | |- | ||
− | | | + | | Reached Total Depth |
+ | | 1976-08-05 | ||
+ | | I.P.NONE RPT. FDT/RED ROCK | ||
|- | |- | ||
− | | | + | | Record Last Modified |
+ | | 2013-10-03 | ||
+ | | I.P.NONE RPT. FDT/RED ROCK | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Period |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Operator Name |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Gas Quantity (mcf) |
− | !scope="col" | + | !scope="col" style="text-align: center"| Oil Quantity (bbl) |
− | + | !scope="col" style="text-align: center"| Production Days | |
− | !scope="col" | ||
− | |||
|- | |- | ||
− | | 1985-0 | + | | 1985 |
− | | style="text-align:right;" | 0. | + | | [[MIDWEST OIL & GAS]] |
− | | | + | | style="text-align: right;" | 0.00 |
− | | | + | | style="text-align: right;" | 387.00 |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | + | |- |
− | | | + | | 1986 |
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 330.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 1987 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 135.00 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
+ | | 1988 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 68.00 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 1989 |
− | | style="text-align:right;" | 0. | + | | [[MIDWEST OIL & GAS]] |
− | | | + | | style="text-align: right;" | 0.00 |
− | + | | style="text-align: right;" | 217.00 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2008 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 66.00 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2009 |
− | | style="text-align:right;" | 0. | + | | [[MIDWEST OIL & GAS]] |
− | | | + | | style="text-align: right;" | 0.00 |
− | + | | style="text-align: right;" | 72.00 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2010 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 71.00 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2011 |
− | | style="text-align:right;" | 0. | + | | [[MIDWEST OIL & GAS]] |
− | | | + | | style="text-align: right;" | 0.00 |
− | + | | style="text-align: right;" | 134.00 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2012 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 165.00 | ||
+ | | style="text-align: right;" | 366 | ||
|- | |- | ||
− | | | + | |} |
− | | style="text-align: | + | For data sources see<ref>{{cite web |
− | | | + | | title = Risk Based Data Management System - Production Table - Oil and Gas Data |
− | | | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | | + | | date = 2020-11-16 |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | |
− | + | | accessdate = 2020-11-16 }}</ref> | |
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
|- | |- | ||
+ | | 1985 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 35 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 1986 |
− | | style="text-align:right;" | | + | | [[MIDWEST OIL & GAS]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 103 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 1987 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 165 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 1988 |
− | | style="text-align:right;" | 0 | + | | [[MIDWEST OIL & GAS]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 1989 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2008 |
− | | style="text-align:right;" | 0 | + | | [[MIDWEST OIL & GAS]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2009 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2010 |
− | | style="text-align:right;" | 0 | + | | [[MIDWEST OIL & GAS]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2011 | ||
+ | | [[MIDWEST OIL & GAS]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 110 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | 2012 | + | | 2012 |
− | | style="text-align:right;" | | + | | [[MIDWEST OIL & GAS]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 80 | |
− | + | | style="text-align: right;" | 366 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = Ohio Department of Natural Resources | + | | title = Risk Based Data Management System - Production Table - Brine Data |
− | | | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | -1898201587 | |
+ | | 2016-2-3 0:00:0 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | | ||
+ | |- | ||
+ | | -291788356 | ||
+ | | 2016-2-2 0:00:0 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 3.00 | ||
+ | |- | ||
+ | | -413530437 | ||
+ | | 2014-9-25 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -730140835 | ||
+ | | 2018-1-26 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.50 | ||
+ | |- | ||
+ | | 0277642619 | ||
+ | | 2011-07-28 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | No violations at this time. | ||
+ | |- | ||
+ | | 0291788356 | ||
+ | | 2016-02-02 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | There was a gas leak on 02/02/2016 that evacuated part of Crooksville. The PUCO inspector Mike Purcell that was called out on the job said the cause of the gas smell was coming from this well. During my inspection that today I found no trace of this well being fiscally able to supply enough gas to evacuate a town. The well is shut in and has been for the last two months because the pumper has been sick. The investigation will continue on 02/02/2016. | ||
+ | |- | ||
+ | | 0413530437 | ||
+ | | 2014-09-25 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | A Chiefs Order has been issued on this well for Failure to Maintain Liability Insurance. The well is capable of production at this time. The well has a pumping unit on it with rods and 2 tubing in it The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. | ||
+ | |- | ||
+ | | 0730140835 | ||
+ | | 2018-01-26 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. There are no violations at this time. | ||
+ | |- | ||
+ | | 1318597995 | ||
+ | | 2016-03-07 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | I returned to this well to do a field inspection on it to see if it was leaking any gas around the well. The production lines are hooked up to the well and are in operation. There is a flare coming off of the well to burn off exes gas. There was no heavy gas smell around the well. There are no violations to report. | ||
|- | |- | ||
| 1401521953 | | 1401521953 | ||
| 2008-12-23 | | 2008-12-23 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| No violations. | | No violations. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1450037273 | | 1450037273 | ||
| 2008-02-11 | | 2008-02-11 | ||
− | | | + | | Production Wells |
+ | | Violations Noted | ||
| An inspection of the well revealed the well is idle, no production has been reported on well since 1987, and flow line is parted in several places. No ID at the well or tank battery, need a dike around production tanks. | | An inspection of the well revealed the well is idle, no production has been reported on well since 1987, and flow line is parted in several places. No ID at the well or tank battery, need a dike around production tanks. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 1490472249 | ||
+ | | 2019-01-04 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. There are no violations at this time. | ||
+ | |- | ||
+ | | 1597696855 | ||
+ | | 2020-8-17 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.30 | ||
|- | |- | ||
| 1724906547 | | 1724906547 | ||
| 2008-04-17 | | 2008-04-17 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| Follow-up on NOV, In-Compliance. | | Follow-up on NOV, In-Compliance. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 1898201587 | ||
+ | | 2016-02-03 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | I returned to this well to continue the investigation of this gas leak with Doug Bennett, Dan Goins and Scott King all from the Division of Oil and Gas. We were accompanied by Todd Altier and Benny Altier. They are the operators of the well. During the inspection we found that this well could not be the cause of the evacuation. We inspected the surrounding area and found where Columbia Gas was working the day before on there lines. The gas smell was still coming from there transmission line and we did find more leaks in that line. We all believe the well in question was not leaking or capable of leaking since the valves are shut at the well. | ||
|- | |- | ||
| 277642619 | | 277642619 | ||
− | | 2011- | + | | 2011-7-28 0:00: |
− | | | + | | PW |
− | | No | + | | No Violations |
− | + | | 1.00 | |
− | |||
− | | | ||
|- | |- | ||
+ | |} | ||
+ | ==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
|- | |- | ||
− | | - | + | | 1450037273 |
− | | | + | | US-OH-113054 |
+ | | 2008-02-13 | ||
| | | | ||
− | | | + | | General Safety |
+ | |- | ||
+ | | 1450037273 | ||
+ | | US-OH-113055 | ||
+ | | 2008-02-13 | ||
| | | | ||
+ | | Failure to legibly identify well | ||
+ | |- | ||
+ | | 1450037273 | ||
+ | | US-OH-113056 | ||
+ | | 2008-02-13 | ||
| | | | ||
+ | | No SPCC dike/or failure to keep dike free of water or oil | ||
+ | |- | ||
+ | | 1450037273 | ||
+ | | US-OH-113057 | ||
+ | | 2008-02-13 | ||
| | | | ||
+ | | Well shall be plugged | ||
|- | |- | ||
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-127-23757 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Harrison Township | |
Operator Name: MIDWEST OIL & GAS | |
Well Pad ID: | |
Farm/Lease Name: CANNON ROBERT E | |
License Status: Producing | |
License Date: 1976-03-12 | |
Spud Date: 1976-07-06 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-08-05 | |
Well Total Depth: 3592.00 ft | |
Configuration: Vertical | |
Latitude: 39.790000 | |
Longitude: -82.080000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-03-12 | 573 MIDWEST OIL & GAS GeoDate 3/12/76 |
Original Spud | 1976-07-06 | I.P.NONE RPT. FDT/RED ROCK |
Completed | 1976-08-05 | I.P.NONE RPT. FDT/RED ROCK |
Reached Total Depth | 1976-08-05 | I.P.NONE RPT. FDT/RED ROCK |
Record Last Modified | 2013-10-03 | I.P.NONE RPT. FDT/RED ROCK |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | MIDWEST OIL & GAS | 0.00 | 387.00 | 365 |
1986 | MIDWEST OIL & GAS | 0.00 | 330.00 | 365 |
1987 | MIDWEST OIL & GAS | 0.00 | 135.00 | 365 |
1988 | MIDWEST OIL & GAS | 0.00 | 68.00 | 365 |
1989 | MIDWEST OIL & GAS | 0.00 | 217.00 | 365 |
2008 | MIDWEST OIL & GAS | 0.00 | 66.00 | 365 |
2009 | MIDWEST OIL & GAS | 0.00 | 72.00 | 365 |
2010 | MIDWEST OIL & GAS | 0.00 | 71.00 | 365 |
2011 | MIDWEST OIL & GAS | 0.00 | 134.00 | 365 |
2012 | MIDWEST OIL & GAS | 0.00 | 165.00 | 366 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | MIDWEST OIL & GAS | Brine | 35 | 365 |
1986 | MIDWEST OIL & GAS | Brine | 103 | 365 |
1987 | MIDWEST OIL & GAS | Brine | 165 | 365 |
1988 | MIDWEST OIL & GAS | Brine | 0 | 365 |
1989 | MIDWEST OIL & GAS | Brine | 0 | 365 |
2008 | MIDWEST OIL & GAS | Brine | 0 | 365 |
2009 | MIDWEST OIL & GAS | Brine | 0 | 365 |
2010 | MIDWEST OIL & GAS | Brine | 0 | 365 |
2011 | MIDWEST OIL & GAS | Brine | 110 | 365 |
2012 | MIDWEST OIL & GAS | Brine | 80 | 366 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1898201587 | 2016-2-3 0:00:0 | PW | No Violations | |
-291788356 | 2016-2-2 0:00:0 | PW | No Violations | 3.00 |
-413530437 | 2014-9-25 0:00: | PW | No Violations | 1.00 |
-730140835 | 2018-1-26 0:00: | PW | No Violations | 0.50 |
0277642619 | 2011-07-28 | Production Wells | No Violations | No violations at this time. |
0291788356 | 2016-02-02 | Production Wells | No Violations | There was a gas leak on 02/02/2016 that evacuated part of Crooksville. The PUCO inspector Mike Purcell that was called out on the job said the cause of the gas smell was coming from this well. During my inspection that today I found no trace of this well being fiscally able to supply enough gas to evacuate a town. The well is shut in and has been for the last two months because the pumper has been sick. The investigation will continue on 02/02/2016. |
0413530437 | 2014-09-25 | Production Wells | No Violations | A Chiefs Order has been issued on this well for Failure to Maintain Liability Insurance. The well is capable of production at this time. The well has a pumping unit on it with rods and 2 tubing in it The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. |
0730140835 | 2018-01-26 | Production Wells | No Violations | The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. There are no violations at this time. |
1318597995 | 2016-03-07 | Production Wells | No Violations | I returned to this well to do a field inspection on it to see if it was leaking any gas around the well. The production lines are hooked up to the well and are in operation. There is a flare coming off of the well to burn off exes gas. There was no heavy gas smell around the well. There are no violations to report. |
1401521953 | 2008-12-23 | Production Wells | No Violations | No violations. |
1450037273 | 2008-02-11 | Production Wells | Violations Noted | An inspection of the well revealed the well is idle, no production has been reported on well since 1987, and flow line is parted in several places. No ID at the well or tank battery, need a dike around production tanks. |
1490472249 | 2019-01-04 | Production Wells | No Violations | The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. There are no violations at this time. |
1597696855 | 2020-8-17 0:00: | PW | No Violations | 0.30 |
1724906547 | 2008-04-17 | Production Wells | No Violations | Follow-up on NOV, In-Compliance. |
1898201587 | 2016-02-03 | Production Wells | No Violations | I returned to this well to continue the investigation of this gas leak with Doug Bennett, Dan Goins and Scott King all from the Division of Oil and Gas. We were accompanied by Todd Altier and Benny Altier. They are the operators of the well. During the inspection we found that this well could not be the cause of the evacuation. We inspected the surrounding area and found where Columbia Gas was working the day before on there lines. The gas smell was still coming from there transmission line and we did find more leaks in that line. We all believe the well in question was not leaking or capable of leaking since the valves are shut at the well. |
277642619 | 2011-7-28 0:00: | PW | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1450037273 | US-OH-113054 | 2008-02-13 | General Safety | |
1450037273 | US-OH-113055 | 2008-02-13 | Failure to legibly identify well | |
1450037273 | US-OH-113056 | 2008-02-13 | No SPCC dike/or failure to keep dike free of water or oil | |
1450037273 | US-OH-113057 | 2008-02-13 | Well shall be plugged |
For data sources see[7]