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Difference between revisions of "34-127-24296"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-127-24296
 
| Well ID: 34-127-24296
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.67782227, -82.33390604 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.67, -82.33 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Perry County, Ohio|Perry]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Perry_County,_Ohio|Perry]]
 +
|-
 +
| Municipality: [[Jackson_Township,_Perry_County,_Ohio|Jackson Township]]
 
|-
 
|-
 
| Operator Name: [[BELL OIL]]
 
| Operator Name: [[BELL OIL]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: BELL ROBERT
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2016-10-31
 
|-
 
|-
| Spud Date:  
+
| Spud Date: 1979-03-05
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[L A MOORE & SON]]
 +
|-
 +
| Final Drill Date: 1979-05-15
 +
|-
 +
| Well Total Depth: 2870.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Not Drilled
+
| Latitude: 39.670000
 +
|-
 +
| Longitude: -82.330000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| CO
 +
| 1979-03-01
 +
| 315  BELL OIL  GeoDate  3/1/79
 
|-
 
|-
| Latitude: 39.67782227
+
| Reached Total Depth
 +
| 1979-05-15
 +
| CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE  06/20/17
 
|-
 
|-
| Longitude: -82.33390604
+
| APP
 +
| 2016-10-31
 +
| Proposed Formations:CLINTON SAND, Issued Date:10/31/2016, Expired Date:10/31/2017 12:00:00 PM, Drilling unit acres:191.9, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Plugged/Abandoned
 +
| 2017-05-25
 +
| CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE  06/20/17
 +
|-
 +
| Record Last Modified
 +
| 2017-10-23
 +
| CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE  06/20/17
 +
|-
 +
| Construction Permit Expires
 +
| 2017-10-31
 +
| CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE  06/20/17
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 1989-0
+
| 1989
| style="text-align:right;" | 1000.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 1000.00
|  
+
| style="text-align: right;" | 64.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 64.0
+
|-
|  
+
| 1990
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 73.00
 +
| style="text-align: right;" | 61.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1991
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 944.00
 +
| style="text-align: right;" | 110.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 561.00
 +
| style="text-align: right;" | 13.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1994
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 685.00
 +
| style="text-align: right;" | 28.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1995
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 100.00
 +
| style="text-align: right;" | 40.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1996
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 624.00
 +
| style="text-align: right;" | 39.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1997
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 612.00
 +
| style="text-align: right;" | 12.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1998
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 1696.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 1999
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 1134.00
 +
| style="text-align: right;" | 25.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1990-0
+
| 2000
| style="text-align:right;" | 73.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 319.00
|
+
| style="text-align: right;" | 8.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 61.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1991-0
+
| 2002
| style="text-align:right;" | 944.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 3.00
|
+
| style="text-align: right;" | 12.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 110.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1993-0
+
| 2004
| style="text-align:right;" | 561.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 13.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1994-0
+
| 2006
| style="text-align:right;" | 685.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 28.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1995-0
+
| 2008
| style="text-align:right;" | 100.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 40.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1996-0
+
| 2010
| style="text-align:right;" | 624.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 39.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1997-0
+
| 2012
| style="text-align:right;" | 612.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 366
| style="text-align:right;" | 12.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 2016
| style="text-align:right;" | 1696.0
+
| [[BELL OIL]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2017
 +
| [[BELL OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1999-0
+
|}
| style="text-align:right;" | 1134.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2020-11-16
| style="text-align:right;" | 25.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1989
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 51
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 1990
| style="text-align:right;" | 319.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 8.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 1993
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1994
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 1995
| style="text-align:right;" | 3.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 20
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 12.0
 
|
 
 
|-
 
|-
 +
| 1996
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 1997
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1998
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2004-0
+
| 1999
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 2001
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2006-0
+
| 2003
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 60
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2007-0
+
| 2005
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2007
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 2009
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2010-0
+
| 2011
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 2011-0
+
| 2015
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[BELL OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2012-0
+
| 2017
| style="text-align:right;" | 0.0
+
| [[BELL OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 547295323
+
| -119034352
 +
| 2017-5-4 0:00:0
 +
| PB
 +
| No Violations
 +
| 6.00
 +
|-
 +
| -2031514435
 +
| 2017-4-21 0:00:
 +
| PB
 +
| No Violations
 +
| 5.00
 +
|-
 +
| -267875149
 +
| 2017-5-9 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -520238473
 +
| 2017-5-12 0:00:
 +
| PB
 +
| No Violations
 +
| 3.00
 +
|-
 +
| 0119034352
 +
| 2017-05-04
 +
| Plug / Plug Back
 +
| No Violations
 +
| I returned to this well to check on the plugging of it. They were not able to retrieve the ripping tools from the well but they were able to get back down the hole to rip the casing at 1800 feet. After ripping the casing the rig crew pulled out one joint of the casing to wash in the 500 foot Lime plug.
 +
|-
 +
| 0223512889
 +
| 2017-04-25
 +
| Plug / Plug Back
 +
| No Violations
 +
| I stopped by the well today to see if the rig crew was ready to start ripping the 4.5 inch diameter casing. The rig crew was not on location during my field inspection.
 +
|-
 +
| 0248120119
 +
| 2017-05-08
 +
| Plug / Plug Back
 +
| No Violations
 +
| I returned to this well to witness the plugging of the well. Today the rig crew ran the 7 inch pre-cast plug in down to the 7 inch seat. They tagged the plug down at 910 feet. At this point the rig crew started washing in the plugging clay up to the bottom of the 8 inch surface casing.
 +
|-
 +
| 0267875149
 +
| 2017-05-09
 +
| Plug / Plug Back
 +
| No Violations
 +
| I returned to this well today to witness the plugging of it. While washing in the clay plug on top of the 7 inch seat the clay bridged off in the 8 inch casing. The rig crew are working on washing out the clay with a pump at this time.
 +
|-
 +
| 0454818001
 +
| 2017-04-27
 +
| Plug / Plug Back
 +
| No Violations
 +
| I went out on location today while the rig crew tried to rip the 4.5 inch diameter casing. They had trouble getting the tools down the hole. After working on it for a while they were able to get down the casing. While trying to rip the casing the ripping tools got stuck in the casing at 1900 feet. The cable ended up breaking and the tools were lost in the hole at 1900 feet. The rig crew tried working on retrieving the ripping tools after this.
 +
|-
 +
| 0520238473
 +
| 2017-05-12
 +
| Plug / Plug Back
 +
| No Violations
 +
| I was on location today to witness the rig crew washing in more clay onto the top of the 7 inch seat. They will bring the clay plug up to the bottom of the 8 inch surface casing before they work on retrieving the casing.
 +
|-
 +
| 0547295323
 
| 2009-01-26
 
| 2009-01-26
|  
+
| Production Wells
 +
| No Violations
 
| No violations.
 
| No violations.
 +
|-
 +
| 0666136622
 +
| 2017-05-25
 +
| Plug / Plug Back
 +
| No Violations
 +
| I returned to this well today to check to see if the clay was still at the surface. The clay has not settled so I let the company know that they could work on reclaiming this location.
 +
|-
 +
| 1494589793
 +
| 2017-05-11
 +
| Plug / Plug Back
 +
| No Violations
 +
| I stopped by the location first thing this morning to see how things were coming along on this job. The rig crew is just working on cleaning up the hole today. They plan on washing in more clay tomorrow.
 +
|-
 +
| 1495022348
 +
| 2017-05-17
 +
| Plug / Plug Back
 +
| No Violations
 +
| I stopped by this well today to check on the plugging operations. The rig crew is working on getting the rest of the 8 inch diameter casing out of the well at this time. They ended up retrieving all of the 8 inch casing from the well.
 +
|-
 +
| 1796952738
 +
| 2017-08-14
 +
| Final Restoration
 +
| No Violations
 +
| The final restoration meets 1509.072(B) requirements.
 +
|-
 +
| 2031514435
 +
| 2017-04-21
 +
| Plug / Plug Back
 +
| No Violations
 +
| I was on location today to witness the plugging of this well. Today the company set a 500 foot bottom plug with plugging clay through the 4.5 inch diameter casing. They will rip the 4.5 inch casing next week.
 +
|-
 +
| 223512889
 +
| 2017-4-25 0:00:
 +
| PB
 +
| No Violations
 +
| 1.00
 +
|-
 +
| 248120119
 +
| 2017-5-8 0:00:0
 +
| PB
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| 454818001
 +
| 2017-4-27 0:00:
 +
| PB
 +
| No Violations
 +
| 6.00
 +
|-
 +
| 547295323
 +
| 2009-1-26 0:00:
 +
| PW
 +
| No Violations
 
|  
 
|  
|  
+
|-
 +
| 666136622
 +
| 2017-5-25 0:00:
 +
| PB
 +
| No Violations
 +
| 1.00
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 12:17, 12 January 2021

Well Details

Well ID: 34-127-24296
Loading map...
Country: United States
State: Ohio
County: Perry
Municipality: Jackson Township
Operator Name: BELL OIL
Well Pad ID:
Farm/Lease Name: BELL ROBERT
License Status: Final Restoration
License Date: 2016-10-31
Spud Date: 1979-03-05
Spud Drilling Contractor: L A MOORE & SON
Final Drill Date: 1979-05-15
Well Total Depth: 2870.00 ft
Configuration: Vertical
Latitude: 39.670000
Longitude: -82.330000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-03-01 315 BELL OIL GeoDate 3/1/79
Reached Total Depth 1979-05-15 CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17
APP 2016-10-31 Proposed Formations:CLINTON SAND, Issued Date:10/31/2016, Expired Date:10/31/2017 12:00:00 PM, Drilling unit acres:191.9, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-05-25 CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17
Record Last Modified 2017-10-23 CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17
Construction Permit Expires 2017-10-31 CHANGED STATUS TO PR BASED ON COMPLETION AND PRODUCTION DATA-TE 10/20/16; UPDATED RECORD WITH WCR INFO. 12/2/16 MM UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 BELL OIL 1000.00 64.00 365
1990 BELL OIL 73.00 61.00 365
1991 BELL OIL 944.00 110.00 365
1993 BELL OIL 561.00 13.00 365
1994 BELL OIL 685.00 28.00 365
1995 BELL OIL 100.00 40.00 365
1996 BELL OIL 624.00 39.00 365
1997 BELL OIL 612.00 12.00 365
1998 BELL OIL 1696.00 0.00 365
1999 BELL OIL 1134.00 25.00 365
2000 BELL OIL 319.00 8.00 365
2001 BELL OIL 0.00 0.00 365
2002 BELL OIL 3.00 12.00 365
2003 BELL OIL 0.00 0.00 365
2004 BELL OIL 0.00 0.00 365
2005 BELL OIL 0.00 0.00 365
2006 BELL OIL 0.00 0.00 365
2007 BELL OIL 0.00 0.00 365
2008 BELL OIL 0.00 0.00 365
2009 BELL OIL 0.00 0.00 365
2010 BELL OIL 0.00 0.00 365
2011 BELL OIL 0.00 0.00 365
2012 BELL OIL 0.00 0.00 366
2015 BELL OIL 0.00 0.00 365
2016 BELL OIL 0.00 0.00 0
2017 BELL OIL 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 BELL OIL Brine 51 365
1990 BELL OIL Brine 0 365
1991 BELL OIL Brine 0 365
1993 BELL OIL Brine 0 365
1994 BELL OIL Brine 0 365
1995 BELL OIL Brine 20 365
1996 BELL OIL Brine 0 365
1997 BELL OIL Brine 0 365
1998 BELL OIL Brine 0 365
1999 BELL OIL Brine 0 365
2000 BELL OIL Brine 0 365
2001 BELL OIL Brine 0 365
2002 BELL OIL Brine 0 365
2003 BELL OIL Brine 60 365
2004 BELL OIL Brine 0 365
2005 BELL OIL Brine 0 365
2006 BELL OIL Brine 0 365
2007 BELL OIL Brine 0 365
2008 BELL OIL Brine 0 365
2009 BELL OIL Brine 0 365
2010 BELL OIL Brine 0 365
2011 BELL OIL Brine 0 365
2012 BELL OIL Brine 0 366
2015 BELL OIL Brine 0 365
2016 BELL OIL Brine 0 0
2017 BELL OIL Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-119034352 2017-5-4 0:00:0 PB No Violations 6.00
-2031514435 2017-4-21 0:00: PB No Violations 5.00
-267875149 2017-5-9 0:00:0 PB No Violations
-520238473 2017-5-12 0:00: PB No Violations 3.00
0119034352 2017-05-04 Plug / Plug Back No Violations I returned to this well to check on the plugging of it. They were not able to retrieve the ripping tools from the well but they were able to get back down the hole to rip the casing at 1800 feet. After ripping the casing the rig crew pulled out one joint of the casing to wash in the 500 foot Lime plug.
0223512889 2017-04-25 Plug / Plug Back No Violations I stopped by the well today to see if the rig crew was ready to start ripping the 4.5 inch diameter casing. The rig crew was not on location during my field inspection.
0248120119 2017-05-08 Plug / Plug Back No Violations I returned to this well to witness the plugging of the well. Today the rig crew ran the 7 inch pre-cast plug in down to the 7 inch seat. They tagged the plug down at 910 feet. At this point the rig crew started washing in the plugging clay up to the bottom of the 8 inch surface casing.
0267875149 2017-05-09 Plug / Plug Back No Violations I returned to this well today to witness the plugging of it. While washing in the clay plug on top of the 7 inch seat the clay bridged off in the 8 inch casing. The rig crew are working on washing out the clay with a pump at this time.
0454818001 2017-04-27 Plug / Plug Back No Violations I went out on location today while the rig crew tried to rip the 4.5 inch diameter casing. They had trouble getting the tools down the hole. After working on it for a while they were able to get down the casing. While trying to rip the casing the ripping tools got stuck in the casing at 1900 feet. The cable ended up breaking and the tools were lost in the hole at 1900 feet. The rig crew tried working on retrieving the ripping tools after this.
0520238473 2017-05-12 Plug / Plug Back No Violations I was on location today to witness the rig crew washing in more clay onto the top of the 7 inch seat. They will bring the clay plug up to the bottom of the 8 inch surface casing before they work on retrieving the casing.
0547295323 2009-01-26 Production Wells No Violations No violations.
0666136622 2017-05-25 Plug / Plug Back No Violations I returned to this well today to check to see if the clay was still at the surface. The clay has not settled so I let the company know that they could work on reclaiming this location.
1494589793 2017-05-11 Plug / Plug Back No Violations I stopped by the location first thing this morning to see how things were coming along on this job. The rig crew is just working on cleaning up the hole today. They plan on washing in more clay tomorrow.
1495022348 2017-05-17 Plug / Plug Back No Violations I stopped by this well today to check on the plugging operations. The rig crew is working on getting the rest of the 8 inch diameter casing out of the well at this time. They ended up retrieving all of the 8 inch casing from the well.
1796952738 2017-08-14 Final Restoration No Violations The final restoration meets 1509.072(B) requirements.
2031514435 2017-04-21 Plug / Plug Back No Violations I was on location today to witness the plugging of this well. Today the company set a 500 foot bottom plug with plugging clay through the 4.5 inch diameter casing. They will rip the 4.5 inch casing next week.
223512889 2017-4-25 0:00: PB No Violations 1.00
248120119 2017-5-8 0:00:0 PB No Violations
454818001 2017-4-27 0:00: PB No Violations 6.00
547295323 2009-1-26 0:00: PW No Violations
666136622 2017-5-25 0:00: PB No Violations 1.00

For data sources see[7]

References