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Difference between revisions of "34-099-22776"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-099-22776
 
| Well ID: 34-099-22776
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.10796204, -80.74547917 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.1, -80.74 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Mahoning County, Ohio|Mahoning]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[ENERGY RESOURCES AMERICA]]
+
| County: [[Mahoning_County,_Ohio|Mahoning]]
 +
|-
 +
| Municipality: [[Austintown_Township,_Mahoning_County,_Ohio|Austintown Township]]
 +
|-
 +
| Operator Name: [[ENERGY RESOURCES OF AMERICA IN]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: TOBIN
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1997-10-20
 
|-
 
|-
 
| Spud Date: 1997-10-30
 
| Spud Date: 1997-10-30
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[ADVENT DRLG]]
 +
|-
 +
| Final Drill Date: 1997-11-06
 +
|-
 +
| Well Total Depth: 5300.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 41.100000
 +
|-
 +
| Longitude: -80.740000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| APP
 +
| 1997-10-20
 +
| Proposed Formations:CLINTON, Issued Date:10/20/97, Expired Date:10/20/98 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
 +
|-
 +
| Original Spud
 +
| 1997-10-30
 +
| RBDMS Rec
 
|-
 
|-
| Violations: 0
+
| Completed
 +
| 1997-11-06
 +
| RBDMS Rec
 
|-
 
|-
| Latitude: 41.10796204
+
| Reached Total Depth
 +
| 1997-11-06
 +
| RBDMS Rec
 
|-
 
|-
| Longitude: -80.74547917
+
| Completion Report Received
 +
| 1998-04-13
 +
| RBDMS Rec
 +
|-
 +
| Construction Permit Expires
 +
| 1998-10-20
 +
| RBDMS Rec
 +
|-
 +
| Record Last Modified
 +
| 2017-02-15
 +
| RBDMS Rec
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | CONDENSATE PRODUCTION DAYS
+
|-
!scope="col" | OIL QUANTITY
+
| 1998-06-24
!scope="col" | OIL PRODUCTION DAYS
+
| style="text-align: right;" | 5125
 +
| style="text-align: right;" | 5200
 +
| style="text-align: right;" | 52
 
|-
 
|-
| 1997-0
 
| style="text-align:right;" | 0.0
 
 
|  
 
|  
 +
| style="text-align: right;" | 5125
 +
| style="text-align: right;" | 5200
 +
| style="text-align: right;" | 52
 +
|-
 
|  
 
|  
 +
| style="text-align: right;" | 5125
 +
| style="text-align: right;" | 5200
 +
| style="text-align: right;" | 52
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 
|  
 
|  
| style="text-align:right;" | 0.0
+
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 78500 Gal
 +
| style="text-align: right;" | 27000
 
|  
 
|  
 +
| 800 GALLONS IC ACID
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1997
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1998-0
+
| 1998
| style="text-align:right;" | 5190.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|  
+
| style="text-align: right;" | 5190.00
|  
+
| style="text-align: right;" | 807.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 807.0
+
|-
|  
+
| 2000
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 2468.00
 +
| style="text-align: right;" | 146.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 1308.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2002
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 1235.00
 +
| style="text-align: right;" | 140.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2003
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 1019.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2004
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 595.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2005
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 464.00
 +
| style="text-align: right;" | 76.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2006
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 537.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2007
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 330.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2008
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 457.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2009
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 451.00
 +
| style="text-align: right;" | 53.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2010
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 243.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 2011
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 451.00
 +
| style="text-align: right;" | 121.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 2012
| style="text-align:right;" | 2468.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|  
+
| style="text-align: right;" | 908.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 366
| style="text-align:right;" | 146.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 232.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 2014
| style="text-align:right;" | 1308.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|  
+
| style="text-align: right;" | 252.00
|
+
| style="text-align: right;" | 44.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 2016
| style="text-align:right;" | 1235.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|  
+
| style="text-align: right;" | 35.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 140.0
 
|
 
 
|-
 
|-
 +
| 2017
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 2018
| style="text-align:right;" | 1019.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 2004-0
+
| 1997
| style="text-align:right;" | 595.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 1719
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1998
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 118
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 2000
| style="text-align:right;" | 464.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 45
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 76.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 38
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2006-0
+
| 2002
| style="text-align:right;" | 537.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2007-0
+
| 2004
| style="text-align:right;" | 330.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2006
| style="text-align:right;" | 457.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 2008
| style="text-align:right;" | 451.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 53.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2010-0
+
| 2010
| style="text-align:right;" | 243.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2011-0
+
| 2012
| style="text-align:right;" | 451.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 30
|
+
| style="text-align: right;" | 366
| style="text-align:right;" | 121.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2012-0
+
| 2014
| style="text-align:right;" | 908.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2013-0
+
| 2016
| style="text-align:right;" | 232.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2017
 +
| [[ENERGY RESOURCES OF AMERICA IN]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2014-0
+
| 2018
| style="text-align:right;" | 252.0
+
| [[ENERGY RESOURCES OF AMERICA IN]]
| style="text-align:right;" | 365.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 44.0
 
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| -1671440792
 +
| 2005-6-2 0:00:0
 +
| PW
 +
| No Violations
 +
| 0.50
 
|-
 
|-
 
| 1259937555
 
| 1259937555
 
| 2009-12-04
 
| 2009-12-04
|  
+
| Production Wells
 +
| No Violations
 
| I performed a NOV follow-up.  Nothing has been done yet.  I went to the Energy Resources of America office and talked with Joe Glista and Kelly Koval.  Mr. Glista stated that the 50 barrel plastic tank will be replaced and the dike area cleaned up tomorrow.  This case continues.
 
| I performed a NOV follow-up.  Nothing has been done yet.  I went to the Energy Resources of America office and talked with Joe Glista and Kelly Koval.  Mr. Glista stated that the 50 barrel plastic tank will be replaced and the dike area cleaned up tomorrow.  This case continues.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1260798488
 
| 1260798488
 
| 2009-12-09
 
| 2009-12-09
|  
+
| Production Wells
 +
| No Violations
 
| I performed a NOV follow-up.  The 50 barrel plastic tank had been replaced and the dike area cleaned up.  This case is resolved.
 
| I performed a NOV follow-up.  The 50 barrel plastic tank had been replaced and the dike area cleaned up.  This case is resolved.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1431358545
 
| 1431358545
 
| 2011-08-12
 
| 2011-08-12
|  
+
| Production Wells
 +
| No Violations
 
| Received call on 08/12/2011 from Austintown, OH Fire Inspector Lt. Rick Millirn (330-799-8502) in regards to homeowner complaints of gas odors from well. I inspected well head and tank battery and walked local area. Did not notice any signs of leaks or spills and did not detect any odor related to oil/gas leaks. Spoke with Joe Glista (330-953-1813) of Energy Resources America on 08/12/2011 in regards to complaint. Glista reported that he had a truck on site that morning to collect oil from stock tank.  I relayed this information to Lt. Millirn via voicemail. No violations at this time, complaint resolved.
 
| Received call on 08/12/2011 from Austintown, OH Fire Inspector Lt. Rick Millirn (330-799-8502) in regards to homeowner complaints of gas odors from well. I inspected well head and tank battery and walked local area. Did not notice any signs of leaks or spills and did not detect any odor related to oil/gas leaks. Spoke with Joe Glista (330-953-1813) of Energy Resources America on 08/12/2011 in regards to complaint. Glista reported that he had a truck on site that morning to collect oil from stock tank.  I relayed this information to Lt. Millirn via voicemail. No violations at this time, complaint resolved.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1598357322
 
| 1598357322
 
| 2009-11-25
 
| 2009-11-25
|  
+
| Production Wells
 +
| Violations Noted
 
| I performed a well inspection.  The50 barrel plastic brine tank inside the dike has a 4 inch hole, 12 inches from the bottom.  The brine inside was leaking outside the tank.  I drove to the Energy Recourses office in Austintown and talked to Joe Klista Jr.(field superintendent) about the hole in the brine tank.  He would get a water truck to vacuum out the brine and replace the tank.  I would check back next week.  This NOV continues.
 
| I performed a well inspection.  The50 barrel plastic brine tank inside the dike has a 4 inch hole, 12 inches from the bottom.  The brine inside was leaking outside the tank.  I drove to the Energy Recourses office in Austintown and talked to Joe Klista Jr.(field superintendent) about the hole in the brine tank.  He would get a water truck to vacuum out the brine and replace the tank.  I would check back next week.  This NOV continues.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1671440792
| -1671440792
 
 
| 2005-06-02
 
| 2005-06-02
|  
+
| Production Wells
 +
| No Violations
 
| The tank battery consists of 1-100 bbl storage tank, 1-1,300 gallon plastic salt water tank, 1-separator and a dike.
 
| The tank battery consists of 1-100 bbl storage tank, 1-1,300 gallon plastic salt water tank, 1-separator and a dike.
 +
|-
 +
| iDIAN00033
 +
| 1998-11-03
 +
| Preliminary Restoration
 +
| No Violations
 
|  
 
|  
|  
+
|-
 +
| iDIAN000337
 +
| 1998-11-3 0:00:
 +
| PL
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| iDIAN000337
+
| 1598357322
| 1998-11-03
+
| US-OH-115652
|
+
| 2009-11-24
|
 
|
 
|  
 
 
|  
 
|  
 +
| Well operation causing pollution and contamination
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 15:31, 12 January 2021

Well Details

Well ID: 34-099-22776
Loading map...
Country: United States
State: Ohio
County: Mahoning
Municipality: Austintown Township
Operator Name: ENERGY RESOURCES OF AMERICA IN
Well Pad ID:
Farm/Lease Name: TOBIN
License Status: Producing
License Date: 1997-10-20
Spud Date: 1997-10-30
Spud Drilling Contractor: ADVENT DRLG
Final Drill Date: 1997-11-06
Well Total Depth: 5300.00 ft
Configuration: Vertical
Latitude: 41.100000
Longitude: -80.740000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 1997-10-20 Proposed Formations:CLINTON, Issued Date:10/20/97, Expired Date:10/20/98 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 1997-10-30 RBDMS Rec
Completed 1997-11-06 RBDMS Rec
Reached Total Depth 1997-11-06 RBDMS Rec
Completion Report Received 1998-04-13 RBDMS Rec
Construction Permit Expires 1998-10-20 RBDMS Rec
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1998-06-24 5125 5200 52
5125 5200 52
5125 5200 52

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 78500 Gal 27000 800 GALLONS IC ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1997 ENERGY RESOURCES OF AMERICA IN 0.00 0.00 0
1998 ENERGY RESOURCES OF AMERICA IN 5190.00 807.00 365
2000 ENERGY RESOURCES OF AMERICA IN 2468.00 146.00 365
2001 ENERGY RESOURCES OF AMERICA IN 1308.00 0.00 365
2002 ENERGY RESOURCES OF AMERICA IN 1235.00 140.00 365
2003 ENERGY RESOURCES OF AMERICA IN 1019.00 0.00 365
2004 ENERGY RESOURCES OF AMERICA IN 595.00 0.00 365
2005 ENERGY RESOURCES OF AMERICA IN 464.00 76.00 365
2006 ENERGY RESOURCES OF AMERICA IN 537.00 0.00 365
2007 ENERGY RESOURCES OF AMERICA IN 330.00 0.00 365
2008 ENERGY RESOURCES OF AMERICA IN 457.00 0.00 365
2009 ENERGY RESOURCES OF AMERICA IN 451.00 53.00 365
2010 ENERGY RESOURCES OF AMERICA IN 243.00 0.00 365
2011 ENERGY RESOURCES OF AMERICA IN 451.00 121.00 365
2012 ENERGY RESOURCES OF AMERICA IN 908.00 0.00 366
2013 ENERGY RESOURCES OF AMERICA IN 232.00 0.00 365
2014 ENERGY RESOURCES OF AMERICA IN 252.00 44.00 365
2015 ENERGY RESOURCES OF AMERICA IN 0.00 0.00 365
2016 ENERGY RESOURCES OF AMERICA IN 35.00 0.00 365
2017 ENERGY RESOURCES OF AMERICA IN 0.00 0.00 365
2018 ENERGY RESOURCES OF AMERICA IN 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1997 ENERGY RESOURCES OF AMERICA IN Brine 1719 0
1998 ENERGY RESOURCES OF AMERICA IN Brine 118 365
2000 ENERGY RESOURCES OF AMERICA IN Brine 45 365
2001 ENERGY RESOURCES OF AMERICA IN Brine 38 365
2002 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2003 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2004 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2005 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2006 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2007 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2008 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2009 ENERGY RESOURCES OF AMERICA IN Brine 15 365
2010 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2011 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2012 ENERGY RESOURCES OF AMERICA IN Brine 30 366
2013 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2014 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2015 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2016 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2017 ENERGY RESOURCES OF AMERICA IN Brine 0 365
2018 ENERGY RESOURCES OF AMERICA IN Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1671440792 2005-6-2 0:00:0 PW No Violations 0.50
1259937555 2009-12-04 Production Wells No Violations I performed a NOV follow-up. Nothing has been done yet. I went to the Energy Resources of America office and talked with Joe Glista and Kelly Koval. Mr. Glista stated that the 50 barrel plastic tank will be replaced and the dike area cleaned up tomorrow. This case continues.
1260798488 2009-12-09 Production Wells No Violations I performed a NOV follow-up. The 50 barrel plastic tank had been replaced and the dike area cleaned up. This case is resolved.
1431358545 2011-08-12 Production Wells No Violations Received call on 08/12/2011 from Austintown, OH Fire Inspector Lt. Rick Millirn (330-799-8502) in regards to homeowner complaints of gas odors from well. I inspected well head and tank battery and walked local area. Did not notice any signs of leaks or spills and did not detect any odor related to oil/gas leaks. Spoke with Joe Glista (330-953-1813) of Energy Resources America on 08/12/2011 in regards to complaint. Glista reported that he had a truck on site that morning to collect oil from stock tank. I relayed this information to Lt. Millirn via voicemail. No violations at this time, complaint resolved.
1598357322 2009-11-25 Production Wells Violations Noted I performed a well inspection. The50 barrel plastic brine tank inside the dike has a 4 inch hole, 12 inches from the bottom. The brine inside was leaking outside the tank. I drove to the Energy Recourses office in Austintown and talked to Joe Klista Jr.(field superintendent) about the hole in the brine tank. He would get a water truck to vacuum out the brine and replace the tank. I would check back next week. This NOV continues.
1671440792 2005-06-02 Production Wells No Violations The tank battery consists of 1-100 bbl storage tank, 1-1,300 gallon plastic salt water tank, 1-separator and a dike.
iDIAN00033 1998-11-03 Preliminary Restoration No Violations
iDIAN000337 1998-11-3 0:00: PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1598357322 US-OH-115652 2009-11-24 Well operation causing pollution and contamination

For data sources see[9]

References