X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-101-20221"

m
m
 
(4 intermediate revisions by the same user not shown)
Line 1: Line 1:
__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-101-20221
 
| Well ID: 34-101-20221
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.59951081, -82.96389264 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.59, -82.96 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Marion County, Ohio|Marion]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Marion_County,_Ohio|Marion]]
 +
|-
 +
| Municipality: [[Claridon_Township,_Marion_County,_Ohio|Claridon Township]]
 
|-
 
|-
 
| Operator Name: [[GEOPETRO LLC]]
 
| Operator Name: [[GEOPETRO LLC]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: MCCLENATHAN (ERP #1)
 
|-
 
|-
| First Permit Date:  
+
| License Status: Well Drilled
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2013-09-17
 
|-
 
|-
 
| Spud Date: 2013-06-27
 
| Spud Date: 2013-06-27
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[KILBARGER DRLG]]
 +
|-
 +
| Final Drill Date: 2013-07-05
 +
|-
 +
| Well Total Depth: 2967.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Well Drilled
+
| Latitude: 40.590000
 +
|-
 +
| Longitude: -82.960000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| APP
 +
| 2013-05-17
 +
| Proposed Formations:TRENTON, BLACK RIVER, TREMPEALEAU, Issued Date:5/17/2013, Expired Date:5/17/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
 
|-
 
|-
| Latitude: 40.59951081
+
| Reached Total Depth
 +
| 2013-07-05
 +
| WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
 
|-
 
|-
| Longitude: -82.96389264
+
| Completion Report Received
 +
| 2013-08-05
 +
| WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
 +
|-
 +
| APP
 +
| 2013-09-17
 +
| Proposed Formations:TREMPEALEAU, Issued Date:9/17/2013, Expired Date:9/17/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:EOR, Proposed Well Class:ERP
 +
|-
 +
| Last Compliance Report
 +
| 2013-09-17
 +
| WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
 +
|-
 +
| Construction Permit Expires
 +
| 2015-09-17
 +
| WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
 +
|-
 +
| Record Last Modified
 +
| 2017-02-10
 +
| WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2018
 +
| [[GEOPETRO LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2018
 +
| [[GEOPETRO LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 1031143440
+
| -1191041472
| 2013-06-13
+
| 2013-6-30 0:00:
 +
| DD
 +
| No Violations
 +
|
 +
|-
 +
| -1299892688
 +
| 2013-7-3 0:00:0
 +
| DD
 +
| No Violations
 
|  
 
|  
| Kilbarger #5 moving to location on hold pending weather.
+
|-
 +
| -1379847428
 +
| 2016-1-19 0:00:
 +
| SW
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -1481601637
 +
| 2013-7-1 0:00:0
 +
| DD
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -1715185059
 +
| 2014-1-13 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
| -1736952180
 +
| 2017-1-19 0:00:
 +
| ER
 +
| No Violations
 +
|
 
|-
 
|-
| -1191041472
+
| -1773584388
| 2013-06-30
+
| 2015-9-1 0:00:0
 +
| WR
 +
| No Violations
 
|  
 
|  
| Kilbarger #5 switch to fluid at 1030'. Making too much water from Newburg.
+
|-
 +
| -1928257551
 +
| 2017-4-11 0:00:
 +
| SW
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -1958594937
 +
| 2013-8-26 0:00:
 +
| CS
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -1962444657
 +
| 2014-5-27 0:00:
 +
| PL
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
| -1963472042
 +
| 2014-7-28 0:00:
 +
| ER
 +
| No Violations
 +
|
 
|-
 
|-
| -1299892688
+
| -252823231
| 2013-07-03
+
| 2019-1-8 0:00:0
 +
| DD
 +
| No Violations
 
|  
 
|  
| Kilbarger #5 Tripping at 1965'.
+
|-
 +
| -257577080
 +
| 2020-1-14 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -309574765
 +
| 2016-7-26 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -494604358
 +
| 2015-9-18 0:00:
 +
| WR
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
| -552416882
 +
| 2015-9-9 0:00:0
 +
| ER
 +
| No Violations
 +
|
 
|-
 
|-
| 1370539779
+
| -595351781
| 2013-06-06
+
| 2014-7-30 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
| Mason Drilling has removed the topsoil and stoned the entrance way off  state route 746.
+
|-
 +
| -673817450
 +
| 2013-6-5 0:00:0
 +
| DD
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -699918834
 +
| 2018-8-23 0:00:
 +
| SW
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -770357554
 +
| 2015-9-15 0:00:
 +
| WR
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
| -777938658
 +
| 2019-10-30 0:00
 +
| ER
 +
| No Violations
 +
|
 
|-
 
|-
| 1370878599
+
| -800620239
| 2013-06-10
+
| 2014-12-9 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
| Waiting on Kilbarger #5.
+
|-
 +
| -857888275
 +
| 2015-11-9 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -929164922
 +
| 2014-5-27 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| 0061138679
 +
| 2015-09-15
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Mason Service Rig in on the well for conversion.
 +
|-
 +
| 0309574765
 +
| 2016-07-26
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. The well is behind corn. A flow line has not been installed as of this date. The well is shut in and authorization has not been granted to utilize the well.
 +
|-
 +
| 0353620797
 +
| 2015-09-17
 +
| Work Over Reconditioning
 +
| No Violations
 +
| Inspect well. The cement shoe has been drilled out. The tubing with drill bit were tripped out of the hole. The same tubing was run in the hole with a rebuilt Halliburton R-4 packer with a 6 foot pup joint set in compression. The tubing is used barely.
 +
|-
 +
| 0494604358
 +
| 2015-09-18
 +
| Work Over Reconditioning
 +
| No Violations
 +
| The packer and tubing were run in the hole. The cement shoe was displaced to 2785 feet. The packer was set at 2770 with 2-3/8 inch EUE upset tubing at 4.7 pounds per foot. There were 10 joints left on the rack when the job was complete.  The string weight was about 13,019 pounds. The packer was set in tension with 23,000 pounds of stretch. The annulus was loaded with water with inhibitor and pressure tested. The test passed with less than two percent loss in pressure.
 +
|-
 +
| 0552416882
 +
| 2015-09-09
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| The operator has moved a dozer onto location in preparation for conversion.
 +
|-
 +
| 0595351781
 +
| 2014-07-30
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well for integrity and pressure. The well has not been completed for salt water injection.
 +
|-
 +
| 0616635339
 +
| 2018-02-08
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. No activity or contact has been made by the operator since previous inspection. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
 +
|-
 +
| 0673817450
 +
| 2013-06-05
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Mason drilling has begun building the location.
 +
|-
 +
| 0699918834
 +
| 2018-08-23
 +
| Salt Water Injection Well
 +
| No Violations
 +
| Inspect location. The well is behind corn.
 +
|-
 +
| 0750438715
 +
| 2014-01-22
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Location Information. ENTRANCE: Lat. 40.59962  Long. -82.96249 / WELL HEAD: Lat. 40.59952  Long.  -82.96388  / CENTER-OF-STORAGE: no storage built at the time of inspection.
 +
|-
 +
| 0770357554
 +
| 2015-09-15
 +
| Work Over Reconditioning
 +
| No Violations
 +
| Jet Wireline on location to perform a cement bond log to determine the top of cement circulated for 4.5 inch production casing.  Service rig mobilized onto location.
 +
|-
 +
| 0772267980
 +
| 2017-12-22
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. The tubing and packer were installed and MIT tested on September 18, 2015. The proposed flow line from the water source, Mcclenathan #1; 3410120219, has not been installed.  The operator has not requested initial operation status. This well is incapable of operation and is idle.
 +
|-
 +
| 0800620239
 +
| 2014-12-09
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspected the McClenathan #2 (ERP #221) as part of a standard injection well status check. Inspect well, storage and identification. Status: no change in status from previous inspection.
 +
|-
 +
| 0857888275
 +
| 2015-11-09
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well for integrity and pressure. The well is shut in and flow line has not been installed.
 +
|-
 +
| 0929164922
 +
| 2014-05-27
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check. Status: no change in status from previous inspection.
 +
|-
 +
| 1031143440
 +
| 2013-06-13
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Kilbarger #5 moving to location on hold pending weather.
 +
|-
 +
| 1128082576
 +
| 2020-4-8 0:00:0
 +
| ER
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
| 1191041472
 +
| 2013-06-30
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Kilbarger #5 switch to fluid at 1030. Making too much water from Newburg.
 +
|-
 +
| 1205476676
 +
| 2015-09-22
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Mason service rig has left the location. Conversion process continues.
 +
|-
 +
| 1284406160
 +
| 2016-11-15
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. A flow line has not been installed as of this date. The well is shut in and authorization has not been granted to utilize the well. Currently no access is available to the tubing.
 +
|-
 +
| 1299892688
 +
| 2013-07-03
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Kilbarger #5 Tripping at 1965.
 +
|-
 +
| 1370539779
 +
| 2013-06-06
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Mason Drilling has removed the topsoil and stoned the entrance way off  state route 746.
 +
|-
 +
| 1370878599
 +
| 2013-06-10
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Waiting on Kilbarger #5.
 
|-
 
|-
 
| 1372268945
 
| 1372268945
 
| 2013-06-26
 
| 2013-06-26
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Kilbarger #5 moving on location and rigging up. Spud:
 
| Kilbarger #5 moving on location and rigging up. Spud:
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1372269857
 
| 1372269857
 
| 2013-06-26
 
| 2013-06-26
|  
+
| Brine Hauler
 +
| No Violations
 
| Accompany Mullins Energy services brine truck to collect fresh water for the drilling rig. Status: ok.
 
| Accompany Mullins Energy services brine truck to collect fresh water for the drilling rig. Status: ok.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1372351028
 
| 1372351028
 
| 2013-06-27
 
| 2013-06-27
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Kilbarger #5 spud 10:00 pm 6/26/2013 with 8.75 drill bit on fresh water mud.
 
| Kilbarger #5 spud 10:00 pm 6/26/2013 with 8.75 drill bit on fresh water mud.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1372382768
 
| 1372382768
 
| 2013-06-27
 
| 2013-06-27
|  
+
| Casing String Witnessed
| Kilbarger #5 reach total depth on the surface hole on fluid at 334 feet at 6:20 pm 6/27/2013, drillers top of Big Lime 238'. No lost circulation zones or fluid loss while drilling noted. Ran 10 joints of new and used/tested 17 pound, 7 inch surface casing. Two new joints on bottom with guide shoe and two new joints on top landed with a 10 foot landing joint. Ran 307' set at 317'. Petroset hooked up and started pumping, broke circulation and pressured up to 400 pounds. Rig down and hook up Kilbarger which worked casing up and down, gained circulation and circulate hole from 10:05-10:30 pm. Hook-up Petroset, gained circulation and pumped away 60 sacks of class A with 3% calcium ran  50% excess, plug down 11:00 pm. Achieved no returns at surface, fluid level stayed at surface. Attempted grout at surface level. Jet wireline to run bond log on the surface casing before drilling out-from-surface. Surface casing cementing witnessed by Mason Drilling's John Mason.
+
| No Violations
|
+
| Kilbarger #5 reach total depth on the surface hole on fluid at 334 feet at 6:20 pm 6/27/2013, drillers top of Big Lime 238. No lost circulation zones or fluid loss while drilling noted. Ran 10 joints of new and used/tested 17 pound, 7 inch surface casing. Two new joints on bottom with guide shoe and two new joints on top landed with a 10 foot landing joint. Ran 307 set at 317. Petroset hooked up and started pumping, broke circulation and pressured up to 400 pounds. Rig down and hook up Kilbarger which worked casing up and down, gained circulation and circulate hole from 10:05-10:30 pm. Hook-up Petroset, gained circulation and pumped away 60 sacks of class A with 3% calcium ran  50% excess, plug down 11:00 pm. Achieved no returns at surface, fluid level stayed at surface. Attempted grout at surface level. Jet wireline to run bond log on the surface casing before drilling out-from-surface. Surface casing cementing witnessed by Mason Drillings John Mason.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1372704322
 
| 1372704322
 
| 2013-06-29
 
| 2013-06-29
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Operator ran Jet Wireline bond log, gamma ray and ccl log. Pressure tested surface casing and tested the BOP. Status: ok.
 
| Operator ran Jet Wireline bond log, gamma ray and ccl log. Pressure tested surface casing and tested the BOP. Status: ok.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1372790912
 
| 1372790912
 
| 2013-07-02
 
| 2013-07-02
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Gary Van Dike is providing mud control with his plow truck on State Route 746.
 
| Gary Van Dike is providing mud control with his plow truck on State Route 746.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1373045530
 
| 1373045530
 
| 2013-07-04
 
| 2013-07-04
|  
+
| Drill / Deepen /  Reopen
| Mud pump down at 2697' . Wait on replacement mud pump.
+
| No Violations
|
+
| Mud pump down at 2697 . Wait on replacement mud pump.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1373295499
 
| 1373295499
 
| 2013-07-08
 
| 2013-07-08
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Kilbarger #5 rigging down. Operator is currently evaluating the well. Ran 4.5 casing  (hung in the hole/not cemented) and may turn the well into a ERP site or possibly plug back to redrill to the intended target. Directional wireline survey showed the well to be deviated. Status: will continue to  monitor.
 
| Kilbarger #5 rigging down. Operator is currently evaluating the well. Ran 4.5 casing  (hung in the hole/not cemented) and may turn the well into a ERP site or possibly plug back to redrill to the intended target. Directional wireline survey showed the well to be deviated. Status: will continue to  monitor.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1373311160
 
| 1373311160
 
| 2013-07-05
 
| 2013-07-05
|  
+
| Drill / Deepen /  Reopen
| Kilbarger #5 reached total depth at 2967' in the Trempealeau at 11:25 pm.
+
| No Violations
|
+
| Kilbarger #5 reached total depth at 2967 in the Trempealeau at 11:25 pm.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1373552157
 
| 1373552157
 
| 2013-07-11
 
| 2013-07-11
|  
+
| Preliminary Restoration
 +
| No Violations
 
| Informed by the operator that the fluid from the drilling pits was pumped into the storage tanks at the entrance on Monday 7/8/13 prior to the flooding on Wednesday 7/10/13.
 
| Informed by the operator that the fluid from the drilling pits was pumped into the storage tanks at the entrance on Monday 7/8/13 prior to the flooding on Wednesday 7/10/13.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1374592533
 
| 1374592533
 
| 2013-07-23
 
| 2013-07-23
|  
+
| Preliminary Restoration
| The operator has closed all drilling permits.
+
| No Violations
|
+
| The operator has closed all drilling pits.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1378824987
 
| 1378824987
 
| 2013-09-10
 
| 2013-09-10
|  
+
| Preliminary Restoration
 +
| No Violations
 
| The operator has closed all pits, removed drilling debris, restored top soil and graded location.
 
| The operator has closed all pits, removed drilling debris, restored top soil and graded location.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1379588973
 
| 1379588973
 
| 2013-08-30
 
| 2013-08-30
|  
+
| Salt Water Injection Well
 +
| No Violations
 
| Inspected well location and surrounding area for Salt Water Injection Conversion (SWIW).  The well is located in a crop field.  The Olentagny River is located 2100 feet west of the well location.  An intermittent stream that drains into to Olentangy River  is located just north of the well location.  There are nine residential homes within 0.25 miles of the well on Caledonia Road (SR 746) and Roberts Road. Each of these homes are anticipated to have a water well that may be used for domestic purposes. The Del-Co Water Company, Inc. in the year 2002 laid water lines along Caledonia Road and Roberts Road.  Currently it is the option of the residents to be hooked up to the rural water supply. There are no significant issues that are of issue for the conversion of this well to a SWIW well.
 
| Inspected well location and surrounding area for Salt Water Injection Conversion (SWIW).  The well is located in a crop field.  The Olentagny River is located 2100 feet west of the well location.  An intermittent stream that drains into to Olentangy River  is located just north of the well location.  There are nine residential homes within 0.25 miles of the well on Caledonia Road (SR 746) and Roberts Road. Each of these homes are anticipated to have a water well that may be used for domestic purposes. The Del-Co Water Company, Inc. in the year 2002 laid water lines along Caledonia Road and Roberts Road.  Currently it is the option of the residents to be hooked up to the rural water supply. There are no significant issues that are of issue for the conversion of this well to a SWIW well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1379600451
 
| 1379600451
 
| 2013-09-19
 
| 2013-09-19
|  
+
| Enhanced Recovery Project
| Permit to convert to enhanced recovery project received. Permit issued: 9/17/2013 Expires: 9/17/2013
+
| No Violations
|
+
| Permit to convert to enhanced recovery project received. Permit issued: 9/17/2013 Expires: 9/17/2015
|
 
|
 
 
|-
 
|-
 +
| 1379847428
 +
| 2016-01-19
 +
| Salt Water Injection Well
 +
| No Violations
 +
| Inspect well for integrity and pressure. Well is shut in and no activity has occurred at the well head since last inspection.
 
|-
 
|-
 
| 1382377346
 
| 1382377346
 
| 2013-10-21
 
| 2013-10-21
|  
+
| Enhanced Recovery Project
 +
| No Violations
 
| The McClenathan #2 ERP project has not commenced. Production casing has been run and cemented and the operator has placed a marker at the well head. Status: will continue to monitor.
 
| The McClenathan #2 ERP project has not commenced. Production casing has been run and cemented and the operator has placed a marker at the well head. Status: will continue to monitor.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1386700837
 
| 1386700837
 
| 2013-12-10
 
| 2013-12-10
|  
+
| Enhanced Recovery Project
 +
| No Violations
 
| Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check.. No change in status from previous inspection.
 
| Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check.. No change in status from previous inspection.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1410656147
 
| 1410656147
 
| 2013-07-05
 
| 2013-07-05
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| 1:30 pm Mud pump replaced, going back into hole.
 
| 1:30 pm Mud pump replaced, going back into hole.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1443526853
 +
| 2015-09-10
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well and location. Service rig and pipe trailer at location.
 
|-
 
|-
| -1481601637
+
| 1481601637
 
| 2013-07-01
 
| 2013-07-01
|  
+
| Drill / Deepen /  Reopen
| Kilbarger #5 drilling on fluid 1358'.
+
| No Violations
|  
+
| Kilbarger #5 drilling on fluid 1358.
|  
+
|-
|  
+
| 1518891575
 +
| 2015-07-21
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| No change-in-status from previous inspection.
 +
|-
 +
| 1542288162
 +
| 2018-11-13
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. The well is shut in and has not been permitted for use.  There has been no activity and the status has not changed since the previous inspection.
 
|-
 
|-
 +
| 1551113543
 +
| 2016-04-11
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Inspect well. The well is shut in. Flow lines from production well has not been installed at the location.  Operator has not requested or been granted approval to use well for injection.
 
|-
 
|-
 
| 1604318192
 
| 1604318192
 
| 2014-12-09
 
| 2014-12-09
|  
+
| Preliminary Restoration
 +
| No Violations
 
| The preliminary restoration is complete.
 
| The preliminary restoration is complete.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1638871195
 
| 1638871195
 
| 2015-03-09
 
| 2015-03-09
|  
+
| Enhanced Recovery Project
 +
| No Violations
 
| No change in status from previous inspection.
 
| No change in status from previous inspection.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1662535117
 
| 1662535117
 
| 2015-05-05
 
| 2015-05-05
|  
+
| Production Wells
 +
| No Violations
 
| No change in status from previous inspection. No conversion.
 
| No change in status from previous inspection. No conversion.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1715185059
+
| 1715185059
 
| 2014-01-13
 
| 2014-01-13
|  
+
| Enhanced Recovery Project
 +
| No Violations
 
| No change in status from previous inspection. Work has not commenced on the McClenathan #2 ERP project.
 
| No change in status from previous inspection. Work has not commenced on the McClenathan #2 ERP project.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1736952180
 +
| 2017-01-19
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. A flow line has not been installed as of this date. The well is shut in and authorization has not been granted to utilize the well. Currently no access is available to the tubing. The annulus was measured for current pressure.
 +
|-
 +
| 1773584388
 +
| 2015-09-01
 +
| Work Over Reconditioning
 +
| No Violations
 +
| Inspect well.  Well is shut in. No on site activity to convert well to salt water injection well.
 +
|-
 +
| 1802686682
 +
| 2017-11-01
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. No activity or contact has been made by the operator since previous inspection. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
 
|-
 
|-
 
| 1811277284
 
| 1811277284
 
| 2014-03-14
 
| 2014-03-14
|  
+
| Enhanced Recovery Project
 +
| No Violations
 
| Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check. Inspect well,  storage and identification. Status: no change in status from previous inspection.
 
| Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check. Inspect well,  storage and identification. Status: no change in status from previous inspection.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1834089947
 
| 1834089947
 
| 2013-10-21
 
| 2013-10-21
|  
+
| Preliminary Restoration
 +
| No Violations
 
| The preliminary restoration is complete except for erosion control being established. The location is in cropland (soybeans recently harvested) and the farmer may plant through the surface location. Status: will continue to monitor.
 
| The preliminary restoration is complete except for erosion control being established. The location is in cropland (soybeans recently harvested) and the farmer may plant through the surface location. Status: will continue to monitor.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1897585527
 +
| 2017-08-10
 +
| Salt Water Injection Well
 +
| No Violations
 +
| Inspect well. The well is behind a crop of soybeans. No activity or contact has been made by the operator since previous inspection. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
 +
|-
 +
| 1928257551
 +
| 2017-04-11
 +
| Salt Water Injection Well
 +
| No Violations
 +
| Inspect well. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
 
|-
 
|-
| -1958594937
+
| 1958594937
 
| 2013-08-26
 
| 2013-08-26
|  
+
| Casing String Witnessed
| I witnessed the cementing of the production casing for Geopetro LLC. John Mason with Mason Drilling was on location. Petroset Cementing was on location to cement the casing. Please refer to Mr. Eric Daugstrup's report for details.
+
| No Violations
|
+
| I witnessed the cementing of the production casing for Geopetro LLC. John Mason with Mason Drilling was on location. Petroset Cementing was on location to cement the casing. Please refer to Mr. Eric Daugstrups report for details.
|
 
|
 
 
|-
 
|-
|-
+
| 1962444657
| -1962444657
 
 
| 2014-05-27
 
| 2014-05-27
|  
+
| Preliminary Restoration
 +
| No Violations
 
| The farmer has planted through the well location. Preliminary restoration complete.
 
| The farmer has planted through the well location. Preliminary restoration complete.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1963472042
+
| 1963472042
 
| 2014-07-28
 
| 2014-07-28
|  
+
| Enhanced Recovery Project
 +
| No Violations
 
| Inspected the McClenathan #1 (ERP #1) as part of a standard injection well status check.  Status: no change in status from previous inspection. Operations to convert have not begun and the well is currently in corn.
 
| Inspected the McClenathan #1 (ERP #1) as part of a standard injection well status check.  Status: no change in status from previous inspection. Operations to convert have not begun and the well is currently in corn.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1982863654
 +
| 2018-05-07
 +
| Enhanced Recovery Project
 +
| No Violations
 +
| Inspect well. The well is shut in and has not been permitted for use.
 
|-
 
|-
 
| 2137691405
 
| 2137691405
 
| 2014-08-25
 
| 2014-08-25
|  
+
| Enhanced Recovery Project
 +
| No Violations
 
| No change in status from previous inspection. The well is currently in mature crops.
 
| No change in status from previous inspection. The well is currently in mature crops.
 +
|-
 +
| 353620797
 +
| 2015-9-17 0:00:
 +
| WR
 +
| No Violations
 
|  
 
|  
|  
+
|-
 +
| 61138679
 +
| 2015-9-15 0:00:
 +
| ER
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
|-
+
| 616635339
| -595351781
+
| 2018-2-8 0:00:0
| 2014-07-30
+
| ER
|
+
| No Violations
| Inspect well for integrity and pressure. The well has not been completed for salt water injection.
 
|  
 
|  
 
 
|  
 
|  
 
|-
 
|-
|-
+
| 737455625
| -673817450
+
| 2019-7-16 0:00:
| 2013-06-05
+
| SW
|
+
| No Violations
| Mason drilling has begun building the location.
 
|  
 
|  
 
 
|  
 
|  
|-
 
 
|-
 
|-
 
| 750438715
 
| 750438715
| 2014-01-22
+
| 2014-1-22 0:00:
|
+
| ER
| Location Information. ENTRANCE: Lat. 40.59962  Long. -82.96249 / WELL HEAD: Lat. 40.59952  Long.  -82.96388  / CENTER-OF-STORAGE: no storage built at the time of inspection.
+
| No Violations
|  
 
|  
 
 
|  
 
|  
 
|-
 
|-
|-
+
| 772267980
| -800620239
+
| 2017-12-22 0:00
| 2014-12-09
+
| ER
|
+
| No Violations
| Inspected the McClenathan #2 (ERP #221) as part of a standard injection well status check. Inspect well, storage and identification. Status: no change in status from previous inspection.
 
|  
 
|  
 
 
|  
 
|  
 
|-
 
|-
|-
+
| 930061370
| -929164922
+
| 2019-4-9 0:00:0
| 2014-05-27
+
| SW
|
+
| No Violations
| Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check. Status: no change in status from previous inspection.
 
|  
 
|  
 
 
|  
 
|  
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 17:08, 12 January 2021

Well Details

Well ID: 34-101-20221
Loading map...
Country: United States
State: Ohio
County: Marion
Municipality: Claridon Township
Operator Name: GEOPETRO LLC
Well Pad ID:
Farm/Lease Name: MCCLENATHAN (ERP #1)
License Status: Well Drilled
License Date: 2013-09-17
Spud Date: 2013-06-27
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2013-07-05
Well Total Depth: 2967.00 ft
Configuration: Vertical
Latitude: 40.590000
Longitude: -82.960000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-05-17 Proposed Formations:TRENTON, BLACK RIVER, TREMPEALEAU, Issued Date:5/17/2013, Expired Date:5/17/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2013-07-05 WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
Completion Report Received 2013-08-05 WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
APP 2013-09-17 Proposed Formations:TREMPEALEAU, Issued Date:9/17/2013, Expired Date:9/17/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:EOR, Proposed Well Class:ERP
Last Compliance Report 2013-09-17 WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
Construction Permit Expires 2015-09-17 WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET
Record Last Modified 2017-02-10 WELL PERMITTED TO CONVERT FOR ERP - 09/17/2013 - TET

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2018 GEOPETRO LLC 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2018 GEOPETRO LLC Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1191041472 2013-6-30 0:00: DD No Violations
-1299892688 2013-7-3 0:00:0 DD No Violations
-1379847428 2016-1-19 0:00: SW No Violations
-1481601637 2013-7-1 0:00:0 DD No Violations
-1715185059 2014-1-13 0:00: ER No Violations
-1736952180 2017-1-19 0:00: ER No Violations
-1773584388 2015-9-1 0:00:0 WR No Violations
-1928257551 2017-4-11 0:00: SW No Violations
-1958594937 2013-8-26 0:00: CS No Violations
-1962444657 2014-5-27 0:00: PL No Violations
-1963472042 2014-7-28 0:00: ER No Violations
-252823231 2019-1-8 0:00:0 DD No Violations
-257577080 2020-1-14 0:00: ER No Violations
-309574765 2016-7-26 0:00: ER No Violations
-494604358 2015-9-18 0:00: WR No Violations
-552416882 2015-9-9 0:00:0 ER No Violations
-595351781 2014-7-30 0:00: ER No Violations
-673817450 2013-6-5 0:00:0 DD No Violations
-699918834 2018-8-23 0:00: SW No Violations
-770357554 2015-9-15 0:00: WR No Violations
-777938658 2019-10-30 0:00 ER No Violations
-800620239 2014-12-9 0:00: ER No Violations
-857888275 2015-11-9 0:00: ER No Violations
-929164922 2014-5-27 0:00: ER No Violations
0061138679 2015-09-15 Enhanced Recovery Project No Violations Mason Service Rig in on the well for conversion.
0309574765 2016-07-26 Enhanced Recovery Project No Violations Inspect well. The well is behind corn. A flow line has not been installed as of this date. The well is shut in and authorization has not been granted to utilize the well.
0353620797 2015-09-17 Work Over Reconditioning No Violations Inspect well. The cement shoe has been drilled out. The tubing with drill bit were tripped out of the hole. The same tubing was run in the hole with a rebuilt Halliburton R-4 packer with a 6 foot pup joint set in compression. The tubing is used barely.
0494604358 2015-09-18 Work Over Reconditioning No Violations The packer and tubing were run in the hole. The cement shoe was displaced to 2785 feet. The packer was set at 2770 with 2-3/8 inch EUE upset tubing at 4.7 pounds per foot. There were 10 joints left on the rack when the job was complete. The string weight was about 13,019 pounds. The packer was set in tension with 23,000 pounds of stretch. The annulus was loaded with water with inhibitor and pressure tested. The test passed with less than two percent loss in pressure.
0552416882 2015-09-09 Enhanced Recovery Project No Violations The operator has moved a dozer onto location in preparation for conversion.
0595351781 2014-07-30 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well has not been completed for salt water injection.
0616635339 2018-02-08 Enhanced Recovery Project No Violations Inspect well. No activity or contact has been made by the operator since previous inspection. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
0673817450 2013-06-05 Drill / Deepen / Reopen No Violations Mason drilling has begun building the location.
0699918834 2018-08-23 Salt Water Injection Well No Violations Inspect location. The well is behind corn.
0750438715 2014-01-22 Enhanced Recovery Project No Violations Location Information. ENTRANCE: Lat. 40.59962 Long. -82.96249 / WELL HEAD: Lat. 40.59952 Long. -82.96388 / CENTER-OF-STORAGE: no storage built at the time of inspection.
0770357554 2015-09-15 Work Over Reconditioning No Violations Jet Wireline on location to perform a cement bond log to determine the top of cement circulated for 4.5 inch production casing. Service rig mobilized onto location.
0772267980 2017-12-22 Enhanced Recovery Project No Violations Inspect well. The tubing and packer were installed and MIT tested on September 18, 2015. The proposed flow line from the water source, Mcclenathan #1; 3410120219, has not been installed. The operator has not requested initial operation status. This well is incapable of operation and is idle.
0800620239 2014-12-09 Enhanced Recovery Project No Violations Inspected the McClenathan #2 (ERP #221) as part of a standard injection well status check. Inspect well, storage and identification. Status: no change in status from previous inspection.
0857888275 2015-11-09 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well is shut in and flow line has not been installed.
0929164922 2014-05-27 Enhanced Recovery Project No Violations Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check. Status: no change in status from previous inspection.
1031143440 2013-06-13 Drill / Deepen / Reopen No Violations Kilbarger #5 moving to location on hold pending weather.
1128082576 2020-4-8 0:00:0 ER No Violations
1191041472 2013-06-30 Drill / Deepen / Reopen No Violations Kilbarger #5 switch to fluid at 1030. Making too much water from Newburg.
1205476676 2015-09-22 Enhanced Recovery Project No Violations Mason service rig has left the location. Conversion process continues.
1284406160 2016-11-15 Enhanced Recovery Project No Violations Inspect well. A flow line has not been installed as of this date. The well is shut in and authorization has not been granted to utilize the well. Currently no access is available to the tubing.
1299892688 2013-07-03 Drill / Deepen / Reopen No Violations Kilbarger #5 Tripping at 1965.
1370539779 2013-06-06 Drill / Deepen / Reopen No Violations Mason Drilling has removed the topsoil and stoned the entrance way off state route 746.
1370878599 2013-06-10 Drill / Deepen / Reopen No Violations Waiting on Kilbarger #5.
1372268945 2013-06-26 Drill / Deepen / Reopen No Violations Kilbarger #5 moving on location and rigging up. Spud:
1372269857 2013-06-26 Brine Hauler No Violations Accompany Mullins Energy services brine truck to collect fresh water for the drilling rig. Status: ok.
1372351028 2013-06-27 Drill / Deepen / Reopen No Violations Kilbarger #5 spud 10:00 pm 6/26/2013 with 8.75 drill bit on fresh water mud.
1372382768 2013-06-27 Casing String Witnessed No Violations Kilbarger #5 reach total depth on the surface hole on fluid at 334 feet at 6:20 pm 6/27/2013, drillers top of Big Lime 238. No lost circulation zones or fluid loss while drilling noted. Ran 10 joints of new and used/tested 17 pound, 7 inch surface casing. Two new joints on bottom with guide shoe and two new joints on top landed with a 10 foot landing joint. Ran 307 set at 317. Petroset hooked up and started pumping, broke circulation and pressured up to 400 pounds. Rig down and hook up Kilbarger which worked casing up and down, gained circulation and circulate hole from 10:05-10:30 pm. Hook-up Petroset, gained circulation and pumped away 60 sacks of class A with 3% calcium ran 50% excess, plug down 11:00 pm. Achieved no returns at surface, fluid level stayed at surface. Attempted grout at surface level. Jet wireline to run bond log on the surface casing before drilling out-from-surface. Surface casing cementing witnessed by Mason Drillings John Mason.
1372704322 2013-06-29 Drill / Deepen / Reopen No Violations Operator ran Jet Wireline bond log, gamma ray and ccl log. Pressure tested surface casing and tested the BOP. Status: ok.
1372790912 2013-07-02 Drill / Deepen / Reopen No Violations Gary Van Dike is providing mud control with his plow truck on State Route 746.
1373045530 2013-07-04 Drill / Deepen / Reopen No Violations Mud pump down at 2697 . Wait on replacement mud pump.
1373295499 2013-07-08 Drill / Deepen / Reopen No Violations Kilbarger #5 rigging down. Operator is currently evaluating the well. Ran 4.5 casing (hung in the hole/not cemented) and may turn the well into a ERP site or possibly plug back to redrill to the intended target. Directional wireline survey showed the well to be deviated. Status: will continue to monitor.
1373311160 2013-07-05 Drill / Deepen / Reopen No Violations Kilbarger #5 reached total depth at 2967 in the Trempealeau at 11:25 pm.
1373552157 2013-07-11 Preliminary Restoration No Violations Informed by the operator that the fluid from the drilling pits was pumped into the storage tanks at the entrance on Monday 7/8/13 prior to the flooding on Wednesday 7/10/13.
1374592533 2013-07-23 Preliminary Restoration No Violations The operator has closed all drilling pits.
1378824987 2013-09-10 Preliminary Restoration No Violations The operator has closed all pits, removed drilling debris, restored top soil and graded location.
1379588973 2013-08-30 Salt Water Injection Well No Violations Inspected well location and surrounding area for Salt Water Injection Conversion (SWIW). The well is located in a crop field. The Olentagny River is located 2100 feet west of the well location. An intermittent stream that drains into to Olentangy River is located just north of the well location. There are nine residential homes within 0.25 miles of the well on Caledonia Road (SR 746) and Roberts Road. Each of these homes are anticipated to have a water well that may be used for domestic purposes. The Del-Co Water Company, Inc. in the year 2002 laid water lines along Caledonia Road and Roberts Road. Currently it is the option of the residents to be hooked up to the rural water supply. There are no significant issues that are of issue for the conversion of this well to a SWIW well.
1379600451 2013-09-19 Enhanced Recovery Project No Violations Permit to convert to enhanced recovery project received. Permit issued: 9/17/2013 Expires: 9/17/2015
1379847428 2016-01-19 Salt Water Injection Well No Violations Inspect well for integrity and pressure. Well is shut in and no activity has occurred at the well head since last inspection.
1382377346 2013-10-21 Enhanced Recovery Project No Violations The McClenathan #2 ERP project has not commenced. Production casing has been run and cemented and the operator has placed a marker at the well head. Status: will continue to monitor.
1386700837 2013-12-10 Enhanced Recovery Project No Violations Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check.. No change in status from previous inspection.
1410656147 2013-07-05 Drill / Deepen / Reopen No Violations 1:30 pm Mud pump replaced, going back into hole.
1443526853 2015-09-10 Enhanced Recovery Project No Violations Inspect well and location. Service rig and pipe trailer at location.
1481601637 2013-07-01 Drill / Deepen / Reopen No Violations Kilbarger #5 drilling on fluid 1358.
1518891575 2015-07-21 Enhanced Recovery Project No Violations No change-in-status from previous inspection.
1542288162 2018-11-13 Enhanced Recovery Project No Violations Inspect well. The well is shut in and has not been permitted for use. There has been no activity and the status has not changed since the previous inspection.
1551113543 2016-04-11 Drill / Deepen / Reopen No Violations Inspect well. The well is shut in. Flow lines from production well has not been installed at the location. Operator has not requested or been granted approval to use well for injection.
1604318192 2014-12-09 Preliminary Restoration No Violations The preliminary restoration is complete.
1638871195 2015-03-09 Enhanced Recovery Project No Violations No change in status from previous inspection.
1662535117 2015-05-05 Production Wells No Violations No change in status from previous inspection. No conversion.
1715185059 2014-01-13 Enhanced Recovery Project No Violations No change in status from previous inspection. Work has not commenced on the McClenathan #2 ERP project.
1736952180 2017-01-19 Enhanced Recovery Project No Violations Inspect well. A flow line has not been installed as of this date. The well is shut in and authorization has not been granted to utilize the well. Currently no access is available to the tubing. The annulus was measured for current pressure.
1773584388 2015-09-01 Work Over Reconditioning No Violations Inspect well. Well is shut in. No on site activity to convert well to salt water injection well.
1802686682 2017-11-01 Enhanced Recovery Project No Violations Inspect well. No activity or contact has been made by the operator since previous inspection. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
1811277284 2014-03-14 Enhanced Recovery Project No Violations Inspected the McClenathan #2 (ERP #1) as part of a standard injection well status check. Inspect well, storage and identification. Status: no change in status from previous inspection.
1834089947 2013-10-21 Preliminary Restoration No Violations The preliminary restoration is complete except for erosion control being established. The location is in cropland (soybeans recently harvested) and the farmer may plant through the surface location. Status: will continue to monitor.
1897585527 2017-08-10 Salt Water Injection Well No Violations Inspect well. The well is behind a crop of soybeans. No activity or contact has been made by the operator since previous inspection. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
1928257551 2017-04-11 Salt Water Injection Well No Violations Inspect well. Authorization to inject fluids has not been requested by the operator. The well is shut in and incapable of injection.
1958594937 2013-08-26 Casing String Witnessed No Violations I witnessed the cementing of the production casing for Geopetro LLC. John Mason with Mason Drilling was on location. Petroset Cementing was on location to cement the casing. Please refer to Mr. Eric Daugstrups report for details.
1962444657 2014-05-27 Preliminary Restoration No Violations The farmer has planted through the well location. Preliminary restoration complete.
1963472042 2014-07-28 Enhanced Recovery Project No Violations Inspected the McClenathan #1 (ERP #1) as part of a standard injection well status check. Status: no change in status from previous inspection. Operations to convert have not begun and the well is currently in corn.
1982863654 2018-05-07 Enhanced Recovery Project No Violations Inspect well. The well is shut in and has not been permitted for use.
2137691405 2014-08-25 Enhanced Recovery Project No Violations No change in status from previous inspection. The well is currently in mature crops.
353620797 2015-9-17 0:00: WR No Violations
61138679 2015-9-15 0:00: ER No Violations
616635339 2018-2-8 0:00:0 ER No Violations
737455625 2019-7-16 0:00: SW No Violations
750438715 2014-1-22 0:00: ER No Violations
772267980 2017-12-22 0:00 ER No Violations
930061370 2019-4-9 0:00:0 SW No Violations

For data sources see[7]

References