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Difference between revisions of "34-075-60012"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-075-60012
 
| Well ID: 34-075-60012
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.59450591, -81.97364455 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.59, -81.97 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Holmes County, Ohio|Holmes]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[PATTEN W H DRLG CO]]
+
| County: [[Holmes_County,_Ohio|Holmes]]
 +
|-
 +
| Municipality: [[Hardy_Township,_Holmes_County,_Ohio|Hardy Township]]
 +
|-
 +
| Operator Name: [[W H PATTEN  DRILLING CO]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: NOWELLS G K
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2015-06-15
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional:  
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1929-01-27
 +
|-
 +
| Well Total Depth: 3286.00 ft
 +
|-
 +
| Configuration: Vertical
 +
|-
 +
| Latitude: 40.590000
 +
|-
 +
| Longitude: -81.970000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Completed
 +
| 1929-01-27
 +
| FDT=R.R., PF=1ST & 2ND
 
|-
 
|-
| Configuration:
+
| Reached Total Depth
 +
| 1929-01-27
 +
| FDT=R.R., PF=1ST & 2ND
 
|-
 
|-
| Well Status: Producing
+
| APP
 +
| 2015-06-15
 +
| Proposed Formations:CLINTON, Issued Date:6/15/2015, Expired Date:6/14/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Violations: 0
+
| Plugged/Abandoned
 +
| 2015-10-14
 +
| FDT=R.R., PF=1ST & 2ND
 
|-
 
|-
| Latitude: 40.59450591
+
| Record Last Modified
 +
| 2017-02-10
 +
| FDT=R.R., PF=1ST & 2ND
 
|-
 
|-
| Longitude: -81.97364455
+
| Construction Permit Expires
 +
| 2017-06-14
 +
| FDT=R.R., PF=1ST & 2ND
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | CONDENSATE PRODUCTION DAYS
+
|-
!scope="col" | OIL QUANTITY
+
| 2006-09-11
!scope="col" | OIL PRODUCTION DAYS
+
| style="text-align: right;" | 3213
 +
| style="text-align: right;" | 3237
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2006-09-11
 +
| style="text-align: right;" | 3251
 +
| style="text-align: right;" | 3272
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1996-0
 
| style="text-align:right;" | 0.0
 
 
|  
 
|  
 +
| style="text-align: right;" | 3213
 +
| style="text-align: right;" | 3237
 +
| style="text-align: right;" | 0
 +
|-
 
|  
 
|  
|  
+
| style="text-align: right;" | 3213
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 3237
|  
+
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
 +
|}-->
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1997-0
 
| style="text-align:right;" | 0.0
 
 
|  
 
|  
 +
| ACID
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 130 Qts
 +
| style="text-align: right;" | 0
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1996
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1997
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1998
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 802.00
 +
| style="text-align: right;" | 839.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2002
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 45
 +
|-
 +
| 2003
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2004
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2005
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2006
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2007
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2008
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2009
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2010
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2011
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2012
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 366
 +
|-
 +
| 2013
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2014
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2015
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2016
 +
| [[W H PATTEN  DRILLING CO]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1996
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1997
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1998
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1998-0
+
| 2002
| style="text-align:right;" | 0.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 45
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 2004
| style="text-align:right;" | 802.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 839.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 2006
| style="text-align:right;" | 0.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 2008
| style="text-align:right;" | 0.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 2010
| style="text-align:right;" | 0.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 2012
| style="text-align:right;" | 0.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 366
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2004-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[W H PATTEN  DRILLING CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 2016
| style="text-align:right;" | 0.0
+
| [[W H PATTEN  DRILLING CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| 2006-0
+
| -1103492314
| style="text-align:right;" | 0.0
+
| 2015-10-6 0:00:
 +
| PB
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| -1993539117
 +
| 2015-9-24 0:00:
 +
| PB
 +
| No Violations
 
|  
 
|  
|  
+
|-
| style="text-align:right;" | 0.0
+
| -507528750
 +
| 2015-9-28 0:00:
 +
| PB
 +
| No Violations
 
|  
 
|  
 
|-
 
|-
 +
| 0507528750
 +
| 2015-09-28
 +
| Plug / Plug Back
 +
| No Violations
 +
| The rods were eaten in two at 3125.  The tubing was eaten off at the same place.  The packer on the 3-1/2 tubing was un-jayed and they pulled about half of the tubing and shut down for the night.
 
|-
 
|-
| 2007-0
+
| 0565713327
| style="text-align:right;" | 0.0
+
| 2015-10-07
|  
+
| Plug / Plug Back
|  
+
| No Violations
|  
+
| Pulled balance of 5-1/2 casing without having to re-rip.  Ran tubing to 1834 and shut down fo rthe night.  Will set rip and Berea plugs on the morrow.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1103492314
 +
| 2015-10-06
 +
| Plug / Plug Back
 +
| No Violations
 +
| Pulled approximately 300 of casing and it was tight and dragging all the way.  Cant pull any more.  Tight.  Will run in with the rippers in the morning and try to rip the pipe in an area that is free.
 
|-
 
|-
| 2008-0
+
| 1128983747
| style="text-align:right;" | 0.0
+
| 2016-05-03
|  
+
| Final Restoration
|  
+
| No Violations
|  
+
| Good growth of grasses.  Final restoration is passed.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1443437732
 +
| 2015-09-25
 +
| Plug / Plug Back
 +
| No Violations
 +
| Pulling tubing and rods.
 
|-
 
|-
| 2009-0
+
| 1443611241
| style="text-align:right;" | 0.0
+
| 2015-09-29
|  
+
| Plug / Plug Back
|  
+
| No Violations
|  
+
| Pulled balance of the 3-1/2 tubing.  There were 3 tail joints below the packer with turned down collars indicating that there is probably a 4 liner in the well.  They ran the tools and were able to get to 3175 before they started feeling something on the tools.  (likely the rods and tubing left in the hole).  They came out of the hole with the tools and shut down to repair the power tongs.  They will run the tubing for the bottom plug in the morning.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1443782064
 +
| 2015-10-01
 +
| Plug / Plug Back
 +
| No Violations
 +
| Ran tubing to 3230 and spotted a 60 sack plug thru the tubing.  Pulled out of the plug and will tag it in the morning.
 
|-
 
|-
| 2010-0
+
| 1444043302
| style="text-align:right;" | 0.0
+
| 2015-10-02
|  
+
| Plug / Plug Back
|  
+
| No Violations
|  
+
| Ran tubing back to bottom and tagged the cement at 2975  Pulled the tubing.  Ran ripper into the hole and got first telegraph at 2039.  Ripped the casing there and shut down for the weekend.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1444130914
 +
| 2015-10-05
 +
| Plug / Plug Back
 +
| No Violations
 +
| Working the 5-1/2 casing which is dragging badly.  Top joint pulled loose at 60+K.  Gathering fishing tools for 5-1/2 11V casing.
 
|-
 
|-
| 2011-0
+
| 1444388015
| style="text-align:right;" | 0.0
+
| 2015-10-08
|  
+
| Plug / Plug Back
|  
+
| No Violations
|  
+
| Cemenco Services set the rip and Berea plugs thru 1-1/2 tubing.  See the plugging report for the details.  Welded a nipple on the 8 and tried to pull it.  It would not come loose.    Ripped on the 8 at 290 with a good telegraph.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1444734139
 +
| 2015-10-09
 +
| Plug / Plug Back
 +
| No Violations
 +
| Ripped and pulled 8 casing.  Ran 1-1/2 tubing to 257 and shut down for the weekend.
 
|-
 
|-
| 2012-0
+
| 1500177450
| style="text-align:right;" | 0.0
+
| 2015-10-14
|  
+
| Plug / Plug Back
|  
+
| No Violations
|  
+
| the top plug was tagged at 90.  Holmes Readymix put 2 cubic yards of 9 sack grout down the well to bring the cement level back to the surface.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1541639839
 +
| 2015-09-23
 +
| Plug / Plug Back
 +
| No Violations
 +
| Move on and rig up.
 
|-
 
|-
| 2013-0
+
| 1880810849
| style="text-align:right;" | 0.0
+
| 2015-10-13
|
+
| Plug / Plug Back
|  
+
| No Violations
|  
+
| Cemenco Services spotted the top plug thru 1-1/2 tubing from 257 to 0.   The well circulated until the calculated volume of cement was mixed and pumped and then quit circulating.    Shut down and rmoved the tubing from the well.  The fluid level was at ~ 5 from surface.  Will check the cement top after it sets up and grout back to surface as necessary.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1993539117
 +
| 2015-09-24
 +
| Plug / Plug Back
 +
| No Violations
 +
| They have rigged up and unseated the pump.  There is no activity today.
 
|-
 
|-
| 2014-0
+
| 565713327
| style="text-align:right;" | 0.0
+
| 2015-10-7 0:00:
| style="text-align:right;" | 365.0
+
| PB
|  
+
| No Violations
 
|  
 
|  
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 17:09, 12 January 2021

Well Details

Well ID: 34-075-60012
Loading map...
Country: United States
State: Ohio
County: Holmes
Municipality: Hardy Township
Operator Name: W H PATTEN DRILLING CO
Well Pad ID:
Farm/Lease Name: NOWELLS G K
License Status: Final Restoration
License Date: 2015-06-15
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1929-01-27
Well Total Depth: 3286.00 ft
Configuration: Vertical
Latitude: 40.590000
Longitude: -81.970000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1929-01-27 FDT=R.R., PF=1ST & 2ND
Reached Total Depth 1929-01-27 FDT=R.R., PF=1ST & 2ND
APP 2015-06-15 Proposed Formations:CLINTON, Issued Date:6/15/2015, Expired Date:6/14/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-10-14 FDT=R.R., PF=1ST & 2ND
Record Last Modified 2017-02-10 FDT=R.R., PF=1ST & 2ND
Construction Permit Expires 2017-06-14 FDT=R.R., PF=1ST & 2ND

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3213 3237 0
2006-09-11 3251 3272 0
3213 3237 0
3213 3237 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 130 Qts 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1996 W H PATTEN DRILLING CO 0.00 0.00 365
1997 W H PATTEN DRILLING CO 0.00 0.00 365
1998 W H PATTEN DRILLING CO 0.00 0.00 365
1999 W H PATTEN DRILLING CO 802.00 839.00 365
2000 W H PATTEN DRILLING CO 0.00 0.00 365
2001 W H PATTEN DRILLING CO 0.00 0.00 0
2002 W H PATTEN DRILLING CO 0.00 0.00 45
2003 W H PATTEN DRILLING CO 0.00 0.00 365
2004 W H PATTEN DRILLING CO 0.00 0.00 365
2005 W H PATTEN DRILLING CO 0.00 0.00 365
2006 W H PATTEN DRILLING CO 0.00 0.00 365
2007 W H PATTEN DRILLING CO 0.00 0.00 365
2008 W H PATTEN DRILLING CO 0.00 0.00 365
2009 W H PATTEN DRILLING CO 0.00 0.00 365
2010 W H PATTEN DRILLING CO 0.00 0.00 365
2011 W H PATTEN DRILLING CO 0.00 0.00 365
2012 W H PATTEN DRILLING CO 0.00 0.00 366
2013 W H PATTEN DRILLING CO 0.00 0.00 365
2014 W H PATTEN DRILLING CO 0.00 0.00 365
2015 W H PATTEN DRILLING CO 0.00 0.00 365
2016 W H PATTEN DRILLING CO 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1996 W H PATTEN DRILLING CO Brine 0 365
1997 W H PATTEN DRILLING CO Brine 0 365
1998 W H PATTEN DRILLING CO Brine 0 365
1999 W H PATTEN DRILLING CO Brine 0 365
2000 W H PATTEN DRILLING CO Brine 0 365
2001 W H PATTEN DRILLING CO Brine 0 0
2002 W H PATTEN DRILLING CO Brine 0 45
2003 W H PATTEN DRILLING CO Brine 0 365
2004 W H PATTEN DRILLING CO Brine 0 365
2005 W H PATTEN DRILLING CO Brine 0 365
2006 W H PATTEN DRILLING CO Brine 0 365
2007 W H PATTEN DRILLING CO Brine 0 365
2008 W H PATTEN DRILLING CO Brine 0 365
2009 W H PATTEN DRILLING CO Brine 0 365
2010 W H PATTEN DRILLING CO Brine 0 365
2011 W H PATTEN DRILLING CO Brine 0 365
2012 W H PATTEN DRILLING CO Brine 0 366
2013 W H PATTEN DRILLING CO Brine 0 365
2014 W H PATTEN DRILLING CO Brine 0 365
2015 W H PATTEN DRILLING CO Brine 0 365
2016 W H PATTEN DRILLING CO Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1103492314 2015-10-6 0:00: PB No Violations
-1993539117 2015-9-24 0:00: PB No Violations
-507528750 2015-9-28 0:00: PB No Violations
0507528750 2015-09-28 Plug / Plug Back No Violations The rods were eaten in two at 3125. The tubing was eaten off at the same place. The packer on the 3-1/2 tubing was un-jayed and they pulled about half of the tubing and shut down for the night.
0565713327 2015-10-07 Plug / Plug Back No Violations Pulled balance of 5-1/2 casing without having to re-rip. Ran tubing to 1834 and shut down fo rthe night. Will set rip and Berea plugs on the morrow.
1103492314 2015-10-06 Plug / Plug Back No Violations Pulled approximately 300 of casing and it was tight and dragging all the way. Cant pull any more. Tight. Will run in with the rippers in the morning and try to rip the pipe in an area that is free.
1128983747 2016-05-03 Final Restoration No Violations Good growth of grasses. Final restoration is passed.
1443437732 2015-09-25 Plug / Plug Back No Violations Pulling tubing and rods.
1443611241 2015-09-29 Plug / Plug Back No Violations Pulled balance of the 3-1/2 tubing. There were 3 tail joints below the packer with turned down collars indicating that there is probably a 4 liner in the well. They ran the tools and were able to get to 3175 before they started feeling something on the tools. (likely the rods and tubing left in the hole). They came out of the hole with the tools and shut down to repair the power tongs. They will run the tubing for the bottom plug in the morning.
1443782064 2015-10-01 Plug / Plug Back No Violations Ran tubing to 3230 and spotted a 60 sack plug thru the tubing. Pulled out of the plug and will tag it in the morning.
1444043302 2015-10-02 Plug / Plug Back No Violations Ran tubing back to bottom and tagged the cement at 2975 Pulled the tubing. Ran ripper into the hole and got first telegraph at 2039. Ripped the casing there and shut down for the weekend.
1444130914 2015-10-05 Plug / Plug Back No Violations Working the 5-1/2 casing which is dragging badly. Top joint pulled loose at 60+K. Gathering fishing tools for 5-1/2 11V casing.
1444388015 2015-10-08 Plug / Plug Back No Violations Cemenco Services set the rip and Berea plugs thru 1-1/2 tubing. See the plugging report for the details. Welded a nipple on the 8 and tried to pull it. It would not come loose. Ripped on the 8 at 290 with a good telegraph.
1444734139 2015-10-09 Plug / Plug Back No Violations Ripped and pulled 8 casing. Ran 1-1/2 tubing to 257 and shut down for the weekend.
1500177450 2015-10-14 Plug / Plug Back No Violations the top plug was tagged at 90. Holmes Readymix put 2 cubic yards of 9 sack grout down the well to bring the cement level back to the surface.
1541639839 2015-09-23 Plug / Plug Back No Violations Move on and rig up.
1880810849 2015-10-13 Plug / Plug Back No Violations Cemenco Services spotted the top plug thru 1-1/2 tubing from 257 to 0. The well circulated until the calculated volume of cement was mixed and pumped and then quit circulating. Shut down and rmoved the tubing from the well. The fluid level was at ~ 5 from surface. Will check the cement top after it sets up and grout back to surface as necessary.
1993539117 2015-09-24 Plug / Plug Back No Violations They have rigged up and unseated the pump. There is no activity today.
565713327 2015-10-7 0:00: PB No Violations

For data sources see[9]

References