If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
m |
m |
||
(3 intermediate revisions by the same user not shown) | |||
Line 1: | Line 1: | ||
− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-103-24255 | | Well ID: 34-103-24255 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 41.1, -82.06 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | Municipality: | + | | State: Ohio |
+ | |- | ||
+ | | County: [[Medina_County,_Ohio|Medina]] | ||
+ | |- | ||
+ | | Municipality: [[Chatham_Township,_Medina_County,_Ohio|Chatham Township]] | ||
|- | |- | ||
| Operator Name: [[JESSE OIL]] | | Operator Name: [[JESSE OIL]] | ||
Line 13: | Line 17: | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: CONLEY D& E |
|- | |- | ||
− | | | + | | License Status: Orphan Well - Ready |
|- | |- | ||
− | | | + | | License Date: 1985-08-20 |
|- | |- | ||
| Spud Date: 1985-09-04 | | Spud Date: 1985-09-04 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: [[D M WALTZ DRLG]] |
+ | |- | ||
+ | | Final Drill Date: | ||
+ | |- | ||
+ | | Well Total Depth: 0.00 ft | ||
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Well Status: | + | | Latitude: 41.100000 |
+ | |- | ||
+ | | Longitude: -82.060000 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | CO | ||
+ | | 1985-08-20 | ||
+ | | 2223 JESSE OIL GeoDate 8/20/85 | ||
+ | |- | ||
+ | | Oil and Gas | ||
+ | | 1985-08-20 | ||
+ | | Issued Date 8/20/85 Expired Date 8/20/86 Acres 0001000 Tool Type RTA Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 | ||
|- | |- | ||
− | | | + | | Original Spud |
+ | | 1985-09-04 | ||
+ | | Referred to Orphan Well June, 2000. NEVER RECEIVED A WELL COMPLETION REPORT. WELL IS LEAKING OIL. I&O CASE # 2000 06 017. PERMIT EXPIRED | ||
|- | |- | ||
− | | | + | | Construction Permit Expires |
+ | | 1986-08-20 | ||
+ | | Referred to Orphan Well June, 2000. NEVER RECEIVED A WELL COMPLETION REPORT. WELL IS LEAKING OIL. I&O CASE # 2000 06 017. PERMIT EXPIRED | ||
|- | |- | ||
− | | | + | | Changed to Orphan Well Ready |
+ | | 2000-06-01 | ||
+ | | Changed Well To Orphan Ready | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2019-03-25 | ||
+ | | Referred to Orphan Well June, 2000. NEVER RECEIVED A WELL COMPLETION REPORT. WELL IS LEAKING OIL. I&O CASE # 2000 06 017. PERMIT EXPIRED | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | |}--> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | -2059686023 | |
+ | | 2014-6-12 0:00: | ||
+ | | OR | ||
+ | | No Violations | ||
+ | | | ||
+ | |- | ||
+ | | 000PL11434 | ||
+ | | | ||
+ | | Preliminary Restoration | ||
+ | | No Violations | ||
+ | | Preliminary Restoration done information from Data Point | ||
|- | |- | ||
| 1106708266 | | 1106708266 | ||
| 2014-01-13 | | 2014-01-13 | ||
− | | | + | | Orphan |
+ | | No Violations | ||
| Inspected orphan well with Norburt Lowder on 01/13/2014. Well consists of wellhead sitting on 4 1/2 casing within 7 casing. There is what appears to be a domestic gas hook-up for 2 houses present, and the line was open. Wellhead is within a concrete structure. Tank battery consists of 1-100 bbl steel tank, 1-75 bbl steel tank, and 1-25 bbl plastic tank that is caved in. Well identification was posted at the tank battery for all wells utilizing it. | | Inspected orphan well with Norburt Lowder on 01/13/2014. Well consists of wellhead sitting on 4 1/2 casing within 7 casing. There is what appears to be a domestic gas hook-up for 2 houses present, and the line was open. Wellhead is within a concrete structure. Tank battery consists of 1-100 bbl steel tank, 1-75 bbl steel tank, and 1-25 bbl plastic tank that is caved in. Well identification was posted at the tank battery for all wells utilizing it. | ||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 2059686023 |
− | |||
| 2014-06-12 | | 2014-06-12 | ||
− | | | + | | Orphan |
+ | | No Violations | ||
| Visited location on 06/12/2014 with Jeff Fry for a status update inspection at the request of Gene Chini. The well consists of an 8 wellhead with a homemade reducer and 2 tubing with a submersible pump. The well is located within a poured concrete structure. An old electric hook-up is present. GPS coordinates and pictures were taken to update the well file. | | Visited location on 06/12/2014 with Jeff Fry for a status update inspection at the request of Gene Chini. The well consists of an 8 wellhead with a homemade reducer and 2 tubing with a submersible pump. The well is located within a poured concrete structure. An old electric hook-up is present. GPS coordinates and pictures were taken to update the well file. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| PL11434 | | PL11434 | ||
| | | | ||
− | | | + | | PL |
− | | | + | | No Violations |
− | |||
− | |||
| | | | ||
|- | |- | ||
|} | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-103-24255 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":41.1,"lon":-82.06,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Medina | |
Municipality: Chatham Township | |
Operator Name: JESSE OIL | |
Well Pad ID: | |
Farm/Lease Name: CONLEY D& E | |
License Status: Orphan Well - Ready | |
License Date: 1985-08-20 | |
Spud Date: 1985-09-04 | |
Spud Drilling Contractor: D M WALTZ DRLG | |
Final Drill Date: | |
Well Total Depth: 0.00 ft | |
Configuration: Vertical | |
Latitude: 41.100000 | |
Longitude: -82.060000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-08-20 | 2223 JESSE OIL GeoDate 8/20/85 |
Oil and Gas | 1985-08-20 | Issued Date 8/20/85 Expired Date 8/20/86 Acres 0001000 Tool Type RTA Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1985-09-04 | Referred to Orphan Well June, 2000. NEVER RECEIVED A WELL COMPLETION REPORT. WELL IS LEAKING OIL. I&O CASE # 2000 06 017. PERMIT EXPIRED |
Construction Permit Expires | 1986-08-20 | Referred to Orphan Well June, 2000. NEVER RECEIVED A WELL COMPLETION REPORT. WELL IS LEAKING OIL. I&O CASE # 2000 06 017. PERMIT EXPIRED |
Changed to Orphan Well Ready | 2000-06-01 | Changed Well To Orphan Ready |
Record Last Modified | 2019-03-25 | Referred to Orphan Well June, 2000. NEVER RECEIVED A WELL COMPLETION REPORT. WELL IS LEAKING OIL. I&O CASE # 2000 06 017. PERMIT EXPIRED |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2059686023 | 2014-6-12 0:00: | OR | No Violations | |
000PL11434 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1106708266 | 2014-01-13 | Orphan | No Violations | Inspected orphan well with Norburt Lowder on 01/13/2014. Well consists of wellhead sitting on 4 1/2 casing within 7 casing. There is what appears to be a domestic gas hook-up for 2 houses present, and the line was open. Wellhead is within a concrete structure. Tank battery consists of 1-100 bbl steel tank, 1-75 bbl steel tank, and 1-25 bbl plastic tank that is caved in. Well identification was posted at the tank battery for all wells utilizing it. |
2059686023 | 2014-06-12 | Orphan | No Violations | Visited location on 06/12/2014 with Jeff Fry for a status update inspection at the request of Gene Chini. The well consists of an 8 wellhead with a homemade reducer and 2 tubing with a submersible pump. The well is located within a poured concrete structure. An old electric hook-up is present. GPS coordinates and pictures were taken to update the well file. |
PL11434 | PL | No Violations |
For data sources see[3]