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Difference between revisions of "34-081-20721"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-081-20721
 
| Well ID: 34-081-20721
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.351031856, -80.66734446 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.35, -80.66 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 11: Line 11:
 
| County: [[Jefferson_County,_Ohio|Jefferson]]
 
| County: [[Jefferson_County,_Ohio|Jefferson]]
 
|-
 
|-
| Municipality: [[Steubenville,_Ohio|Steubenville]]
+
| Municipality: [[Cross Creek_Township,_Jefferson_County,_Ohio|Cross Creek Township]]
 
|-
 
|-
 
| Operator Name: [[ASCENT RESOURCES UTICA LLC]]
 
| Operator Name: [[ASCENT RESOURCES UTICA LLC]]
Line 19: Line 19:
 
| Farm/Lease Name: HAMMACK W CRC JF
 
| Farm/Lease Name: HAMMACK W CRC JF
 
|-
 
|-
| License Status: Drilling
+
| License Status: Not Drilled
 
|-
 
|-
 
| License Date: 2017-03-30
 
| License Date: 2017-03-30
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| Spud Drilling Contractor:  
 
| Spud Drilling Contractor:  
 
|-
 
|-
| Final Drill Date:  
+
| Final Drill Date: 2017-06-06
 
|-
 
|-
| Well Total Depth:  
+
| Well Total Depth: 100.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Latitude: 40.351031856
+
| Latitude: 40.350000
 
|-
 
|-
| Longitude: -80.66734446
+
| Longitude: -80.660000
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Well History ==
 
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 65: Line 65:
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<!--== Perforation Treatments ==
 
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Comments
 
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| -2019902726
 +
| 2017-6-14 0:00:
 +
| DD
 +
| No Violations
 +
| 0.30
 +
|-
 +
| -25742503
 +
| 2019-7-22 0:00:
 +
| UD
 +
| No Violations
 +
| 1.00
 
|-
 
|-
 
| 0012713258
 
| 0012713258
Line 155: Line 167:
 
| No Violations
 
| No Violations
 
| I am on site today to witness the cementing of 30 inch conductor casing.  Precision Drilling drilled a 36 inch diameter hole to a depth of 100 feet and ran 100 feet of 30 inch diameter 118 pound per foot conductor casing.  O-Tex pumped 320 sacks of class A cement, 1.2 yield, 15.6 pounds per gallon with 1.5 percent Calcium Chloride and 0.25 pound per sack flow seal.  O-Tex then displaced with 74 barrels of water, leaving 10 feet of cement in the casing.  Cement did returns to surface then fell back.  During displacement water returned to surface in permit 3408120720, showing that the boreholes were communicating.  Both wells will be topped out on 6/7/17 using grout pumped through a 1 inch line.
 
| I am on site today to witness the cementing of 30 inch conductor casing.  Precision Drilling drilled a 36 inch diameter hole to a depth of 100 feet and ran 100 feet of 30 inch diameter 118 pound per foot conductor casing.  O-Tex pumped 320 sacks of class A cement, 1.2 yield, 15.6 pounds per gallon with 1.5 percent Calcium Chloride and 0.25 pound per sack flow seal.  O-Tex then displaced with 74 barrels of water, leaving 10 feet of cement in the casing.  Cement did returns to surface then fell back.  During displacement water returned to surface in permit 3408120720, showing that the boreholes were communicating.  Both wells will be topped out on 6/7/17 using grout pumped through a 1 inch line.
 +
|-
 +
| 12713258
 +
| 2017-6-8 0:00:0
 +
| CS
 +
| No Violations
 +
| 2.50
 
|-
 
|-
 
| 1497961341
 
| 1497961341
Line 167: Line 185:
 
| No Violations
 
| No Violations
 
| I spoke with Steve Perkins regarding complaint number 5624.  Ascent did a preliminary evaluation of the situation on 6/13/17.  Ascent plans to have the site engineer Rettew re-evaluate the drainage for the lower portion of the lease road to determine how best to alleviate the excess water issue.  They also determined that the mold growth within the structure was likely due to other issues.  Ascent indicated that they should have the drainage re-evaluation complete by 6/23, and would keep me aware of their plan.
 
| I spoke with Steve Perkins regarding complaint number 5624.  Ascent did a preliminary evaluation of the situation on 6/13/17.  Ascent plans to have the site engineer Rettew re-evaluate the drainage for the lower portion of the lease road to determine how best to alleviate the excess water issue.  They also determined that the mold growth within the structure was likely due to other issues.  Ascent indicated that they should have the drainage re-evaluation complete by 6/23, and would keep me aware of their plan.
 +
|-
 +
| 537276437
 +
| 2017-8-21 0:00:
 +
| DD
 +
| No Violations
 +
| 1.00
 
|-
 
|-
 
|}
 
|}
Line 181: Line 205:
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Ohio Wells]]
 
[[Category:Ohio Wells]]

Latest revision as of 19:55, 12 January 2021

Well Details

Well ID: 34-081-20721
Loading map...
Country: United States
State: Ohio
County: Jefferson
Municipality: Cross Creek Township
Operator Name: ASCENT RESOURCES UTICA LLC
Well Pad ID:
Farm/Lease Name: HAMMACK W CRC JF
License Status: Not Drilled
License Date: 2017-03-30
Spud Date: 2017-06-06
Spud Drilling Contractor:
Final Drill Date: 2017-06-06
Well Total Depth: 100.00 ft
Configuration: Vertical
Latitude: 40.350000
Longitude: -80.660000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2017-03-30 Proposed Formations:UTICA THROUGH POINT PLEASANT, Issued Date:3/30/2017, Expired Date:3/30/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
Construction Permit Expires 2018-03-30 CONDUCTOR ONLY SET
Record Last Modified 2018-05-17 CONDUCTOR ONLY SET

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2019902726 2017-6-14 0:00: DD No Violations 0.30
-25742503 2019-7-22 0:00: UD No Violations 1.00
0012713258 2017-06-08 Casing String Witnessed No Violations I am onsite to witness the topping out of the conductor annulus with cement. When I arrived I verified that the cement had fallen to approximately 3 feet below the bottom of the cellar. Smith Concrete topped the annulus out with grout mix. The floor of the cellar was brought to approximately 7 feet below ground surface, leaving an 18 inch floor of grout in the cellar.
0537276437 2017-08-21 Drill / Deepen / Reopen No Violations
1008832559 2017-06-06 Casing String Witnessed No Violations I am on site today to witness the cementing of 30 inch conductor casing. Precision Drilling drilled a 36 inch diameter hole to a depth of 100 feet and ran 100 feet of 30 inch diameter 118 pound per foot conductor casing. O-Tex pumped 320 sacks of class A cement, 1.2 yield, 15.6 pounds per gallon with 1.5 percent Calcium Chloride and 0.25 pound per sack flow seal. O-Tex then displaced with 74 barrels of water, leaving 10 feet of cement in the casing. Cement did returns to surface then fell back. During displacement water returned to surface in permit 3408120720, showing that the boreholes were communicating. Both wells will be topped out on 6/7/17 using grout pumped through a 1 inch line.
12713258 2017-6-8 0:00:0 CS No Violations 2.50
1497961341 2017-06-12 Drill / Deepen / Reopen No Violations
2019902726 2017-06-14 Drill / Deepen / Reopen No Violations I spoke with Steve Perkins regarding complaint number 5624. Ascent did a preliminary evaluation of the situation on 6/13/17. Ascent plans to have the site engineer Rettew re-evaluate the drainage for the lower portion of the lease road to determine how best to alleviate the excess water issue. They also determined that the mold growth within the structure was likely due to other issues. Ascent indicated that they should have the drainage re-evaluation complete by 6/23, and would keep me aware of their plan.
537276437 2017-8-21 0:00: DD No Violations 1.00

For data sources see[3]

References