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Difference between revisions of "34-059-24292"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-059-24292
 
| Well ID: 34-059-24292
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.98873256, -81.38636609 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.98, -81.38 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Guernsey County, Ohio|Guernsey]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[PDC ENERGY INC]]
+
| County: [[Guernsey_County,_Ohio|Guernsey]]
 
|-
 
|-
| Well Pad ID:  
+
| Municipality: [[Richland_Township,_Guernsey_County,_Ohio|Richland Township]]
 
|-
 
|-
| Farm/Lease Name:  
+
| Operator Name: [[UTICA RESOURCE OPERATING LLC]]
 
|-
 
|-
| First Permit Date:  
+
| Well Pad ID: [[US-OH-000560]]
 
|-
 
|-
| Last Permit Date:  
+
| Farm/Lease Name: DETWEILER
 +
|-
 +
| License Status: Producing
 +
|-
 +
| License Date: 2013-06-27
 
|-
 
|-
 
| Spud Date: 2013-08-02
 
| Spud Date: 2013-08-02
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[H&P DRILLING]]
 +
|-
 +
| Final Drill Date: 2013-08-23
 +
|-
 +
| Well Total Depth: 12637.00 ft
 +
|-
 +
| Configuration: Horizontal
 +
|-
 +
| Latitude: 39.980000
 +
|-
 +
| Longitude: -81.380000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| APP
 +
| 2013-06-12
 +
| Proposed Formations:POINT PLEASANT, Issued Date:6/12/2013, Expired Date:6/12/2015 12:00:00 PM, Drilling unit acres:541, Proposed Well Type:OG, Proposed Well Class:EDPW
 
|-
 
|-
| Configuration: Vertical
+
| APP
 +
| 2013-06-27
 +
| Proposed Formations:POINT PLEASANT, Issued Date:6/27/2013, Expired Date:6/27/2015 12:00:00 PM, Drilling unit acres:541, Proposed Well Type:OG, Proposed Well Class:EDPW
 
|-
 
|-
| Well Status: Producing
+
| Reached Total Depth
 +
| 2013-08-23
 +
| FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING  (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
 
|-
 
|-
| Violations: 0
+
| Correction to Well
 +
| 2014-02-07
 +
| CHANGE IN SURFACE AND TAKE-POINT INFORMATION (FOOTAGE AND COORDINATES) FROM AS DRILLED SURVEY PLAT.  UNIT SIZE CHANGED TO 538.60 ACRES.
 
|-
 
|-
| Latitude: 39.98873256
+
| Completion Report Received
 +
| 2014-02-11
 +
| FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING  (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
 
|-
 
|-
| Longitude: -81.38636609
+
| Construction Permit Expires
 +
| 2015-06-27
 +
| FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING  (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
 +
|-
 +
| Change of Owner
 +
| 2018-05-04
 +
| Operator changed from 8595, PDC ENERGY INC to 10114, UTICA RESOURCE OPERATING LLC
 +
|-
 +
| Record Last Modified
 +
| 2019-01-22
 +
| FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING  (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | CONDENSATE PRODUCTION DAYS
+
|-
!scope="col" | OIL QUANTITY
+
| 2014-03-04
!scope="col" | OIL PRODUCTION DAYS
+
| style="text-align: right;" | 0
 +
| style="text-align: right;" |  
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2013-12
 
| style="text-align:right;" | 53450.0
 
 
|  
 
|  
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 0
 +
|-
 
|  
 
|  
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 12116.0
+
| style="text-align: right;" |
|  
+
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
| 1
 +
| 09/15/2013
 +
| 10/15/2013
 +
| style="text-align: right;" | 7000
 +
| style="text-align: right;" | 6,091,010.0
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|- valign="top"
 +
| rowspan="26"| 1
 +
| rowspan="1"| Ferrotrol 300L
 +
| rowspan="1"| Baker Hughes
 +
| rowspan="1"| Iron Control
 +
| Citric acid
 +
| 77-92-9
 +
| style="text-align: right;" | 70
 +
| style="text-align: right;" | 0.003339
 +
| style="text-align: right;" | 1954.95
 +
|-
 +
|- valign="top"
 +
| rowspan="3"| XLW-32
 +
| rowspan="3"| Baker Hughes
 +
| rowspan="3"| Crosslinker
 +
| Methyl borate
 +
| 121-43-7
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.00938141
 +
| style="text-align: right;" | 5492.7
 +
|-
 +
| Boric acid
 +
| 10043-35-3
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.00938141
 +
| style="text-align: right;" | 5492.7
 +
|-
 +
| Methanol
 +
| 67-56-1
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.0187628
 +
| style="text-align: right;" | 10985.4
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| CL-14
 +
| rowspan="2"| Baker Hughes
 +
| rowspan="2"| Corrosion Inhibitor
 +
| Methanol
 +
| 67-56-1
 +
| style="text-align: right;" | 67
 +
| style="text-align: right;" | 0.000553701
 +
| style="text-align: right;" | 324.185
 +
|-
 +
| Propargyl alcohol
 +
| NA
 +
| style="text-align: right;" | 4
 +
| style="text-align: right;" | 0.00003306
 +
| style="text-align: right;" | 19.354
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| FRW-18
 +
| rowspan="1"| Baker Hughes
 +
| rowspan="1"| Friction Reducer
 +
| Hydrotreated light distillate
 +
| 64742-47-8
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.0316946
 +
| style="text-align: right;" | 18556.8
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| BF-9L
 +
| rowspan="2"| Baker Hughes
 +
| rowspan="2"| Buffer
 +
| Potassium hydroxide
 +
| 1310-58-3
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.0156731
 +
| style="text-align: right;" | 9176.4
 +
|-
 +
| Potassium carbonate
 +
| 584-08-7
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.0313462
 +
| style="text-align: right;" | 18352.8
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Hydrochloric Acid (15%)
 +
| rowspan="1"| Baker Hughes
 +
| rowspan="1"| Acidizing
 +
| Hydrochloric Acid
 +
| 7647-01-0
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 0.0764064
 +
| style="text-align: right;" | 44735
 +
|-
 +
|- valign="top"
 +
| rowspan="5"| Alpha 1427
 +
| rowspan="5"| Baker Hughes
 +
| rowspan="5"| Biocide
 +
| Glutaraldehyde
 +
| 111-30-8
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.00674954
 +
| style="text-align: right;" | 3951.78
 +
|-
 +
| Quaternary ammonium chloride
 +
| 7173-51-5
 +
| style="text-align: right;" | 10
 +
| style="text-align: right;" | 0.00224985
 +
| style="text-align: right;" | 1317.26
 +
|-
 +
| Alkyl dimethyl benzyl ammonium chloride (c12-16)
 +
| 68424-85-1
 +
| style="text-align: right;" | 7
 +
| style="text-align: right;" | 0.00157489
 +
| style="text-align: right;" | 922.081
 +
|-
 +
| Water
 +
| 7732-18-5
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.0134991
 +
| style="text-align: right;" | 7903.55
 +
|-
 +
| Ethanol
 +
| 64-17-5
 +
| style="text-align: right;" | 5
 +
| style="text-align: right;" | 0.00112492
 +
| style="text-align: right;" | 658.629
 +
|-
 +
|- valign="top"
 +
| rowspan="3"| Gasflo G
 +
| rowspan="3"| Baker Hughes
 +
| rowspan="3"| Surfactant
 +
| Water
 +
| 7732-18-5
 +
| style="text-align: right;" | 70
 +
| style="text-align: right;" | 0.0564196
 +
| style="text-align: right;" | 33033
 +
|-
 +
| Methanol
 +
| 67-56-1
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.0241798
 +
| style="text-align: right;" | 14157
 +
|-
 +
| Surfactants
 +
| NA
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.0483596
 +
| style="text-align: right;" | 28314
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| GW-3LDF
 +
| rowspan="2"| Baker Hughes
 +
| rowspan="2"| Gellant
 +
| Petroleum Distillate Blend
 +
| Proprietary
 +
| style="text-align: right;" | 70
 +
| style="text-align: right;" | 0.162834
 +
| style="text-align: right;" | 95337.4
 +
|-
 +
| Guar Gum
 +
| 9000-30-0
 +
| style="text-align: right;" | 40
 +
| style="text-align: right;" | 0.0930481
 +
| style="text-align: right;" | 54478.5
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| GBW-5
 +
| rowspan="1"| Baker Hughes
 +
| rowspan="1"| Water
 +
| Ammonium Persulfate
 +
| 7727-54-0
 +
| style="text-align: right;" | 98
 +
| style="text-align: right;" | 0.00103609
 +
| style="text-align: right;" | 606.62
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Water
 +
| rowspan="1"| Operator
 +
| rowspan="1"| Carrier/Base Fluid
 +
| Water
 +
| 7732-18-5
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 84.1972
 +
| style="text-align: right;" | 49,296,400.0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Enzyme G-NE
 +
| rowspan="1"| Baker Hughes
 +
| rowspan="1"| Breaker
 +
| Enzyme G-NE
 +
| NA
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.029601
 +
| style="text-align: right;" | 17331
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| Scaletrol 720
 +
| rowspan="2"| Baker Hughes
 +
| rowspan="2"| Scale Inhibitor
 +
| Ethylene glycol
 +
| NA
 +
| style="text-align: right;" | 44
 +
| style="text-align: right;" | 0.0102764
 +
| style="text-align: right;" | 6016.72
 +
|-
 +
| Diethylene glycol
 +
| 111-46-6
 +
| style="text-align: right;" | 4
 +
| style="text-align: right;" | 0.00093422
 +
| style="text-align: right;" | 546.975
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Sand (Proppant)
 +
| rowspan="1"| Baker Hughes
 +
| rowspan="1"| Proppant
 +
| Silica Substrate
 +
| NA
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 14.709
 +
| style="text-align: right;" | 8,611,920.0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = FracFocus Fracking Chemicals Database
 +
| date = 2019-04-02
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-06-19 }}</ref>
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
| 2013-09-18
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 613900 Bbl
 +
| style="text-align: right;" | 347187
 +
| [[BAKER-HUGHES]]
 +
| STAGE 5, 60 SHOTS
 +
|-
 +
| 2013-09-25
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 617300 Bbl
 +
| style="text-align: right;" | 381725
 +
| [[BAKER-HUGHES]]
 +
| STAGE 13, 60 SHOTS
 +
|-
 +
| 2013-09-27
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 665700 Bbl
 +
| style="text-align: right;" | 377753
 +
| [[BAKER-HUGHES]]
 +
| STAGE 16, 60 SHOTS
 +
|-
 +
| 2013-09-23
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 670000 Bbl
 +
| style="text-align: right;" | 421836
 +
| [[BAKER-HUGHES]]
 +
| STAGE 22, 60 SHOTS
 +
|-
 +
| 2013-09-17
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 727600 Bbl
 +
| style="text-align: right;" | 380585
 +
| [[BAKER-HUGHES]]
 +
| STAGE 4, 60 SHOTS
 +
|-
 +
| 2013-09-28
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 910200 Bbl
 +
| style="text-align: right;" | 379186
 +
| [[BAKER-HUGHES]]
 +
| STAGE 18, 30 SHOTS
 +
|-
 +
| 2013-09-16
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 524700 Bbl
 +
| style="text-align: right;" | 150259
 +
| [[BAKER-HUGHES]]
 +
| STAGE 2, 60 SHOTS
 +
|-
 +
| 2013-09-15
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 658800 Bbl
 +
| style="text-align: right;" | 377140
 +
| [[BAKER-HUGHES]]
 +
| STAGE 1, 60 SHOTS
 +
|-
 +
| 2013-09-19
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 613100 Bbl
 +
| style="text-align: right;" | 371257
 +
| [[BAKER-HUGHES]]
 +
| STAGE 6, 60 SHOTS
 +
|-
 +
| 2013-09-29
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 577200 Bbl
 +
| style="text-align: right;" | 322823
 +
| [[BAKER-HUGHES]]
 +
| STAGE 21, 60 SHOTS
 +
|-
 +
| 2013-09-24
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 628400 Bbl
 +
| style="text-align: right;" | 376084
 +
| [[BAKER-HUGHES]]
 +
| STAGE 12, 60 SHOTS
 +
|-
 +
| 2013-09-28
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 604900 Bbl
 +
| style="text-align: right;" | 364767
 +
| [[BAKER-HUGHES]]
 +
| STAGE 19, 60 SHOTS
 +
|-
 +
| 2013-09-23
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 622000 Bbl
 +
| style="text-align: right;" | 387630
 +
| [[BAKER-HUGHES]]
 +
| STAGE 10, 60 SHOTS
 +
|-
 +
| 2013-09-20
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 627800 Bbl
 +
| style="text-align: right;" | 381141
 +
| [[BAKER-HUGHES]]
 +
| STAGE 8, 60 SHOTS
 +
|-
 +
| 2013-09-17
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 626500 Bbl
 +
| style="text-align: right;" | 373121
 +
| [[BAKER-HUGHES]]
 +
| STAGE 3, 60 SHOTS
 +
|-
 +
| 2013-09-24
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 595300 Bbl
 +
| style="text-align: right;" | 372571
 +
| [[BAKER-HUGHES]]
 +
| STAGE 11, 60 SHOTS
 +
|-
 +
| 2013-09-21
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 610800 Bbl
 +
| style="text-align: right;" | 380577
 +
| [[BAKER-HUGHES]]
 +
| STAGE 9, 60 SHOTS
 +
|-
 +
| 2013-09-29
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 572400 Bbl
 +
| style="text-align: right;" | 372165
 +
| [[BAKER-HUGHES]]
 +
| STAGE 20, 60 SHOTS
 +
|-
 +
| 2013-09-20
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 604500 Bbl
 +
| style="text-align: right;" | 373569
 +
| [[BAKER-HUGHES]]
 +
| STAGE 7, 60 SHOTS
 +
|-
 +
| 2013-09-27
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 595500 Bbl
 +
| style="text-align: right;" | 375620
 +
| [[BAKER-HUGHES]]
 +
| STAGE 17, 60 SHOTS
 +
|-
 +
| 2013-09-26
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 708300 Bbl
 +
| style="text-align: right;" | 376817
 +
| [[BAKER-HUGHES]]
 +
| STAGE 14, 60 SHOTS
 +
|-
 +
| 2013-09-26
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 609100 Bbl
 +
| style="text-align: right;" | 373646
 +
| [[BAKER-HUGHES]]
 +
| STAGE 15, 60 SHOTS
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2013
 +
| [[PDC ENERGY INC]]
 +
| style="text-align: right;" | 53450
 +
| style="text-align: right;" | 12116
 +
| style="text-align: right;" | 26
 +
|-
 +
| 2014
 +
| [[PDC ENERGY INC]]
 +
| style="text-align: right;" | 328671
 +
| style="text-align: right;" | 72022
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2015
 +
| [[PDC ENERGY INC]]
 +
| style="text-align: right;" | 171527
 +
| style="text-align: right;" | 26659
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2016
 +
| [[PDC ENERGY INC]]
 +
| style="text-align: right;" | 118846
 +
| style="text-align: right;" | 17179
 +
| style="text-align: right;" | 366
 +
|-
 +
| 2017
 +
| [[PDC ENERGY INC]]
 +
| style="text-align: right;" | 98323
 +
| style="text-align: right;" | 12240
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 2018
 +
| [[UTICA RESOURCE OPERATING LLC]]
 +
| style="text-align: right;" | 83815
 +
| style="text-align: right;" | 6794
 +
| style="text-align: right;" | 364
 
|-
 
|-
| 2014-1
+
| 2019
| style="text-align:right;" | 102886.0
+
| [[UTICA RESOURCE OPERATING LLC]]
| style="text-align:right;" | 90.0
+
| style="text-align: right;" | 16364
|
+
| style="text-align: right;" | 1672
|
+
| style="text-align: right;" | 90
| style="text-align:right;" | 24808.0
 
| style="text-align:right;" | 90.0
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 2014-2
+
| 2013
| style="text-align:right;" | 89418.0
+
| [[PDC ENERGY INC]]
| style="text-align:right;" | 91.0
+
| Brine
|  
+
| style="text-align: right;" | 6572
|  
+
| style="text-align: right;" | 26
| style="text-align:right;" | 20232.0
 
| style="text-align:right;" | 91.0
 
 
|-
 
|-
 +
| 2014
 +
| [[PDC ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 17708
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2014-3
+
| 2015
| style="text-align:right;" | 70925.0
+
| [[PDC ENERGY INC]]
| style="text-align:right;" | 92.0
+
| Brine
|  
+
| style="text-align: right;" | 5531
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 14700.0
 
| style="text-align:right;" | 92.0
 
 
|-
 
|-
 +
| 2016
 +
| [[PDC ENERGY INC]]
 +
| Brine
 +
| style="text-align: right;" | 2293
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 2015-1
+
| 2017
| style="text-align:right;" | 54777.0
+
| [[PDC ENERGY INC]]
| style="text-align:right;" | 90.0
+
| Brine
|  
+
| style="text-align: right;" | 1991
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 8969.0
 
| style="text-align:right;" | 90.0
 
 
|-
 
|-
 +
| 2018
 +
| [[UTICA RESOURCE OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 939
 +
| style="text-align: right;" | 273
 
|-
 
|-
| 2014-4
+
| 2019
| style="text-align:right;" | 65442.0
+
| [[UTICA RESOURCE OPERATING LLC]]
| style="text-align:right;" | 92.0
+
| Brine
|  
+
| style="text-align: right;" | 299
|  
+
| style="text-align: right;" | 90
| style="text-align:right;" | 12282.0
 
| style="text-align:right;" | 92.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
 
| -1277941116
 
| -1277941116
 +
| 2013-8-5 0:00:0
 +
| DD
 +
| No Violations
 +
| 6.00
 +
|-
 +
| -1497234997
 +
| 2019-4-30 0:00:
 +
| PW
 +
| No Violations
 +
| 0.30
 +
|-
 +
| -273209696
 +
| 2020-7-22 0:00:
 +
| PW
 +
| No Violations
 +
| 1.00
 +
|-
 +
| 0020708993
 +
| 2014-01-28
 +
| Preliminary Restoration
 +
| No Violations
 +
| The site passed preliminary restoration according to 1509.072A.
 +
|-
 +
| 0237133591
 +
| 2017-10-24
 +
| Production Wells
 +
| No Violations
 +
| On the day of my inspection I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500 barrel tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Gauge present read 240 pounds per square inch on the tubing and 465 pounds per square inch on the casing. Identification was present with production records current.
 +
|-
 +
| 0673784731
 +
| 2015-07-16
 +
| Production Wells
 +
| No Violations
 +
| On the day of my inspection I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500bbl tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Gauge present read 850psi on the tubing. Identification was present with production records current.
 +
|-
 +
| 1277941116
 
| 2013-08-05
 
| 2013-08-05
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| On the evening of my inspection I witnessed Universal displace one thousand four hundred twenty five sacks of type 1, gas block with 2% calcium, 15% cr-3,25% celloflake, the cement density was 15.7 with a yield of 1.29, I witnessed 67 barrels of cement returns.
 
| On the evening of my inspection I witnessed Universal displace one thousand four hundred twenty five sacks of type 1, gas block with 2% calcium, 15% cr-3,25% celloflake, the cement density was 15.7 with a yield of 1.29, I witnessed 67 barrels of cement returns.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1375755089
 
| 1375755089
 
| 2013-08-05
 
| 2013-08-05
|  
+
| Drill / Deepen / Reopen
| I am on site today training with Mike Hartshorn and witnessed that PDC Energy Inc. H&P Flex Rig 385 drilled a 17.5 hole to the depth of 1979' and set 1934
+
| No Violations
|
+
 
|  
 
|
 
|-
 
 
|-
 
|-
 
| 1375793519
 
| 1375793519
 
| 2013-08-05
 
| 2013-08-05
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| On the evening of my inspection, I witnessed Universal displace six hundred forty sacks of type 1, 3% calcium, the cement density was 15.6 with a yield of 1.20, I witnessed three barrel of cement returns.
 
| On the evening of my inspection, I witnessed Universal displace six hundred forty sacks of type 1, 3% calcium, the cement density was 15.6 with a yield of 1.20, I witnessed three barrel of cement returns.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1377027166
 
| 1377027166
 
| 2013-08-20
 
| 2013-08-20
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| On the day of my inspection, the drilling rig was not drilling due to a pump issue, there 9.625 casing has been cemented back to surface.
 
| On the day of my inspection, the drilling rig was not drilling due to a pump issue, there 9.625 casing has been cemented back to surface.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1458061136
 +
| 2016-03-15
 +
| Production Wells
 +
| No Violations
 +
| On the day inspection following up on complaint ID 5259, I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500bbl tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Completed walk around with PDC Well Technician Carl Caplinger revealing equipment was functioning properly.
 +
|-
 +
| 1482240186
 +
| 2016-12-20
 +
| Production Wells
 +
| No Violations
 +
| On the day of my inspection I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500 barrel tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Gauge present read 110 pounds per square inch on the tubing and 590 pounds per square inch on the casing. Identification was present with production records current.
 +
|-
 +
| 1497234997
 +
| 2019-04-30
 +
| Production Wells
 +
| No Violations
 +
| The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with production valves in the open position. Annular pressure monitoring was present. The production equipment consisted of eight 500-barrel tanks with three vapor recovery towers, three gas production units, one gas compression skid, horizontal vent scrubber, and one combustor. Identification was present and production records were current. An ECM tanker truck was loading produced fluids from the tank battery and a Utica Resources well tender was present.
 +
|-
 +
| 1942578433
 +
| 2018-05-03
 +
| Production Wells
 +
| No Violations
 +
| The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with production valves in the open position. The gauge on the production casing read 406 and the gauge on the production tubing read 362. Annular pressure monitoring was present. The production equipment consisted of eight 500 barrel tanks with three vapor recovery towers, three gas production units, one gas compression skid, horizontal vent scrubber, and one combustor. Identification was present and production records were current.
 
|-
 
|-
 
| 20708993
 
| 20708993
| 2014-01-28
+
| 2014-1-28 0:00:
|  
+
| PL
| The site passed preliminary restoration according to 1509.072A.
+
| No Violations
|  
+
| 0.50
|  
+
|-
|  
+
| 2136016696
 +
| 2016-02-24
 +
| Production Wells
 +
| No Violations
 +
|  Inspection response to complaint # 5259. Upon inspection the following was observed at the well head- the well is equipped with a tubing head and casing head with the production flow line valve in the open position. Addressing the production facility and equipment- a total of (8) production tanks are present along with 3 vertical sand trap separators all located inside a polymer lined metal containment dike area. Also on location is 3 gas processing units processing the fluid from the 3 existing wells on location. Supporting the production facility is a low pressure vapor recovery system that is supported by a vapor recover burner system that is on the day of my inspection operating, with the vapor recovery ignition stack found to be located at a coordinates of 39.98900 x 81.38609. Addressing the complaint- On the day of my inspection the wind is noted to be coming from the East and the residence of the individual at 61100 Buzz Kirk Lane does lie a measured distance of 2600 approximately due West and downwind of the well pad. The coordinates for the home is 39.98609 x 81.39547. On this day I did contact a Blake Roush with PDC Energy at 970-260-7028 and inform Him that the landowner identified as Lee Ann Rudd has filed a complaint indicating she is getting a caustic smell during the evening hours inside Her home with the strongest odor between 1:30am and 2:00am. Mr. Roush Indicated the company would follow up on the issue. No compliance issues were present the well pad on the day of my inspection and no gas reading were detected with my meter in the area of the residence or well pad.
 +
|-
 +
| 237133591
 +
| 2017-10-24 0:00
 +
| PW
 +
| No Violations
 +
| 0.50
 +
|-
 +
| 673784731
 +
| 2015-7-16 0:00:
 +
| PW
 +
| No Violations
 +
| 0.50
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]
 +
[[Category:FracFocus]]

Latest revision as of 21:33, 12 January 2021

Well Details

Well ID: 34-059-24292
Loading map...
Country: United States
State: Ohio
County: Guernsey
Municipality: Richland Township
Operator Name: UTICA RESOURCE OPERATING LLC
Well Pad ID: US-OH-000560
Farm/Lease Name: DETWEILER
License Status: Producing
License Date: 2013-06-27
Spud Date: 2013-08-02
Spud Drilling Contractor: H&P DRILLING
Final Drill Date: 2013-08-23
Well Total Depth: 12637.00 ft
Configuration: Horizontal
Latitude: 39.980000
Longitude: -81.380000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-06-12 Proposed Formations:POINT PLEASANT, Issued Date:6/12/2013, Expired Date:6/12/2015 12:00:00 PM, Drilling unit acres:541, Proposed Well Type:OG, Proposed Well Class:EDPW
APP 2013-06-27 Proposed Formations:POINT PLEASANT, Issued Date:6/27/2013, Expired Date:6/27/2015 12:00:00 PM, Drilling unit acres:541, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2013-08-23 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
Correction to Well 2014-02-07 CHANGE IN SURFACE AND TAKE-POINT INFORMATION (FOOTAGE AND COORDINATES) FROM AS DRILLED SURVEY PLAT. UNIT SIZE CHANGED TO 538.60 ACRES.
Completion Report Received 2014-02-11 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
Construction Permit Expires 2015-06-27 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
Change of Owner 2018-05-04 Operator changed from 8595, PDC ENERGY INC to 10114, UTICA RESOURCE OPERATING LLC
Record Last Modified 2019-01-22 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2014-03-04 0 0
0 0
0 0

For data sources see[3]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 09/15/2013 10/15/2013 7000 6,091,010.0 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Ferrotrol 300L Baker Hughes Iron Control Citric acid 77-92-9 70 0.003339 1954.95
XLW-32 Baker Hughes Crosslinker Methyl borate 121-43-7 30 0.00938141 5492.7
Boric acid 10043-35-3 30 0.00938141 5492.7
Methanol 67-56-1 60 0.0187628 10985.4
CL-14 Baker Hughes Corrosion Inhibitor Methanol 67-56-1 67 0.000553701 324.185
Propargyl alcohol NA 4 0.00003306 19.354
FRW-18 Baker Hughes Friction Reducer Hydrotreated light distillate 64742-47-8 30 0.0316946 18556.8
BF-9L Baker Hughes Buffer Potassium hydroxide 1310-58-3 30 0.0156731 9176.4
Potassium carbonate 584-08-7 60 0.0313462 18352.8
Hydrochloric Acid (15%) Baker Hughes Acidizing Hydrochloric Acid 7647-01-0 15 0.0764064 44735
Alpha 1427 Baker Hughes Biocide Glutaraldehyde 111-30-8 30 0.00674954 3951.78
Quaternary ammonium chloride 7173-51-5 10 0.00224985 1317.26
Alkyl dimethyl benzyl ammonium chloride (c12-16) 68424-85-1 7 0.00157489 922.081
Water 7732-18-5 60 0.0134991 7903.55
Ethanol 64-17-5 5 0.00112492 658.629
Gasflo G Baker Hughes Surfactant Water 7732-18-5 70 0.0564196 33033
Methanol 67-56-1 30 0.0241798 14157
Surfactants NA 60 0.0483596 28314
GW-3LDF Baker Hughes Gellant Petroleum Distillate Blend Proprietary 70 0.162834 95337.4
Guar Gum 9000-30-0 40 0.0930481 54478.5
GBW-5 Baker Hughes Water Ammonium Persulfate 7727-54-0 98 0.00103609 606.62
Water Operator Carrier/Base Fluid Water 7732-18-5 100 84.1972 49,296,400.0
Enzyme G-NE Baker Hughes Breaker Enzyme G-NE NA 100 0.029601 17331
Scaletrol 720 Baker Hughes Scale Inhibitor Ethylene glycol NA 44 0.0102764 6016.72
Diethylene glycol 111-46-6 4 0.00093422 546.975
Sand (Proppant) Baker Hughes Proppant Silica Substrate NA 100 14.709 8,611,920.0

For data sources see[4]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2013-09-18 H2O 15 613900 Bbl 347187 BAKER-HUGHES STAGE 5, 60 SHOTS
2013-09-25 H2O 15 617300 Bbl 381725 BAKER-HUGHES STAGE 13, 60 SHOTS
2013-09-27 H2O 15 665700 Bbl 377753 BAKER-HUGHES STAGE 16, 60 SHOTS
2013-09-23 H2O 15 670000 Bbl 421836 BAKER-HUGHES STAGE 22, 60 SHOTS
2013-09-17 H2O 15 727600 Bbl 380585 BAKER-HUGHES STAGE 4, 60 SHOTS
2013-09-28 H2O 15 910200 Bbl 379186 BAKER-HUGHES STAGE 18, 30 SHOTS
2013-09-16 H2O 15 524700 Bbl 150259 BAKER-HUGHES STAGE 2, 60 SHOTS
2013-09-15 H2O 15 658800 Bbl 377140 BAKER-HUGHES STAGE 1, 60 SHOTS
2013-09-19 H2O 15 613100 Bbl 371257 BAKER-HUGHES STAGE 6, 60 SHOTS
2013-09-29 H2O 15 577200 Bbl 322823 BAKER-HUGHES STAGE 21, 60 SHOTS
2013-09-24 H2O 15 628400 Bbl 376084 BAKER-HUGHES STAGE 12, 60 SHOTS
2013-09-28 H2O 15 604900 Bbl 364767 BAKER-HUGHES STAGE 19, 60 SHOTS
2013-09-23 H2O 15 622000 Bbl 387630 BAKER-HUGHES STAGE 10, 60 SHOTS
2013-09-20 H2O 15 627800 Bbl 381141 BAKER-HUGHES STAGE 8, 60 SHOTS
2013-09-17 H2O 15 626500 Bbl 373121 BAKER-HUGHES STAGE 3, 60 SHOTS
2013-09-24 H2O 15 595300 Bbl 372571 BAKER-HUGHES STAGE 11, 60 SHOTS
2013-09-21 H2O 15 610800 Bbl 380577 BAKER-HUGHES STAGE 9, 60 SHOTS
2013-09-29 H2O 15 572400 Bbl 372165 BAKER-HUGHES STAGE 20, 60 SHOTS
2013-09-20 H2O 15 604500 Bbl 373569 BAKER-HUGHES STAGE 7, 60 SHOTS
2013-09-27 H2O 15 595500 Bbl 375620 BAKER-HUGHES STAGE 17, 60 SHOTS
2013-09-26 H2O 15 708300 Bbl 376817 BAKER-HUGHES STAGE 14, 60 SHOTS
2013-09-26 H2O 15 609100 Bbl 373646 BAKER-HUGHES STAGE 15, 60 SHOTS

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 PDC ENERGY INC 53450 12116 26
2014 PDC ENERGY INC 328671 72022 365
2015 PDC ENERGY INC 171527 26659 365
2016 PDC ENERGY INC 118846 17179 366
2017 PDC ENERGY INC 98323 12240 365
2018 UTICA RESOURCE OPERATING LLC 83815 6794 364
2019 UTICA RESOURCE OPERATING LLC 16364 1672 90

For data sources see[6] [7]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 PDC ENERGY INC Brine 6572 26
2014 PDC ENERGY INC Brine 17708 365
2015 PDC ENERGY INC Brine 5531 365
2016 PDC ENERGY INC Brine 2293 366
2017 PDC ENERGY INC Brine 1991 365
2018 UTICA RESOURCE OPERATING LLC Brine 939 273
2019 UTICA RESOURCE OPERATING LLC Brine 299 90

For data sources see[8] [9]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1277941116 2013-8-5 0:00:0 DD No Violations 6.00
-1497234997 2019-4-30 0:00: PW No Violations 0.30
-273209696 2020-7-22 0:00: PW No Violations 1.00
0020708993 2014-01-28 Preliminary Restoration No Violations The site passed preliminary restoration according to 1509.072A.
0237133591 2017-10-24 Production Wells No Violations On the day of my inspection I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500 barrel tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Gauge present read 240 pounds per square inch on the tubing and 465 pounds per square inch on the casing. Identification was present with production records current.
0673784731 2015-07-16 Production Wells No Violations On the day of my inspection I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500bbl tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Gauge present read 850psi on the tubing. Identification was present with production records current.
1277941116 2013-08-05 Drill / Deepen / Reopen No Violations On the evening of my inspection I witnessed Universal displace one thousand four hundred twenty five sacks of type 1, gas block with 2% calcium, 15% cr-3,25% celloflake, the cement density was 15.7 with a yield of 1.29, I witnessed 67 barrels of cement returns.
1375755089 2013-08-05 Drill / Deepen / Reopen No Violations
1375793519 2013-08-05 Drill / Deepen / Reopen No Violations On the evening of my inspection, I witnessed Universal displace six hundred forty sacks of type 1, 3% calcium, the cement density was 15.6 with a yield of 1.20, I witnessed three barrel of cement returns.
1377027166 2013-08-20 Drill / Deepen / Reopen No Violations On the day of my inspection, the drilling rig was not drilling due to a pump issue, there 9.625 casing has been cemented back to surface.
1458061136 2016-03-15 Production Wells No Violations On the day inspection following up on complaint ID 5259, I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500bbl tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Completed walk around with PDC Well Technician Carl Caplinger revealing equipment was functioning properly.
1482240186 2016-12-20 Production Wells No Violations On the day of my inspection I witnessed that the production equipment included a GP Unit, a vapor recovery system, a gas combustor and a total of 8-500 barrel tanks all within containment and shared with the 2H and 42-3H. The well was equipped with a plunger lift system with valves in the open position. Gauge present read 110 pounds per square inch on the tubing and 590 pounds per square inch on the casing. Identification was present with production records current.
1497234997 2019-04-30 Production Wells No Violations The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with production valves in the open position. Annular pressure monitoring was present. The production equipment consisted of eight 500-barrel tanks with three vapor recovery towers, three gas production units, one gas compression skid, horizontal vent scrubber, and one combustor. Identification was present and production records were current. An ECM tanker truck was loading produced fluids from the tank battery and a Utica Resources well tender was present.
1942578433 2018-05-03 Production Wells No Violations The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with production valves in the open position. The gauge on the production casing read 406 and the gauge on the production tubing read 362. Annular pressure monitoring was present. The production equipment consisted of eight 500 barrel tanks with three vapor recovery towers, three gas production units, one gas compression skid, horizontal vent scrubber, and one combustor. Identification was present and production records were current.
20708993 2014-1-28 0:00: PL No Violations 0.50
2136016696 2016-02-24 Production Wells No Violations Inspection response to complaint # 5259. Upon inspection the following was observed at the well head- the well is equipped with a tubing head and casing head with the production flow line valve in the open position. Addressing the production facility and equipment- a total of (8) production tanks are present along with 3 vertical sand trap separators all located inside a polymer lined metal containment dike area. Also on location is 3 gas processing units processing the fluid from the 3 existing wells on location. Supporting the production facility is a low pressure vapor recovery system that is supported by a vapor recover burner system that is on the day of my inspection operating, with the vapor recovery ignition stack found to be located at a coordinates of 39.98900 x 81.38609. Addressing the complaint- On the day of my inspection the wind is noted to be coming from the East and the residence of the individual at 61100 Buzz Kirk Lane does lie a measured distance of 2600 approximately due West and downwind of the well pad. The coordinates for the home is 39.98609 x 81.39547. On this day I did contact a Blake Roush with PDC Energy at 970-260-7028 and inform Him that the landowner identified as Lee Ann Rudd has filed a complaint indicating she is getting a caustic smell during the evening hours inside Her home with the strongest odor between 1:30am and 2:00am. Mr. Roush Indicated the company would follow up on the issue. No compliance issues were present the well pad on the day of my inspection and no gas reading were detected with my meter in the area of the residence or well pad.
237133591 2017-10-24 0:00 PW No Violations 0.50
673784731 2015-7-16 0:00: PW No Violations 0.50

For data sources see[10]

References