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Difference between revisions of "34-081-61055"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-081-61055
 
| Well ID: 34-081-61055
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.503764657, -80.69240188 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.5, -80.69 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
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| County: [[Jefferson_County,_Ohio|Jefferson]]
 
| County: [[Jefferson_County,_Ohio|Jefferson]]
 
|-
 
|-
| Municipality: [[Knox Township,_Jefferson_County,_Ohio|Knox Township]]
+
| Municipality: [[Knox_Township,_Jefferson_County,_Ohio|Knox Township]]
 
|-
 
|-
 
| Operator Name: [[FIRSTENERGY GENERATION LLC]]
 
| Operator Name: [[FIRSTENERGY GENERATION LLC]]
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| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Latitude: 40.503764657
+
| Latitude: 40.500000
 
|-
 
|-
| Longitude: -80.69240188
+
| Longitude: -80.690000
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Well History ==
 
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<!--== Perforation Treatments ==
 
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Comments
 
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| -1160559831
 +
| 2013-9-10 0:00:
 +
| PB
 +
| No Violations
 +
| 4.50
 +
|-
 +
| -1695558268
 +
| 2013-7-24 0:00:
 +
| PW
 +
| No Violations
 +
| 3.00
 +
|-
 +
| -27093670
 +
| 2013-9-11 0:00:
 +
| PB
 +
| No Violations
 +
| 4.00
 +
|-
 +
| -619178420
 +
| 2013-9-9 0:00:0
 +
| PB
 +
| No Violations
 +
| 9.50
 
|-
 
|-
 
| 0027093670
 
| 0027093670
Line 199: Line 223:
 
| No Violations
 
| No Violations
 
| Was on location to pull 1 tubing. Pulled in total 1017 of tubing. Also pulled 2 tubing with a total of 1341 being pulled. There was a gas escape packer at 1017.
 
| Was on location to pull 1 tubing. Pulled in total 1017 of tubing. Also pulled 2 tubing with a total of 1341 being pulled. There was a gas escape packer at 1017.
 +
|-
 +
| 152074597
 +
| 2015-3-18 0:00:
 +
| FR
 +
| No Violations
 +
| 1.00
 
|-
 
|-
 
| 1656333366
 
| 1656333366
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  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Ohio Wells]]
 
[[Category:Ohio Wells]]

Latest revision as of 20:48, 12 January 2021

Well Details

Well ID: 34-081-61055
Loading map...
Country: United States
State: Ohio
County: Jefferson
Municipality: Knox Township
Operator Name: FIRSTENERGY GENERATION LLC
Well Pad ID:
Farm/Lease Name: RUSSELL W T
License Status: Final Restoration
License Date: 2013-07-03
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 40.500000
Longitude: -80.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Change of Owner 2013-06-20 Operator changed from 9998, HISTORIC OWNER to 9152, FIRSTENERGY GENERATION LLC. WELL TRANSFERRED PER OWNERSHIP AFFIDAVIT. SEE OWNER FILE FOR DOCUMENTATION. WELL TO BE PLUGGED BY TEMPORARY OWNER.
APP 2013-07-03 Proposed Formations:BEREA, Issued Date:7/3/2013, Expired Date:7/3/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-09-11
Construction Permit Expires 2015-07-03
Record Last Modified 2017-02-10

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1160559831 2013-9-10 0:00: PB No Violations 4.50
-1695558268 2013-7-24 0:00: PW No Violations 3.00
-27093670 2013-9-11 0:00: PB No Violations 4.00
-619178420 2013-9-9 0:00:0 PB No Violations 9.50
0027093670 2013-09-11 Plug / Plug Back No Violations Tagged cement top at 463. Ran 2.375upset tubing in and Cemenco cemented back to surface with 90 sacks of regular class A cement.
0152074597 2015-03-18 Final Restoration No Violations On the date of inspection I am accompanied by SE Regional Manager Brent Bear to inspect the plugged and abandoned well for Final Restoration. The well passes Final Restoration per ORC 1509.072(B).
0619178420 2013-09-09 Plug / Plug Back No Violations Saftey meeting and started pulling 1tubing out. Pulled out 1017of 1tubing, 1341of 2tubing. There was a gas escape sit-down packer at 1017.
1044656989 2013-09-10 Administrative Inspection No Violations Contractors called on the status they were running 2.375upset tubing to 1250with a mud anchor. They had Cemenco run in with 180 sacks of class A cement and then trip tubing all out. Good circulation. Will tag tomorrow.
1160559831 2013-09-10 Plug / Plug Back No Violations I was onsite to witness the cementing of the Berea Sandstone plug. The well was holeshot with nitroglycerin and we pumped 180 sacks at 15.6ppg to fill the void. The cement will set and we will tage it to then top off the plug.
1297698022 2013-07-23 Production Wells No Violations I was on location to see if any work has been done on this well that has been excavated out so that access to the well can be had. Currently lines from the well are running to a 1000L holding tank in case the wells produce any fluid. No changes to the wells have been completed at this time.
1375790763 2013-07-24 Production Wells No Violations Well is old shackle well with 6.625surface and gas escape packer. 2tubing and 1tubing with old grass hopper shacle jack. There is a 100 gal plastic tank on site. Well is idle and not capable.
1378906455 2013-09-06 Plug / Plug Back No Violations Saftey meeting and then started pulling rods out of well. Pulled 720of steel rods and 621of wooden rods.
1379086536 2013-09-09 Plug / Plug Back No Violations Was on location to pull 1 tubing. Pulled in total 1017 of tubing. Also pulled 2 tubing with a total of 1341 being pulled. There was a gas escape packer at 1017.
152074597 2015-3-18 0:00: FR No Violations 1.00
1656333366 2013-09-11 Plug / Plug Back No Violations We tagged cement to 463 and ran 2.375 upset tubing in and Cemenco cemented back to surface with 90 sacks of class A cement. They will rig down and move on to the next well to be plugged after cutting down the casing at surface.
1695558268 2013-07-24 Production Wells No Violations I was on location with ODNR inspector Pat Shreve to try and determine what is in the hole and what will need done to properly plug this well when the permit to plug and abandon is used and a plugging rigs comes on location. We determined that there is likely casing on hangers with packing in the hole, likely being 2 and 3 inside. It was also agreed upon that a full cement plug would need to be cemented in this well to properly plug the well. Information from offset wells was also collected at this time to try and determine what could possibly in the well when it comes time to plug. Each one of the 10 wells on the property could have different downhole properties and each well will need to be addressed separately.

For data sources see[3]

References