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Difference between revisions of "34-081-61788"

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__TOC__
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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-081-61788
 
| Well ID: 34-081-61788
 +
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.35, -80.61 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| Country: United States
 
|-
 
|-
| Municipality:
+
| State: Ohio
 
|-
 
|-
| Operator Name:
+
| County: <County>
 
|-
 
|-
| Well Pad ID:
+
| Municipality:  
 
|-
 
|-
| Farm/Lease Name:
+
| Operator Name: [[HISTORIC OWNER]]
 
|-
 
|-
| First Permit Date:
+
| Well Pad ID:  
 
|-
 
|-
| Last Permit Date:
+
| Farm/Lease Name: OLD JEFFERSON IRON WORKS
 
|-
 
|-
| Spud Date:
+
| License Status: Field Inspected:  Well Not Found
 
|-
 
|-
| Unconventional:
+
| License Date:  
 
|-
 
|-
| Horizontal:
+
| Spud Date: 1900-01-01
 
|-
 
|-
| Producing:
+
| Spud Drilling Contractor:  
 
|-
 
|-
| Violations:
+
| Final Drill Date:  
 
|-
 
|-
| Latitude:
+
| Well Total Depth:  
 
|-
 
|-
| Longitude:
+
| Configuration: Vertical
 
|-
 
|-
 +
| Latitude: 40.350000
 +
|-
 +
| Longitude: -80.610000
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | GAS QUANTITY
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comment
!scope="col" | CONDENSATE QUANTITY
+
|-
!scope="col" | CONDENSATE PRODUCTION DAYS
+
| Record Last Modified
!scope="col" | OIL QUANTITY
+
| 2013-05-23
!scope="col" | OIL PRODUCTION DAYS
+
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | TYPE
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | UNITS
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | DISPOSAL METHOD
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | WASTE FACILITY PERMIT ID
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | WASTE FACILITY NAME
+
!scope="col" style="text-align: center"| Comments
!scope="col" | FACILITY CITY
+
|-
!scope="col" | FACILITY STATE
+
|}-->
|}
+
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
 
| 1352303520
 
| 1352303520
 
| 2012-11-01
 
| 2012-11-01
|
+
| Field Inspected, Well Not Found
| I conducted an inspection of this possible well from a request of Dan Prebonick, an engineer for W.Z. Baumgartner & Associates, Inc. The former RG Steel property, now owned by River Rail Development, LLC, is trying to become involved in a VAP (Voluntary Action Program) with the Ohio EPA. The program stipulates that there cannot be any active oil and gas wells on site, and if there were active wells that they were properly plugged according to ODNR standards. Three possible wells showed up in records near the RG Steel property. They were API# 34081617870000, 34081617880000 and 34081617890000. It was concluded that only 34081617880000 was possibly on RG Steel property. I mapped the well and it appeared to be present inside the former picking building of the property. I was escorted to the location by Dave Kociban of Strauss Industries and tried to locate the well using GPS coordinates. There were no signs of a gas well ever inside the area of the pickling building. The only documents currently on file regarding this well is an incomplete Ohio Geological Survey card. The card only shows only the proposed location, property owner and the well operator. It is my conclusion that this well was either never drilled or was shortly thereafter plugged. Many of the similar wells in the near vicinity are shown as plugged. Also this well card does not show a well drilling date, completion or even when the well was permitted. It appears that this was a planned well that was never drilled. The listed owner of this well was Labelle Ironworks, which in 1920 merged with two other ironworks to form the Wheeling Steel and Iron Company. This would mean that the well would have to be drilled pre 1920 but it was recorded. The deed shows no mention of any oil and gas wells on the property and interviews with RG Steel representatives also show no information of the presence of gas wells on site. With this information and the lack of information I would conclude that there well #34081617880000 has both been plugged and abandoned or was never drilled on the RG Steel property.  This would mean that there are currently no operating or unplugged oil and gas wells present on the RG Steel property allowing them to enter the VAP with the Ohio EPA.
+
| No Violations
|
+
| I conducted an inspection of this possible well from a request of Dan Prebonick, an engineer for W.Z. Baumgartner & Associates, Inc. The former RG Steel property, now owned by River Rail Development, LLC, is trying to become involved in a VAP (Voluntary Action Program) with the Ohio EPA. The program stipulates that there cannot be any active oil and gas wells on site, and if there were active wells that they were properly plugged according to ODNR standards. Three possible wells showed up in records near the RG Steel property. They were API# 34081617870000, 34081617880000 and 34081617890000. It was concluded that only 34081617880000 was possibly on RG Steel property. I mapped the well and it appeared to be present inside the former picking building of the property. I was escorted to the location by Dave Kociban of Strauss Industries and tried to locate the well using GPS coordinates. There were no signs of a gas well ever inside the area of the pickling building. The only documents currently on file regarding this well is an incomplete Ohio Geological Survey card. The card only shows only the proposed location, property owner and the well operator. It is my conclusion that this well was either never drilled or was shortly thereafter plugged. Many of the similar wells in the near vicinity are shown as plugged. Also this well card does not show a well drilling date, completion or even when the well was permitted. It appears that this was a planned well that was never drilled. The listed owner of this well was Labelle Ironworks, which in 1920 merged with two other ironworks to form the Wheeling Steel and Iron Company. This would mean that the well would have to be drilled pre 1920 but it was recorded. The deed shows no mention of any oil and gas wells on the property and interviews with RG Steel representatives also show no information of the presence of gas wells on site. With this information and the lack of information I would conclude that there well #3408161788000
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 21:19, 12 January 2021

Well Details

Well ID: 34-081-61788
Loading map...
Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name: OLD JEFFERSON IRON WORKS
License Status: Field Inspected: Well Not Found
License Date:
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 40.350000
Longitude: -80.610000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Record Last Modified 2013-05-23

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1352303520 2012-11-01 Field Inspected, Well Not Found No Violations I conducted an inspection of this possible well from a request of Dan Prebonick, an engineer for W.Z. Baumgartner & Associates, Inc. The former RG Steel property, now owned by River Rail Development, LLC, is trying to become involved in a VAP (Voluntary Action Program) with the Ohio EPA. The program stipulates that there cannot be any active oil and gas wells on site, and if there were active wells that they were properly plugged according to ODNR standards. Three possible wells showed up in records near the RG Steel property. They were API# 34081617870000, 34081617880000 and 34081617890000. It was concluded that only 34081617880000 was possibly on RG Steel property. I mapped the well and it appeared to be present inside the former picking building of the property. I was escorted to the location by Dave Kociban of Strauss Industries and tried to locate the well using GPS coordinates. There were no signs of a gas well ever inside the area of the pickling building. The only documents currently on file regarding this well is an incomplete Ohio Geological Survey card. The card only shows only the proposed location, property owner and the well operator. It is my conclusion that this well was either never drilled or was shortly thereafter plugged. Many of the similar wells in the near vicinity are shown as plugged. Also this well card does not show a well drilling date, completion or even when the well was permitted. It appears that this was a planned well that was never drilled. The listed owner of this well was Labelle Ironworks, which in 1920 merged with two other ironworks to form the Wheeling Steel and Iron Company. This would mean that the well would have to be drilled pre 1920 but it was recorded. The deed shows no mention of any oil and gas wells on the property and interviews with RG Steel representatives also show no information of the presence of gas wells on site. With this information and the lack of information I would conclude that there well #3408161788000

For data sources see[3]

References