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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-119-22194 | | Well ID: 34-119-22194 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 40.08, -81.77 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | | + | | County: [[Muskingum_County,_Ohio|Muskingum]] |
|- | |- | ||
− | | | + | | Municipality: [[Highland_Township,_Muskingum_County,_Ohio|Highland Township]] |
|- | |- | ||
− | | | + | | Operator Name: [[SMITH RONALD DBA CHIPCO]] |
|- | |- | ||
− | | | + | | Well Pad ID: |
|- | |- | ||
− | | | + | | Farm/Lease Name: MCCORMICK LESTER |
+ | |- | ||
+ | | License Status: Producing | ||
+ | |- | ||
+ | | License Date: 1983-06-01 | ||
|- | |- | ||
| Spud Date: 1969-10-31 | | Spud Date: 1969-10-31 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: |
+ | |- | ||
+ | | Final Drill Date: 1969-11-09 | ||
+ | |- | ||
+ | | Well Total Depth: 4533.00 ft | ||
+ | |- | ||
+ | | Configuration: Vertical | ||
+ | |- | ||
+ | | Latitude: 40.080000 | ||
+ | |- | ||
+ | | Longitude: -81.770000 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | CO | ||
+ | | 1969-10-21 | ||
+ | | 1525 GARBAS GARY A GeoDate 10/21/69 | ||
+ | |- | ||
+ | | Original Spud | ||
+ | | 1969-10-31 | ||
+ | | GL=957.3 KB=966.8 | ||
+ | |- | ||
+ | | Completed | ||
+ | | 1969-11-09 | ||
+ | | GL=957.3 KB=966.8 | ||
+ | |- | ||
+ | | Reached Total Depth | ||
+ | | 1969-11-09 | ||
+ | | GL=957.3 KB=966.8 | ||
+ | |- | ||
+ | | CO | ||
+ | | 1983-06-01 | ||
+ | | 1525 GARBAS GARY A GeoDate 6/1/83 | ||
+ | |- | ||
+ | | Unknown | ||
+ | | 1983-06-01 | ||
+ | | Issued Date 6/1/83 Expired Date 11/28/83 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 1983-11-28 | ||
+ | | GL=957.3 KB=966.8 | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2013-05-09 | ||
+ | | Operator changed from 1525, GARBAS GARY A to 236, POLING R C CO INC | ||
|- | |- | ||
− | | | + | | Change of Owner |
+ | | 2016-01-22 | ||
+ | | Operator changed from 236, R C POLING CO INC to 7640, SMITH RONALD DBA CHIPCO | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2016-01-22 | ||
+ | | GL=957.3 KB=966.8 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
|- | |- | ||
− | | | + | |}--> |
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
|- | |- | ||
− | | | + | |}--> |
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
|- | |- | ||
− | | | + | |}--> |
+ | == Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
|- | |- | ||
− | | | + | | |
+ | | H2O | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 97800 Gal | ||
+ | | style="text-align: right;" | 48900 | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblStimulation Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Period |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Operator Name |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Gas Quantity (mcf) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Oil Quantity (bbl) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Production Days |
− | + | |- | |
− | + | | 1993 | |
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 248.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 1994 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 2.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | 1995 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 1996 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 87.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 93 | ||
+ | |- | ||
+ | | 1997 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 61.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 150 | ||
+ | |- | ||
+ | | 1998 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 12.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | 1999 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2000 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 529.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 334 | ||
+ | |- | ||
+ | | 2001 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 366.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 344 | ||
+ | |- | ||
+ | | 2002 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 227.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2003 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 60.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 261 | ||
+ | |- | ||
+ | | 2004 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 58.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 183 | ||
+ | |- | ||
+ | | 2005 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 3.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 180 | ||
+ | |- | ||
+ | | 2006 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 494.00 | ||
+ | | style="text-align: right;" | 22.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2007 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 609.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2008 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 535.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2009 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 296.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 212.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 115.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | style="text-align: right;" | 56.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 366 | ||
+ | |- | ||
+ | | 2013 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | style="text-align: right;" | 283.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | style="text-align: right;" | 920.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | style="text-align: right;" | 795.00 | ||
+ | | style="text-align: right;" | 37.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | style="text-align: right;" | 1291.00 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[SMITH RONALD DBA CHIPCO]] | ||
+ | | style="text-align: right;" | 893.00 | ||
+ | | style="text-align: right;" | 69.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[SMITH RONALD DBA CHIPCO]] | ||
+ | | style="text-align: right;" | 1507.00 | ||
+ | | style="text-align: right;" | 68.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Waste Data == | == Waste Data == | ||
− | {| class="wikitable sortable" | + | {| class="wikitable sortable" |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Period |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Operator Name |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Waste Type |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Quantity (bbl) |
− | + | !scope="col" style="text-align: center"| Production Days | |
− | + | |- | |
− | + | | 1993 | |
− | + | | [[DANNY LONG & SONS INC]] | |
− | + | | Brine | |
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 1994 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | 1995 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 1996 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 93 | ||
+ | |- | ||
+ | | 1997 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 150 | ||
+ | |- | ||
+ | | 1998 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | 1999 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2000 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 334 | ||
+ | |- | ||
+ | | 2001 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 210 | ||
+ | | style="text-align: right;" | 344 | ||
+ | |- | ||
+ | | 2002 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2003 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 261 | ||
+ | |- | ||
+ | | 2004 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 183 | ||
+ | |- | ||
+ | | 2005 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 180 | ||
+ | |- | ||
+ | | 2006 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2007 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2008 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2009 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[DANNY LONG & SONS INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 366 | ||
+ | |- | ||
+ | | 2013 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[R C POLING CO INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[SMITH RONALD DBA CHIPCO]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[SMITH RONALD DBA CHIPCO]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | ||
− | |||
|- | |- | ||
| -115824230 | | -115824230 | ||
− | | 2008-12- | + | | 2008-12-4 0:00: |
− | | | + | | PW |
− | | | + | | No Violations |
− | | | + | | |
− | |||
− | |||
− | |||
|- | |- | ||
| -1353612231 | | -1353612231 | ||
− | | 2011- | + | | 2011-5-16 0:00: |
− | | | + | | PW |
− | | | + | | No Violations |
− | + | | 1.00 | |
− | |||
− | | | ||
|- | |- | ||
+ | | -1446199557 | ||
+ | | 2011-7-13 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | | ||
|- | |- | ||
− | | - | + | | -261611939 |
− | | 2011- | + | | 2011-7-18 0:00: |
− | + | | PW | |
− | + | | No Violations | |
− | | | + | | |
− | | | ||
− | | | ||
|- | |- | ||
+ | | 0115824230 | ||
+ | | 2008-12-04 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | Has been producig but gas company has shut them in for a bad check valve which allows gas to backfeed into the well. Should be back online soon. No other problems noted. | ||
|- | |- | ||
− | | | + | | 0261611939 |
| 2011-07-18 | | 2011-07-18 | ||
− | | | + | | Production Wells |
− | | Called Long Oil and spoke with Danny | + | | No Violations |
− | + | | Called Long Oil and spoke with Danny Longs wife. I told her that tank pad is to close to the well. The tank and dike have to be a minimum of 50 from the well. She will tell Dan. | |
− | |||
− | |||
|- | |- | ||
+ | | 0585773892 | ||
+ | | 2003-05-20 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | | ||
|- | |- | ||
− | | | + | | 0743377752 |
− | | 2011-04- | + | | 2011-04-25 |
− | | | + | | Production Wells |
− | | | + | | No Violations |
− | + | | Stopped by well site to see if any action has been done since Todd called. They did spread pete out. I spoke with land owners wife. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1303744019 | | 1303744019 | ||
| 2011-04-21 | | 2011-04-21 | ||
− | | | + | | Production Wells |
− | | This complaint was called in by a Scott Williamson. Todd Miller and I went to site and found tank to be leaking oil. There was an affected area approximately 12 | + | | Violations Noted |
− | + | | This complaint was called in by a Scott Williamson. Todd Miller and I went to site and found tank to be leaking oil. There was an affected area approximately 12 wide at the tank and 2 wide and 35 long leading away from the tank. There was a bag of pete moss on site but had not been applied to the affected area. Inspector Miller will call the owner/operator. After oil clean-up, the tank needs to be removed and the impacted soil needs to be hauled away and disposed of properly. New topsoil will need to be brought in and a new tank will need to be installed. A dike (12Wx15Lx36H) will need to be built. The affected area will need to be reseeded. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1315040758 | | 1315040758 | ||
| 2011-08-29 | | 2011-08-29 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| On day of inspection Long Oil and Gas set a new 30 barrel brine tank and removed the old tank. Dike completed, proper idetentification in place and area reseeded. NOC resolved. | | On day of inspection Long Oil and Gas set a new 30 barrel brine tank and removed the old tank. Dike completed, proper idetentification in place and area reseeded. NOC resolved. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 1353612231 | ||
+ | | 2011-05-16 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | Accompanied P. Shreve complaint status check follow up. | ||
|- | |- | ||
| 1409163362 | | 1409163362 | ||
| 2011-06-07 | | 2011-06-07 | ||
− | | | + | | Production Wells |
− | | Stonerock and I checked well site. We called Long Oil and spoke to | + | | No Violations |
− | + | | Stonerock and I checked well site. We called Long Oil and spoke to Dannys wife. I told her the production tank must be a minimum of 50 from the well. | |
− | |||
− | |||
|- | |- | ||
+ | | 1446199557 | ||
+ | | 2011-07-13 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | Inspector Stonerock and I inspected well site. The tank has been moved. The dike and gravel bed are in place. The tank battery area is not 50 away from well head. The well is shut in but is a domestic well. Will call about the tank location. | ||
|- | |- | ||
| 1803123878 | | 1803123878 | ||
| 2005-04-07 | | 2005-04-07 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| Okay | | Okay | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 585773892 | ||
+ | | 2003-5-20 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | | ||
|- | |- | ||
− | | | + | | 743377752 |
− | | | + | | 2011-4-25 0:00: |
− | | | + | | PW |
− | | | + | | No Violations |
− | | | + | | 0.50 |
− | | | + | |- |
− | | | + | |} |
+ | ==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
|- | |- | ||
+ | | 1303744019 | ||
+ | | US-OH-108566 | ||
+ | | 2011-04-25 | ||
+ | | | ||
+ | | Well operation causing pollution and contamination | ||
|- | |- | ||
− | | | + | | 1303744019 |
+ | | US-OH-108567 | ||
| 2011-04-25 | | 2011-04-25 | ||
− | | | + | | |
− | | | + | | No SPCC dike/or failure to keep dike free of water or oil |
− | |||
− | |||
− | |||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | ==References== | ||
+ | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-119-22194 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Highland Township | |
Operator Name: SMITH RONALD DBA CHIPCO | |
Well Pad ID: | |
Farm/Lease Name: MCCORMICK LESTER | |
License Status: Producing | |
License Date: 1983-06-01 | |
Spud Date: 1969-10-31 | |
Spud Drilling Contractor: | |
Final Drill Date: 1969-11-09 | |
Well Total Depth: 4533.00 ft | |
Configuration: Vertical | |
Latitude: 40.080000 | |
Longitude: -81.770000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1969-10-21 | 1525 GARBAS GARY A GeoDate 10/21/69 |
Original Spud | 1969-10-31 | GL=957.3 KB=966.8 |
Completed | 1969-11-09 | GL=957.3 KB=966.8 |
Reached Total Depth | 1969-11-09 | GL=957.3 KB=966.8 |
CO | 1983-06-01 | 1525 GARBAS GARY A GeoDate 6/1/83 |
Unknown | 1983-06-01 | Issued Date 6/1/83 Expired Date 11/28/83 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1983-11-28 | GL=957.3 KB=966.8 |
Change of Owner | 2013-05-09 | Operator changed from 1525, GARBAS GARY A to 236, POLING R C CO INC |
Change of Owner | 2016-01-22 | Operator changed from 236, R C POLING CO INC to 7640, SMITH RONALD DBA CHIPCO |
Record Last Modified | 2016-01-22 | GL=957.3 KB=966.8 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 97800 Gal | 48900 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | DANNY LONG & SONS INC | 248.00 | 0.00 | 365 |
1994 | DANNY LONG & SONS INC | 2.00 | 0.00 | 30 |
1995 | DANNY LONG & SONS INC | 0.00 | 0.00 | 0 |
1996 | DANNY LONG & SONS INC | 87.00 | 0.00 | 93 |
1997 | DANNY LONG & SONS INC | 61.00 | 0.00 | 150 |
1998 | DANNY LONG & SONS INC | 12.00 | 0.00 | 30 |
1999 | DANNY LONG & SONS INC | 0.00 | 0.00 | 0 |
2000 | DANNY LONG & SONS INC | 529.00 | 0.00 | 334 |
2001 | DANNY LONG & SONS INC | 366.00 | 0.00 | 344 |
2002 | DANNY LONG & SONS INC | 227.00 | 0.00 | 365 |
2003 | DANNY LONG & SONS INC | 60.00 | 0.00 | 261 |
2004 | DANNY LONG & SONS INC | 58.00 | 0.00 | 183 |
2005 | DANNY LONG & SONS INC | 3.00 | 0.00 | 180 |
2006 | DANNY LONG & SONS INC | 494.00 | 22.00 | 365 |
2007 | DANNY LONG & SONS INC | 609.00 | 0.00 | 365 |
2008 | DANNY LONG & SONS INC | 535.00 | 0.00 | 365 |
2009 | DANNY LONG & SONS INC | 296.00 | 0.00 | 365 |
2010 | DANNY LONG & SONS INC | 212.00 | 0.00 | 365 |
2011 | DANNY LONG & SONS INC | 115.00 | 0.00 | 365 |
2012 | DANNY LONG & SONS INC | 56.00 | 0.00 | 366 |
2013 | R C POLING CO INC | 283.00 | 0.00 | 365 |
2014 | R C POLING CO INC | 920.00 | 0.00 | 365 |
2015 | R C POLING CO INC | 795.00 | 37.00 | 365 |
2016 | R C POLING CO INC | 1291.00 | 0.00 | 0 |
2017 | SMITH RONALD DBA CHIPCO | 893.00 | 69.00 | 365 |
2018 | SMITH RONALD DBA CHIPCO | 1507.00 | 68.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-115824230 | 2008-12-4 0:00: | PW | No Violations | |
-1353612231 | 2011-5-16 0:00: | PW | No Violations | 1.00 |
-1446199557 | 2011-7-13 0:00: | PW | No Violations | |
-261611939 | 2011-7-18 0:00: | PW | No Violations | |
0115824230 | 2008-12-04 | Production Wells | No Violations | Has been producig but gas company has shut them in for a bad check valve which allows gas to backfeed into the well. Should be back online soon. No other problems noted. |
0261611939 | 2011-07-18 | Production Wells | No Violations | Called Long Oil and spoke with Danny Longs wife. I told her that tank pad is to close to the well. The tank and dike have to be a minimum of 50 from the well. She will tell Dan. |
0585773892 | 2003-05-20 | Production Wells | No Violations | |
0743377752 | 2011-04-25 | Production Wells | No Violations | Stopped by well site to see if any action has been done since Todd called. They did spread pete out. I spoke with land owners wife. |
1303744019 | 2011-04-21 | Production Wells | Violations Noted | This complaint was called in by a Scott Williamson. Todd Miller and I went to site and found tank to be leaking oil. There was an affected area approximately 12 wide at the tank and 2 wide and 35 long leading away from the tank. There was a bag of pete moss on site but had not been applied to the affected area. Inspector Miller will call the owner/operator. After oil clean-up, the tank needs to be removed and the impacted soil needs to be hauled away and disposed of properly. New topsoil will need to be brought in and a new tank will need to be installed. A dike (12Wx15Lx36H) will need to be built. The affected area will need to be reseeded. |
1315040758 | 2011-08-29 | Production Wells | No Violations | On day of inspection Long Oil and Gas set a new 30 barrel brine tank and removed the old tank. Dike completed, proper idetentification in place and area reseeded. NOC resolved. |
1353612231 | 2011-05-16 | Production Wells | No Violations | Accompanied P. Shreve complaint status check follow up. |
1409163362 | 2011-06-07 | Production Wells | No Violations | Stonerock and I checked well site. We called Long Oil and spoke to Dannys wife. I told her the production tank must be a minimum of 50 from the well. |
1446199557 | 2011-07-13 | Production Wells | No Violations | Inspector Stonerock and I inspected well site. The tank has been moved. The dike and gravel bed are in place. The tank battery area is not 50 away from well head. The well is shut in but is a domestic well. Will call about the tank location. |
1803123878 | 2005-04-07 | Production Wells | No Violations | Okay |
585773892 | 2003-5-20 0:00: | PW | No Violations | |
743377752 | 2011-4-25 0:00: | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1303744019 | US-OH-108566 | 2011-04-25 | Well operation causing pollution and contamination | |
1303744019 | US-OH-108567 | 2011-04-25 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[8]