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Difference between revisions of "34-019-22308"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-019-22308
 
| Well ID: 34-019-22308
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.452028799, -81.11154568 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.45, -81.11 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 13: Line 13:
 
| Municipality: [[Perry_Township,_Carroll_County,_Ohio|Perry Township]]
 
| Municipality: [[Perry_Township,_Carroll_County,_Ohio|Perry Township]]
 
|-
 
|-
| Operator Name: [[CHESAPEAKE EXPLORATION LLC]]
+
| Operator Name: [[EAP OHIO LLC]]
 
|-
 
|-
 
| Well Pad ID: [[US-OH-000637]]
 
| Well Pad ID: [[US-OH-000637]]
Line 33: Line 33:
 
| Configuration: Horizontal
 
| Configuration: Horizontal
 
|-
 
|-
| Latitude: 40.452028799
+
| Latitude: 40.450000
 
|-
 
|-
| Longitude: -81.11154568
+
| Longitude: -81.110000
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Well History ==
 
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 93: Line 93:
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<!--== Perforation Treatments ==
 
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 137: Line 137:
 
| rowspan="37"| 1
 
| rowspan="37"| 1
 
|- valign="top"
 
|- valign="top"
| rowspan="8"| APB01 (AMMONIUM PERSUFATE BREAKER)
+
| rowspan="8"| APB01 (AMMONIUM PERSUFATE BREAKER),
BXL02E (BORATE XL- INSTANT XL)
+
BXL02E (BORATE XL- INSTANT
CI-150, CS-250 SI, FE 200
+
XL), CI-150, CS-250 SI, FE 200,
FRW-200, ICI-3240 (1 GAL), LTB-01
+
FRW-200, ICI-3240 (1 GAL), LTB-01
 
| rowspan="8"| FTS INTERNATIONAL
 
| rowspan="8"| FTS INTERNATIONAL
 
| rowspan="8"| Anti-Bacterial Agent, Breaker, Corrosion Inhibitor, Cross Linker, Friction Reducer, Iron Control Agent, Scale Inhibitor
 
| rowspan="8"| Anti-Bacterial Agent, Breaker, Corrosion Inhibitor, Cross Linker, Friction Reducer, Iron Control Agent, Scale Inhibitor
| Proprietary Friction Reducer Additive (FRW-200 and FRW-200W)
+
| Proprietary Friction Reducer Additive
 +
(FRW-200 and FRW-200W)
 
| TRADE SECRET
 
| TRADE SECRET
 
| style="text-align: right;" | 0
 
| style="text-align: right;" | 0
Line 464: Line 465:
 
  | title = Risk Based Data Management System - tblStimulation Table
 
  | title = Risk Based Data Management System - tblStimulation Table
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 509: Line 510:
 
  | title = Risk Based Data Management System - Production Table - Oil and Gas Data
 
  | title = Risk Based Data Management System - Production Table - Oil and Gas Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<ref>{{cite web
 
<ref>{{cite web
 
  | title = Combined Production - Oil and Gas Data
 
  | title = Combined Production - Oil and Gas Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
 
{| class="wikitable sortable"
 
{| class="wikitable sortable"
Line 560: Line 561:
 
  | title = Risk Based Data Management System - Production Table - Brine Data
 
  | title = Risk Based Data Management System - Production Table - Brine Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<ref>{{cite web
 
<ref>{{cite web
 
  | title = Combined Production - Brine Data
 
  | title = Combined Production - Brine Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 
==== Inspections Performed ====
 
==== Inspections Performed ====
Line 577: Line 578:
 
!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Comments
 
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| -1889442261
 +
| 2017-3-2 0:00:0
 +
| PL
 +
| No Violations
 +
|
 +
|-
 +
| -2077328686
 +
| 2018-11-19 0:00
 +
| PW
 +
| No Violations
 +
| 1.00
 
|-
 
|-
 
| 0332798325
 
| 0332798325
Line 583: Line 596:
 
| No Violations
 
| No Violations
 
| I was on site to witness the cementing of the 20 inch conductor casing. My inspection revealed that Enviro Drill has drilled a 30 inch hole to a total depth of 120 feet and ran 120 of 20 inch conductor casing (78.67 pounds per foot / inside diameter of 19.25 inches). Allied pumped 433 sacks of Class A cement with 2% CaCl and 1/2 pound per sack floseal. The cement had a density of 15.6 pounds per gallon, a yield of 1.18 cubic feet per sack, and they used 5.23 gallons of mix water per sack. Allied pumped 91 barrels of cement slurry, 39.5 barrels of displacement, and there was 10 barrels of cement returns to surface. My inspection revealed no violations at this time. NOTE: Started pumping water on the 6H well and found the 2 inch ball valve on the conductor cap was split. Enviro Drill replaced the ball valve and Allied started pumping on the casing again. Had to shut down again because the weld on the conductor cap was leaking. They also found that the 5H and 10H conductor holes were communicating so they decided to pump this cement job first and then go back to the 5H and 10H conductor cement jobs. Region Supervisor Tom Hill was present for the cementing of the casing.
 
| I was on site to witness the cementing of the 20 inch conductor casing. My inspection revealed that Enviro Drill has drilled a 30 inch hole to a total depth of 120 feet and ran 120 of 20 inch conductor casing (78.67 pounds per foot / inside diameter of 19.25 inches). Allied pumped 433 sacks of Class A cement with 2% CaCl and 1/2 pound per sack floseal. The cement had a density of 15.6 pounds per gallon, a yield of 1.18 cubic feet per sack, and they used 5.23 gallons of mix water per sack. Allied pumped 91 barrels of cement slurry, 39.5 barrels of displacement, and there was 10 barrels of cement returns to surface. My inspection revealed no violations at this time. NOTE: Started pumping water on the 6H well and found the 2 inch ball valve on the conductor cap was split. Enviro Drill replaced the ball valve and Allied started pumping on the casing again. Had to shut down again because the weld on the conductor cap was leaking. They also found that the 5H and 10H conductor holes were communicating so they decided to pump this cement job first and then go back to the 5H and 10H conductor cement jobs. Region Supervisor Tom Hill was present for the cementing of the casing.
 +
|-
 +
| 1010857237
 +
| 2019-12-9 0:00:
 +
| PW
 +
| No Violations
 +
| 0.80
 
|-
 
|-
 
| 1393923913
 
| 1393923913
Line 617: Line 636:
 
| No Violations
 
| No Violations
 
| The well was equipped with a plunger-lift assembly. The surface/intermediate and intermediate/production annular gauges displayed readings of zero psi.  I performed a walk-around inspection of the pad and erosional controls appeared functioning.  No violations were observed at the time of inspection.
 
| The well was equipped with a plunger-lift assembly. The surface/intermediate and intermediate/production annular gauges displayed readings of zero psi.  I performed a walk-around inspection of the pad and erosional controls appeared functioning.  No violations were observed at the time of inspection.
 +
|-
 +
| 332798325
 +
| 2014-2-3 0:00:0
 +
| DD
 +
| No Violations
 +
| 5.00
 
|-
 
|-
 
|}
 
|}
Line 631: Line 656:
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
==References==
 
==References==
 
<references/>
 
<references/>

Latest revision as of 22:59, 12 January 2021

Well Details

Well ID: 34-019-22308
Loading map...
Country: United States
State: Ohio
County: Carroll
Municipality: Perry Township
Operator Name: EAP OHIO LLC
Well Pad ID: US-OH-000637
Farm/Lease Name: RAY HAYLEY 5-13-6
License Status: Producing
License Date: 2014-01-16
Spud Date: 2014-02-01
Spud Drilling Contractor: NOMAC DRILLING CORP
Final Drill Date: 2014-03-10
Well Total Depth:
Configuration: Horizontal
Latitude: 40.450000
Longitude: -81.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-01-31 Proposed Formations:TRENTON-BLACK RIVER, Issued Date:1/31/2013, Expired Date:1/31/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
Correction to Well 2013-02-15 CORRECTION TO GROUND LEVEL ELEVATION.
APP 2014-01-16 Proposed Formations:POINT PLEASANT, Issued Date:1/16/2014, Expired Date:1/16/2016 12:00:00 PM, Drilling unit acres:273.88, Proposed Well Type:OG, Proposed Well Class:EOUT
Correction to Well 2014-01-24 CHANGED SURFACE FOOTAGE AND ADDED TARGET FOOTAGE.
Reached Total Depth 2014-03-10
Correction to Well 2015-01-16 CHANGES IN SURFACE, TARGET AND TAKE-POINT INFORMATION (FOOTAGES AND COORDINATES) FROM AS DRILLED SURVEY PLAT.
Correction to Well 2015-01-23 UPDATE TO TAKE-POINT INFORMATION (COORDINATES) FROM NEWLY SUBMITTED PLAT.
Completion Report Received 2015-03-30
Construction Permit Expires 2016-01-16
Record Last Modified 2017-10-24

For data sources see[2]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 11/12/2014 11/23/2014 7889 7,788,190.0 644610

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1
APB01 (AMMONIUM PERSUFATE BREAKER),

BXL02E (BORATE XL- INSTANT XL), CI-150, CS-250 SI, FE 200, FRW-200, ICI-3240 (1 GAL), LTB-01

FTS INTERNATIONAL Anti-Bacterial Agent, Breaker, Corrosion Inhibitor, Cross Linker, Friction Reducer, Iron Control Agent, Scale Inhibitor Proprietary Friction Reducer Additive

(FRW-200 and FRW-200W)

TRADE SECRET 0 0.04048 0
Proprietary Breaker (APB01) Additive TRADE SECRET 0 0 0
Proprietary Corrosion Inhibitor Additive (CI-150) TRADE SECRET 0 0.00058 0
Water 007732-18-5 0 0.07651 0
Proprietary Breaker Additive (LTB-1) TRADE SECRET 0 0.0128 0
Proprietary Iron Control Additive (FE-200L) TRADE SECRET 0 0.00275 0
Proprietary Anti-Bacterial Additive (ICI-3240) TRADE SECRET 0 0.01228 0
Non-MSDS Components Not Provided by Supplier NOT PROVIDED 0 0 0
BXL02E (BORATE XL- INSTANT XL) FTS INTERNATIONAL Cross Linker Sodium Metaborate Tetrahydrate 010555-76-7 30 0.0193 0
FE 200 FTS INTERNATIONAL Iron Control Agent Tetrasodium Ethylenediaminetetraacetate 000064-02-8 41 0.00154 0
Trisodium Nitrilotriacetate 005064-31-3 2 0.00008000 0
Sodium Hydroxide 001310-73-2 2 0.00007000 0
100 Mesh Sand FTS INTERNATIONAL Proppant - Natural Crystalline Silica (Quartz Sand, Silicon Dioxide) 014808-60-7 100 0.43204 0
HVG01 (TURQUOISE-1 BULK) FTS INTERNATIONAL Gelling Agent Petroleum Distillate Hydrotreated Light 064742-47-8 55 0.08438 0
Crystalline Silica (Quartz Sand, Silicon Dioxide) 014808-60-7 2 0.00307 0
Guar Gum 009000-30-0 50 0.07671 0
Surfactant 068439-51-0 2 0.00307 0
CS-250 SI FTS INTERNATIONAL Scale Inhibitor Ethylene Glycol 000107-21-1 10 0.00129 0
LTB-01 FTS INTERNATIONAL Breaker Crystalline Silica (Quartz Sand, Silicon Dioxide) 014808-60-7 25 0.01076 0
Proprietary Cured Acrylic Resin TRADE SECRET 25 0.01076 0
Ammonium Persulfate 007727-54-0 100 0.04305 0
CI-150 FTS INTERNATIONAL Corrosion Inhibitor Proprietary Quaternary Ammonium Compound TRADE SECRET 10 0.00011 0
Dimethyl Formamide 000068-12-2 10 0.00011 0
Proprietary Aromatic Aldehyde TRADE SECRET 10 0.00011 0
Proprietary Organic Amine Resin Salt TRADE SECRET 30 0.00032 0
Isopropanol (Isopropyl Alcohol, Propan-2-ol) 000067-63-0 60 0.00065 0
Fresh Water CHESAPEAKE ENERGY Carrier/Base Fluid Water 007732-18-5 100 82.7123 0
10.1 - 15 HCL FTS INTERNATIONAL Acid Water 007732-18-5 85 0.04899 0
Hydrochloric Acid 007647-01-0 15 0.00864 0
7.5pct HCl FTS INTERNATIONAL Acid Water 007732-18-5 93 0.50359 0
Hydrochloric Acid 007647-01-0 8 0.04083 0
FRW-200 FTS INTERNATIONAL Friction Reducer Petroleum Distillate Hydrotreated Light 064742-47-8 26 0.01074 0
ICI-3240 (1 GAL) FTS INTERNATIONAL Anti-Bacterial Agent Sodium Hydroxide 001310-73-2 4 0.00054 0
Dazomet 000533-74-4 24 0.00326 0
Northern White Sand FTS INTERNATIONAL Proppant - Natural Crystalline Silica (Quartz Sand, Silicon Dioxide) 014808-60-7 100 15.4743 0
APB01 (AMMONIUM PERSUFATE BREAKER) FTS INTERNATIONAL Breaker Ammonium Persulfate 007727-54-0 100 0.00007000 0
Recycled Produced Water CHESAPEAKE ENERGY Carrier/Base Fluid Water 007732-18-5 100 0.44574 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2014-11-23 H2O 15 2476 Bbl 401600 Frac Tech Services STAGE 31/31

25 SHOTS

2014-11-12 H2O 15 3692 Bbl 406000 Frac Tech Services STAGE 1/31

25 SHOTS STAGE 2-30 SEE IMAGES

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2015 CHESAPEAKE EXPLORATION LLC 520378 63581 325
2016 CHESAPEAKE EXPLORATION LLC 259303 22839 366
2017 CHESAPEAKE EXPLORATION LLC 182617 12811 345
2018 CHESAPEAKE EXPLORATION LLC 93042 6686 326
2019 CHESAPEAKE EXPLORATION LLC 22142 1519 90

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2015 CHESAPEAKE EXPLORATION LLC Brine 26500 325
2016 CHESAPEAKE EXPLORATION LLC Brine 5790 366
2017 CHESAPEAKE EXPLORATION LLC Brine 4450 345
2018 CHESAPEAKE EXPLORATION LLC Brine 9141 326
2019 CHESAPEAKE EXPLORATION LLC Brine 1677 90

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1889442261 2017-3-2 0:00:0 PL No Violations
-2077328686 2018-11-19 0:00 PW No Violations 1.00
0332798325 2014-02-03 Drill / Deepen / Reopen No Violations I was on site to witness the cementing of the 20 inch conductor casing. My inspection revealed that Enviro Drill has drilled a 30 inch hole to a total depth of 120 feet and ran 120 of 20 inch conductor casing (78.67 pounds per foot / inside diameter of 19.25 inches). Allied pumped 433 sacks of Class A cement with 2% CaCl and 1/2 pound per sack floseal. The cement had a density of 15.6 pounds per gallon, a yield of 1.18 cubic feet per sack, and they used 5.23 gallons of mix water per sack. Allied pumped 91 barrels of cement slurry, 39.5 barrels of displacement, and there was 10 barrels of cement returns to surface. My inspection revealed no violations at this time. NOTE: Started pumping water on the 6H well and found the 2 inch ball valve on the conductor cap was split. Enviro Drill replaced the ball valve and Allied started pumping on the casing again. Had to shut down again because the weld on the conductor cap was leaking. They also found that the 5H and 10H conductor holes were communicating so they decided to pump this cement job first and then go back to the 5H and 10H conductor cement jobs. Region Supervisor Tom Hill was present for the cementing of the casing.
1010857237 2019-12-9 0:00: PW No Violations 0.80
1393923913 2014-03-04 Drill / Deepen / Reopen No Violations Inspector James Bucksar and I were on site to witness the cementing of the 13 3/8 inch surface casing. Our inspection revealed that Nomac Drilling Rig # 71 has drilled a 17 1/2 inch hole to a total depth of 575 feet and ran 565 feet of 13 3/8 inch surface casing (54.5 pounds per foot / inside diameter is 12.615 inches). They installed 7 bowspring centralizers on the casing string on joints (2 on 1st, 2,3,6,9, and 12). Schlumberger cemented the casing with 514 sacks of Class A D901 with 1% D154, 0.5 B348, 0.15% B160A,, 0.2% D046, .125 pound per sack D130. The cement had a density of 15.6 pounds per gallon, a yield of 1.2 cubic feet per sack, and they used 5.219 gallons of mix water per sack. Schlumberger pumped 110 barrels of cement slurry, 80.5 barrels of displacement, and there was 21 barrels of cement returns to surface. They landed the plug with 275 PSI and bumped the pressure up to 728 PSI for the casing test. The casing test was approved, they released the pressure, the floats held, and there was 1/2 barrel of water flowed back when the pressure was released. Our inspection revealed no violations at this time.
1394076265 2014-03-05 Drill / Deepen / Reopen No Violations I was on site to witness the cementing of the 9 5/8 inch intermediate casing. My inspection revealed that Nomac Drilling Rig #71 has drilled a 12 1/4 inch hole to a total depth of 1896 feet and ran 1888 feet of 9 5/8 inch intermediate casing (40 pounds per foot / inside diameter 8.830 inches). They installed 17 bowspring centralizers on the casing string; 2 on 1st joint,2,3,6,9,12,15,18,21,24,27,30,33,36,39,and 42. O-TEX cemented the casing with 690 sacks of Class H with 3% Gypsum, 2% CaCl, 0.8% MC500,0.5% C45, and 0.4% C-41P. The cement had a density of 15.8 pounds per gallon, a yield of 1.21 cubic feet per sack, and they used 5.14 gallons of mix water per sack. O-TEX pumped 149 barrels of cement slurry, 133 barrels of displacement, and there was 28 barrels of cement returns to surface. They bumped the plug with 1110 PSI and then took the pressure up to 1606 PSI and conducted the casing test. The casing test was approved, pressure was released, floats held, and there was 3/4 barrel of water flowed back. My inspection revealed no violations at this time.
1889442261 2017-03-02 Preliminary Restoration No Violations I was on location to conduct a preliminary restoration inspection. The #6H well is in production and is equipped with plunger lift assembly. Jersey barriers were installed around the wellhead. The well is identified with a legibly-marked well identification sign. Identification was posted at the tank battery which consisted of eight 400 bbl production tanks, four labeled as containing produced water, and four labelled as containing condensate, and one low-pressure vertical separator. The tank battery is surrounded by a dike. There are e-stops outside the barriers, and the tanks are grounded, and have static dissipaters. There is a truck grounding area for trucks collecting condensate and/or produced water. Lightning protection and a windsock are installed on top of the production tanks. Production equipment on the well pad consisted of:

6 producing wells 8- 400 bbl production tanks, four labelled as containing fresh water, and four labelled as containing condensate 6 sand separators 6 gas processing units 1 low pressure vertical separator located inside of the dike 1 vapor recovery unit 1 horizontal separator, 1 compressor station 2 bullet tanks Jersey barriers are installed around the production equipment. The access road and man doors were locked. Drainage and erosion controls at the pad are in place and functioning. A closed-loop, above-ground drilling pit system was used, so there are no earthen pits requiring closure. The pad has a crushed limestone surface, and is in good repair. The lease road was stable in in good repair.

2077328686 2018-11-19 Production Wells No Violations The well was equipped with a plunger-lift assembly. The surface/intermediate and intermediate/production annular gauges displayed readings of zero psi. I performed a walk-around inspection of the pad and erosional controls appeared functioning. No violations were observed at the time of inspection.
332798325 2014-2-3 0:00:0 DD No Violations 5.00

For data sources see[9]

References